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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0046981
EISBN: 978-1-62708-218-1
... Abstract The exhaust valve of a truck engine failed after 488 h of a 1000 h laboratory endurance test. The valve was made of 21-2 valve steel in the solution treated and aged condition and was faced with Stellite 12 alloy. The failure occurred by fracture of the underhead portion of the valve...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047148
EISBN: 978-1-62708-235-8
... Abstract A connecting rod (forged from 15B41 steel and heat treated to a hardness of 29 to 35 HRC) from a truck engine failed after 73,000 Km (45,300 mi) of service. A piece of the I-beam sidewall of the rod, about 6.4 cm (2 in.) long, was missing when the connecting rod arrived at a laboratory...
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001119
EISBN: 978-1-62708-214-3
... was installed in a separate heavy truck engine in an application in which spring failure can cause total engine destruction. The springs were composed of chromium-silicon steel, with a hardness ranging from 50 to 54 HRC. Chemical composition and hardness were substantially within specification. Failure...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0046182
EISBN: 978-1-62708-218-1
... Abstract A connecting cap from a truck engine fractured after 65,200 km (40,500 mi) of normal service. The cap was made from a 15B41 steel forging and was hardened to 29 to 35 HRC. Visual examination of the fracture surface disclosed an open forging defect across one of the outer corners...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0001809
EISBN: 978-1-62708-180-1
... of cleanness, ideal clearance, and normal operating temperature of 80 to 105 °C (180 to 220 °F). Normal fatigue life of bearings is considered to be 161,000 km (100,000 miles) in gasoline automobile engines and 402,000 km (250,000 miles) in diesel truck engines. Electrical Erosion Some bearings...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001360
EISBN: 978-1-62708-215-0
... Abstract A blade from the engine cooling fan of a pickup truck fractured unexpectedly. The blade was made from type 301 stainless steel in the extra full hard tempered condition with a hardness of 47 HRC. Failure analysis indicated that the blade fractured in three modes: crack initiation...
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006806
EISBN: 978-1-62708-329-4
... degree of cleanness, ideal clearance, and normal operating temperature of 80 to 105 °C (180 to 220 °F). Normal fatigue life of bearings is considered to be 161,000 km (100,000 miles) in gasoline automobile engines and 402,000 km (250,000 miles) in diesel truck engines. Abrasive Wear Wear by dirt...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0047846
EISBN: 978-1-62708-218-1
... Abstract An 8640 steel shaft installed in a fuel-injection-pump governor that controlled the speed of a diesel engine used in trucks and tractors broke after few days of operation. The mechanism that drove the shaft was designed to include a slip clutch to protect the governor shaft from shock...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0089572
EISBN: 978-1-62708-218-1
... Abstract Two sand-cast low-alloy steel equalizer beams (ASTM A 148, grade 105-85) designed to distribute the load to the axles of a highway truck broke after an unreported length of service. Normal service life would have been about 805,000 km (500,000 mi) of truck operation. Investigation...
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006836
EISBN: 978-1-62708-329-4
... and operating stresses appeared to be within the material endurance limit ( Ref 7 ). Failure initiated from the spring inside coil surface; final fracture occurred in torsion. Helical compression springs are used in heavy truck engines. They may be subjected to corrosive environments, including exposure...
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006815
EISBN: 978-1-62708-329-4
... suspension with a kingpin mounted near vertically through the eye at each end of the axle. The yoke of each front wheel stub axle fits over the corresponding eye of the beam axle and around the kingpin, thereby forming the axis about which the stub axle can turn to steer the truck. Kingpins are normally...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003502
EISBN: 978-1-62708-180-1
... the axis about which the stub axle can turn in order to steer the truck. Kingpins are normally simple cylindrical hardened shafts extending out of the top and bottom of the axle eye into the top and bottom bearings of the stub axle yoke. A thrust bearing is fitted between the bottom of the axle eye...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001706
EISBN: 978-1-62708-217-4
... Abstract The truck beam of the left main landing gear (MGL) of a Boeing 707 airplane collapsed on the ground just after the aircraft was unloaded and refueled. The investigation revealed that failure was caused by the propagation of an intergranular crack originating from the bottom of the pit...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001139
EISBN: 978-1-62708-221-1
... Abstract A truck-mounted hydraulic crane had a horizontal thrust bearing with one race attached to the truck and the other to the rotating crane. The outside race of the bearing was driven by a pinion gear, and it is through this mechanism that the crane body rotated about a vertical axis...
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006833
EISBN: 978-1-62708-329-4
... to the condition of the bridge. Figure 1 is an illustration of stress that a bridge component may experience from the passage of a heavy truck superimposed on the nonchanging dead load. This cyclic loading can result in fatigue cracking. Fig. 1 Typical stress over time from passage of a truck. Source...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0001821
EISBN: 978-1-62708-180-1
.... and Viest I.M. , Fatigue Life of Bridge Beams Subjected to Controlled Truck Traffic , Preliminary publications , 7th Congress, International Association for Bridge and Structural Engineering, Zurich , 1964 4. Fisher J.W. , Hausammann H. , Sullivan M.D. , and Pense A.W...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001821
EISBN: 978-1-62708-241-9
... Abstract A fire in a storage yard engulfed several propane delivery trucks, causing one of them to explode. A series of elevated-temperature stress-rupture tears developed along the top of the truck-mounted tank as it was heated by the fire. Unstable fracture then occurred suddenly along...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001504
EISBN: 978-1-62708-217-4
... of the trends in failure mechanisms and causes. Case Histories Main Landing Gear Truck Beam of a Large Transport Aircraft A main landing gear truck beam from a large transport aircraft fractured on the ground just after refuelling as a result of a circumferential crack located about 0.14 m (5.5...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001307
EISBN: 978-1-62708-215-0
... of the vehicle had the letter “L” cast into it. The photograph in the figure was taken at a point in the investigation when two metallograhpic specimens had been cut from the broken hanger and one had been cut from the unbroken hanger from the other side of the vehicle. Fig. 1 An exemplar truck showing...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003505
EISBN: 978-1-62708-180-1
... on the right or left side of the road. Smith ( Ref 41 ) tells of a forklift truck that violated the fourth item. The left foot was used to depress a pedal that increased speed, and a brake was applied when the foot was lifted. Preventive Measures What are the implications of the previously...