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Steam reformers

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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001687
EISBN: 978-1-62708-220-4
... Abstract Microstructural examinations on transverse cross sections of a steam reformer tube, showed the presence of large macrovoids elongated in the radial direction and emanating from the internal surface of the tube. The macrovoids were located at the interdendritic regions, and were...
Image
Published: 01 June 2019
Fig. 1 Schematic of Incoloy 800 outlet-piping system for a steam-reformer unit showing the four welds that failed by cracking. Dimensions given in inches More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001738
EISBN: 978-1-62708-220-4
... (and thus the furnace) could be used safely during the foreseen production period. Ammonia Chemical processing equipment Manifolds Oxidation Steam reformers Incoloy 800H UNS N08810 Creep fracture/stress rupture DSM Fertilizers operates several production units in The Netherlands. One...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001328
EISBN: 978-1-62708-215-0
... Intergranular oxidation Mechanical properties Thermal stresses Tubing Weldments Incoloy 800H UNS N08810 Intergranular fracture Background Maintenance shutdown inspections regularly showed cracks in the welded outlet pigtail connections of a steam-methane reformer furnace. Applications...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046991
EISBN: 978-1-62708-234-1
... Abstract The outlet-piping system of a steam-reformer unit failed by extensive cracking at four weld locations. The welded system consisted of Incoloy 800 (Fe-32Ni-21Cr-0.05C) pipe and fittings. The exterior surfaces of the system were insulated with rock wool that did not contain...
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001108
EISBN: 978-1-62708-214-3
... Abstract The curved parts of exit pigtails made of wrought Incoloy 800H tubing used in steam reforming furnaces failed by performance after a period of service shorter than that predicted by the designers. Examination of a set of tubes consisting of both curved (perforated) and straight parts...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001590
EISBN: 978-1-62708-228-0
... Abstract This case study demonstrates that Alloy 601 (UNS N06601) is susceptible to strain-age cracking. The observation illustrates the potential importance of post weld heat treatment to the successful utilization of this alloy in certain applications. Steam reforming Inconel 601 UNS...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c0048719
EISBN: 978-1-62708-228-0
... branched cracking ( Fig. 1b ) and had originated from the inside surface. Transgranular branched cracking of austenitic stainless steels is frequently caused by chlorides in the presence of high residual stresses. The presence of chlorides is not unusual in a reformer unit. Although steam and steam...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0060144
EISBN: 978-1-62708-234-1
... Abstract Two steam-methane reformer furnaces were subjected to short-time heat excursions because of a power outage, which resulted in creep bulging in the Incoloy 800 outlet pigtails, requiring complete replacement. Each furnace had three cells, consisting of 112 vertical tubes per cell, each...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001735
EISBN: 978-1-62708-220-4
... of service. The outlet hydrogen-rich gas resulting from the cracking of naphtha in the presence of steam had a temperature of approximately 850°C, the inlet temperature at the top of the tubes being 525°C. Sections were cut from the tube, which was a spindle cast A297 Grade HK 40 (25 Cr, 20 Ni, 0.4 C...
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001107
EISBN: 978-1-62708-214-3
... the reformer furnace, waste heat is extracted by the production of steam within the waste heat boiler. If the reformer furnace is operating at lower temperatures, an internal bypass can be throttled open to reduce overall heat transfer. This bypass is protected by the alloy 800 liner. Circumstances Leading...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001330
EISBN: 978-1-62708-215-0
... experience a temperature peak in excess of 727 deg C (1340 deg F). The long-term overheating conditions could have been the result of excessive heat flux and /or inadequate steam flow. In addition, the entire superheater bank should have been upgraded to Grade 722 material at the time of retubing...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001341
EISBN: 978-1-62708-215-0
... Abstract An SB407 alloy 800H tube failed at a 100 deg bend shortly after startup of a new steam superheater. Three bends failed and one bend remote from the failure area was examined. Visual examination showed that the fracture started on the outside surface along the inside radius of the bend...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001675
EISBN: 978-1-62708-220-4
... and the temperature of the tube wall approximates the temperature of the product. The operating conditions of the reformer furnace are: Charge: natural gas, steam, and CO 2 Temperature of charge at entrance to reformer: 510 C Skin temperature of the manifold: 800–820 C Product temperature at furnace...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0001817
EISBN: 978-1-62708-180-1
... combustion gases, steam, or water to gases, vapors, or liquids of various types. Heat exchangers are of tube, plate, or sheet construction. Tubular heat exchangers are generally used for large fluid systems, whereas heat exchangers of plate or sheet construction are often preferred for smaller fluid streams...
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006813
EISBN: 978-1-62708-329-4
... exchangers are used to transfer heat from/to combustion gases and steam or water to/from gases, vapors, or liquids of various types where, for example, the effluent is used to heat the incoming stream or external water cools the reactant steam. A great variety of heat-exchanger designs have been used...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001771
EISBN: 978-1-62708-241-9
... section of ruptured tube A mixture of gas, air and steam that promotes the formation of surface oxide layer is commonly used as decoking gas in petrochemical plants. In coking/decoking cycles, tubes are subjected to thermal fatigue and deposited coke swept away by decoking gas [ 3 ]. After long...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0001818
EISBN: 978-1-62708-180-1
... to wrought Monel pipe. Metallographic examination disclosed many small microfissures in the weld metal, but no microfissures were found in the HAZs of the wrought Monel. This section of line contained high thermal stresses that resulted from injection of steam a short distance upstream from the coupling...
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001043
EISBN: 978-1-62708-214-3
... and oxidation Background A 76 mm (3 in.) diam stainless steel tube that was used as a heat shield and water nozzle support in a hydrogen gas plant quench pot failed in a brittle manner. Applications Natural gas and steam are reacted at high temperatures of 870 to 925 °C (1600 to 1700 °F...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003555
EISBN: 978-1-62708-180-1
... and productivity of processes within numerous industries. These include petrochemical processing (processes involving steam reforming of methane or natural gas, such as ammonia and methanol production), direct iron-ore reduction, coal degasification, and heat treating. Fig. 1 Metal dusting attack...