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Search Results for St 145/160

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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001221
EISBN: 978-1-62708-219-8
... Abstract During the construction of a prestressed concrete viaduct, several 12.2 mm diam wires ruptured after tensioning but before the channels were grouted. They were made of heat treated prestressed concrete steel St 145/160. While the wire bundles, each containing over 100 wires, were being...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0001819
EISBN: 978-1-62708-180-1
... prosthesis; metal against metal (G.E.U.P.A.R.). (f) Sliding knee joint prosthesis; metal against plastic (Geomedic). (g) Total shoulder joint prosthesis; metal against plastic (St. Georg). (h) Total finger joint prosthesis with metal and plastic components (St. Georg). (i) Total elbow joint prosthesis; metal...
Series: ASM Handbook
Volume: 11B
Publisher: ASM International
Published: 15 May 2022
DOI: 10.31399/asm.hb.v11B.a0006924
EISBN: 978-1-62708-395-9
... rate of 10 °C/min (18 °F/min) for an epoxy-amine cured isothermally at 160 °C (320 °F). d H/ dt , measured heat flow; T g , glass transition temperature; ΔH res , residual heat of reaction; ΔH rxn , heat of reaction. Source: Ref 26 Figure 12 shows a series of DSC temperature scans...
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006788
EISBN: 978-1-62708-295-2
... to cultures of SRB isolated from oilfield waters ( Ref 78 ). It has been noted that hydrogen permeation through steel under cathodic protection (CP) in artificial seawater was greater for a mixed culture of bacteria producing 160 mg/L sulfide than it was for the same concentration of sulfide under abiotic...
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006787
EISBN: 978-1-62708-295-2
... of service of burning solid waste. The root cause of the failure was overfiring during startup and sulfidation of the nickel-base alloy. Figure 3 shows the perforation of the liner near a patch made of alloy 160. The original wall was 6.35 mm (0.250 in.) and was reduced to 1.27 mm (0.050 in.) thickness...
Series: ASM Handbook
Volume: 11B
Publisher: ASM International
Published: 15 May 2022
DOI: 10.31399/asm.hb.v11B.9781627083959
EISBN: 978-1-62708-395-9
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006831
EISBN: 978-1-62708-329-4
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.9781627083294
EISBN: 978-1-62708-329-4