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Spiking
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0089651
EISBN: 978-1-62708-235-8
... etched 300x magnification) supported the conclusion that the rocker levers failed in fatigue, with casting defects, or spiking, acting as stress raisers to initiate failures in highly loaded engine tests. Recommendations included shot peening of the levers as an interim measure to reduce the possibility...
Abstract
Several diesel-engine rocker levers (malleable iron similar to ASTM A 602, grade M7002) failed at low hours in overspeed, over-fuel, highly loaded developmental engine tests. Identical rocker levers had performed acceptably in normal engine tests. The rocker levers were failing through the radius of an adjusting screw arm. The typical fracture face exhibited two distinct modes of crack propagation: the upper portion indicated overload at final fracture, whereas the majority of the fracture suggested a fatigue fracture. Investigation (visual inspection, 1.5x/30x/60x magnification, and nital etched 300x magnification) supported the conclusion that the rocker levers failed in fatigue, with casting defects, or spiking, acting as stress raisers to initiate failures in highly loaded engine tests. Recommendations included shot peening of the levers as an interim measure to reduce the possibility of failure and redesign to increase the cross-sectional area of the levers.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001376
EISBN: 978-1-62708-215-0
... Abstract An AISI 9260 steel railroad spike maul failed after a relatively short period of service. The maul head fractured in two pieces when struck against a rail. Visual, fractographic, metallographic, and chemical analyses were conducted on sections taken from the maul head, which was found...
Abstract
An AISI 9260 steel railroad spike maul failed after a relatively short period of service. The maul head fractured in two pieces when struck against a rail. Visual, fractographic, metallographic, and chemical analyses were conducted on sections taken from the maul head, which was found to have fractured across both sides of the eye. Failure occurred in at least three separate events: formation of two cracks immediately adjacent to the eye, extension of one of the original cracks over a portion of one of the eye sides, and abrupt extension of the original crack across the eye sides, resulting in separation into two halves.
Image
Published: 01 January 2002
Fig. 46 Section through a spiking defect in rocker lever similar to that shown in Fig. 45 . (a) 30×. (b) 60×
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Image
Published: 01 January 2002
Fig. 47 Microstructure at and near the spiking defect shown in Fig. 46 . (a) Heavy oxidation within an interdendritic void. As-polished. (b) Partial decarburization of the tempered martensitic matrix adjacent to a spiking defect. Etched with nital. Both 300×
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Image
Published: 01 January 2002
Fig. 59 A spiking defect in a centerline section at the root of an electron beam weld. The partial-penetration weld was made in 75 mm (3 in.) thick Ti-6Al-4V titanium alloy plate. 1.6×
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Image
in Fatigue Failure of Malleable Iron Diesel-Engine Rocker Levers Originating at Spiking Defects
> ASM Failure Analysis Case Histories: Processing Errors and Defects
Published: 01 June 2019
Fig. 2 Section through a spiking defect in rocker lever similar to that shown in Fig. 45. (a) 30x. (b) 60x
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in Fatigue Failure of Malleable Iron Diesel-Engine Rocker Levers Originating at Spiking Defects
> ASM Failure Analysis Case Histories: Processing Errors and Defects
Published: 01 June 2019
Fig. 3 Microstructure at and near the spiking defect shown in Fig. 46. (a) Heavy oxidation within an interdendritic void. As-polished. (b) Partial decarburization of the tempered martensitic matrix adjacent to a spiking defect. Etched with nital. Both 300x
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Image
in Thermomechanical Fatigue—Mechanisms and Practical Life Analysis
> Failure Analysis and Prevention
Published: 15 January 2021
Fig. 6 (a) Cross section near the fracture surface of a single-crystal nickel-base superalloy tested in thermomechanical fatigue (TMF) conditions. Note the oxide spike emanating from the fracture surface and the oxidized slip planes. The oxide spike occurs along an active slip plane
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Image
Published: 01 December 1993
Fig. 3 Characteristic features of explosive damage. (a) Reverse slant. (b) Curl. (c) Curved fragment. (d) Dent. (e) Spall. (f) Petaling and curling around a hole. (g) Spikes. (h) Craters. (i) Nondescript fragments.
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Image
in Thermomechanical Fatigue—Mechanisms and Practical Life Analysis
> Failure Analysis and Prevention
Published: 15 January 2021
Fig. 4 Cross section of a nickel-base superalloy after thermomechanical fatigue testing. Image shows surface oxidation at bottom and oxide spike forming in the center of the specimen. Chemical etchant used highlights aluminum in the microstructure. Microstructure shown as white in image
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Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001290
EISBN: 978-1-62708-215-0
... the disintegrated wastepaper receptacle. Fig. 3 Characteristic features of explosive damage. (a) Reverse slant. (b) Curl. (c) Curved fragment. (d) Dent. (e) Spall. (f) Petaling and curling around a hole. (g) Spikes. (h) Craters. (i) Nondescript fragments. Some of the fragments from the wastepaper...
Abstract
Damage to a passenger aircraft that resulted from a midair explosion and subsequent emergency landing was investigated to determine the cause and location of the explosion. Extensive damage had occurred in the front toilet and cockpit areas and to the undercarriage and underside of the aircraft. Fractographic and surface examination of metal fragments (stainless steel and aluminum alloy) from damaged areas indicated that the accident was caused by an explosion in the front toilet. A reconstruction exercise confirmed this conclusion. Damage to the undercarriage and underside resulted from the emergency landing.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001144
EISBN: 978-1-62708-217-4
.... Fractographic analysis of the fractures by scanning electron microscopy revealed striations typical of fatigue, as shown in Fig. 3 . Each striation usually corresponds to a single load cycle ( 1 , 2 , 3 ). The striation pattern indicated random loading with additional distinct spike load indications...
Abstract
A helicopter was hovering approximately 10 ft above a ship when one spar section failed explosively. Visual inspection revealed a crack had progressed through one member of a dual spar plate assembly at a fold pin lug hole. The remaining spar plate carried the blade load until the aircraft was landed. The helicopter main rotor blade spar fracture was analyzed by conventional and advanced computerized fractographic techniques. Digital fractographic Imaging Analysis of theoretical and actual fracture surfaces was applied for automatic detection of fatigue striation spacing. The approach offered a means of quantification of fracture features, providing for objective fractography.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001639
EISBN: 978-1-62708-229-7
... mapping data collected on a carbon steel cooling water pipe with actual corrosion at a liquid to vapor interface. The image also shows pitting and corrosion patterns typical of actual wall loss, as well as noise spikes (also known as data dropout ). The noise spikes are noted with arrows in the top...
Abstract
This paper describes the remote ultrasonic (UT) examinations of a high-level radioactive waste storage tank at the Savannah River Site in South Carolina. The inspections, carried out by E.R. Holland, R.W. Vande Kamp, and J.B. Elder, were performed from the contaminated, annular space of the 46 year old, inactive, 1.03 million gallon waste storage tank. A steerable, magnetic wheel wall crawler was inserted into the annular space through small (6 in., or 150 mm, diam) holes/risers in the tank top. The crawler carried the equipment used to simultaneously collect data with up to four UT transducers and two cameras. The purpose of this inspection was to verify corrosion models and to investigate the possibility of previously unidentified corrosion sites or mechanisms. The inspections included evaluation of previously identified leak sites, thickness mapping, and crack detection scans on specified areas of the tank. No indications of reportable wall loss or pitting were detected. All thickness readings were above minimum design tank-wall thickness, although several small indications of thinning were noted. The crack detection and sizing examinations revealed five previously undetected indications, four of which were only partially through-wall. The cracks that were examined were found to be slightly longer than expected but still well within the flaw size criteria used to evaluate tank structural integrity.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001749
EISBN: 978-1-62708-215-0
... nights. Close examination of the threaded interface ( Fig. 2 ) clearly indicated use of this adhesive, which is unacceptable for oxygen systems. Fig. 2 Closeup view of brass-to-steel joint, showing heavy wrench marks on nipple and puddled adhesive at threaded joint. 4.6×. Evidence of spikes...
Abstract
An oxygen line that was part of a mobile, truck -mounted oxygen-acetylene welding unit exploded in service. Analysis revealed that the failure occurred at the flexible hose-to-valve connection. It was further determined that a steel adapter had been installed at the point of failure to make the connection. Use of the adapter which joined with a brass nipple, created an unacceptable dissimilar metal joint. The steel also provided a source for the generation of sparks. Loctite, a hydrocarbon sealant that is highly flammable and explosive in contact with pure oxygen, had been used to seal the threaded joint. It was recommended that only brass fittings be used to assemble removable joints and that use of washers, sealants, and hydrocarbon lubricants be strictly avoided.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003566
EISBN: 978-1-62708-180-1
... and spalling of various railroad percussion tools. The ultimate goal of the program at Conrail was to reduce maintenance-of-way employee injuries. The HIT is a simple electropneumatic machine that is able to repeatedly strike an anvil with a hammer or spike maul. The end of the striking-tool handle is fitted...
Abstract
This article briefly reviews the analysis methods for spalling of striking tools with emphasis on field tests conducted by A.H. Burn and on the laboratory tests of H.O. McIntire and G.K. Manning and of J.W. Lodge. It focuses on the metallography and fractography of spalling. The macrostructure and microstructure of spall cavities are described, along with some aspects of the numerous specifications for striking/struck tools. The article also describes the availability of spall-resistant metals and the safety aspects of striking/struck tools in railway applications.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001344
EISBN: 978-1-62708-215-0
... of the upset, a sudden spike in the boiler water pH (from 9.5 to 11.8) was recorded. There was no warning of excessive sodium content in the steam because the sodium analyzer was not operative. Within hours after the first indication of the caustic upset, a large differential between the feedwater flow...
Abstract
Several 304H stainless steel superheater tubes fractured in stressed areas within hours of a severe caustic upset in the boiler feedwater system. Tests performed on a longitudinal weld joint, which connected two adjacent tubes in the tertiary superheater bank, confirmed caustic-induced stress-corrosion cracking, promoted by the presence of residual welding stresses. Improved maintenance of check valves and routine inspection of critical monitoring systems (conductivity alarms, sodium analyzers, etc.) were recommended to help avoid future occurrences of severe boiler feedwater contamination. Additional recommendations were to eliminate these short longitudinal weld joints by using a bracket assembly joint between the tubes, use a post-weld heat treatment to relieve residual welding stress or select a more stress-corrosion cracking resistant alloy for this particular application.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001634
EISBN: 978-1-62708-221-1
... had been in service for approximately 6 months prior to the failure, and the site had a policy of replacing critical hoses every 10,000 h (approximately 2 years) of operation. The nominal operating pressure of the hose was approximately 34.5 MPa (5000 psi), with the possibility of spike pressures...
Abstract
The boom lift equalizer hose on an excavator failed and the resultant release of high-pressure hydraulic fluid damaged the operator cabin. The hose was a heavy duty, high-impulse, multiple-spiral wire-reinforced, rubber covered hydraulic hose equivalent to 100R13 specifications as set in AS3791-1991. It had a maximum operating pressure of 34.5 MPa (5000 psi). The failure occurred adjacent to one of the couplings, although some of the wire strands had not broken. The two outer layers of reinforcement wire on the failed end had experienced extensive corrosion, corroding away completely in most areas. This corrosion was fairly uniform around the circumference of the hose. The loss of two spirals/layers of wire reinforcement effectively reduced the pressure carrying capacity of the hose to below that of the maximum operational pressure experienced. Either the hose (or assembly) was already corroded prior to being fitted, or, the hose experienced aggressive conditions causing rapid corrosion of the exposed wire strands.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001635
EISBN: 978-1-62708-221-1
... the maximum in-service operating pressures and spike pressure conditions. This corrosion was primarily caused by the protective outer covering being broken and allowing the ingress of water to the wire strands in a relatively isolated region. This was most likely due to mechanical damage in the form...
Abstract
A hoist lift hose on a loader failed catastrophically. The hoses were a 100R13 type (as classified in AS3791-1991) with 50.8 mm nominal internal diameter. They consisted of six alternating spirals of heavy wire around a synthetic rubber inner tube with a synthetic rubber outer sheath. Failure of the lift hose was approximately 50 to 100 mm away from the "upper" end of the hose, with the straight coupling that attaches to the hydraulic system. The return hose was in much better condition, with no apparent deformation and only small areas of mechanical damage to the outer sheath. There were two modes of failure of the wire: tensile and corrosion related. The predominant corrosion mechanism appeared to be crevice corrosion related, with the corrosion being driven by the retention of water by the cover material around the wire strands. In this case study (and in most wire-reinforced hydraulic hoses), the wire reinforcing strands were a medium-carbon steel in the cold drawn condition. Radiographic nondestructive testing (NDT) was recommended to determine when a hydraulic hose should be replaced.
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006781
EISBN: 978-1-62708-295-2
... aluminum. The portions of the material exposed to air, including the oxide spike shown at the center, are devoid of aluminum, and the microstructure appears white as a result. The aluminum that once resided in the microstructure shown as white in the image has diffused to the surface to create an aluminum...
Abstract
Thermomechanical fatigue (TMF) is the general term given to the material damage accumulation process that occurs with simultaneous changes in temperature and mechanical loading. TMF may couple cyclic inelastic deformation accumulation, temperature-assisted diffusion within the material, temperature-assisted grain-boundary evolution, and temperature-driven surface oxidation, among other things. This article discusses some of the major aspects and challenges of dealing with TMF life prediction. It describes the damage mechanisms of TMF and covers various experimental techniques to promote TMF damage mechanisms and elucidate mechanism coupling interactions. In addition, life modeling in TMF conditions and a practical application of TMF life prediction are presented.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001686
EISBN: 978-1-62708-220-4
... the coil to either single phase liquid, bubbly flow, slug flow or the annular flow regime causing liquid to be in contact with the tube wall. The tube metal temperature spike occurs on the fireside of the coil - i.e. coil inner diameter because of the higher heat flux on the fireside of the tube. High...
Abstract
A root cause failure analysis was performed on a vaporizer coil removed from a horizontal forced circulation vaporizer. The carbon steel coil was wound in a right-hand helix with a coil centerline diameter of about 2 m. The vaporizer was gas fired and used Dowtherm A as the heat transfer fluid. Design conditions are based on annular fluid flow to cool the coil wall. NDE, metallographic and fractographic examinations were performed. Numerous, circumferentially oriented, OD initiating cracks were found near the crown for two coils near the non-fired end of the vaporizer. The cracking was confined to the inner diameter of the vaporizer coil at positions from 4:00 to 7:00. The cracking was characterized as transgranular and the fracture surface had beach marks. The failure mechanism was thermal fatigue. The heat transfer calculation predicted that dryout of the coil would occur for coils at the non-fired end of the vaporizer during low flow transients. Dryout results in rapid increase in the tube wall temperature. Thermal cycling of the coil is completed by liquid quenching resulting from resumption of normal flow rates and the return to annular flow. The probable root cause of failure was low flow transient operation.
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