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Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001309
EISBN: 978-1-62708-215-0
.... The selected redesign configuration consisted of a 4.8-mm (0.188-in.) plate on the side of the frame from the swing arm stub to the axle. This configuration, shown in Fig. 4 , effectively reduced stresses in the upper and lower tubes. The highest stress was 2.14 MPa (310 psi), and was located on the lower...
Abstract
Bending fatigue caused crack propagation and catastrophic failures at several locations near the welds on the low-carbon steel tubular cargo box frame of police three-wheel motorcycles. ANSYS finite element analysis revealed that bending stresses in some of the frame members were aggravated by poor detail design between vertical and horizontal tubes. Stresses observed in the ANSYS analysis were not sufficient to cause the onset of fatigue. However when compounded by stress concentration factors and in-service dynamic loading, the frame could have been regularly subjected to stresses over the fatigue limit of the material. A strain gage static loading test verified FEM results, and finite element techniques were applied in the design of reinforcing members to renovate the frames. Material properties were determined and welding procedures specified for the reinforcing members. Inspection intervals were devised to avoid future problems.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0001784
EISBN: 978-1-62708-218-1
... Abstract Field fatigue failures occurred in a hand-operated gear shift lever mechanism made of 1049 medium carbon steel hardened to 269 to 285 HB. The failures occurred in the 3.18 mm (0.127 in.) radius. Redesign increased the shift lever's diameter to 25 mm (1 in.) and the radius to 4.75 mm...
Abstract
Field fatigue failures occurred in a hand-operated gear shift lever mechanism made of 1049 medium carbon steel hardened to 269 to 285 HB. The failures occurred in the 3.18 mm (0.127 in.) radius. Redesign increased the shift lever's diameter to 25 mm (1 in.) and the radius to 4.75 mm (0.187 in.). Also, instead of the as-forged surface, it was expedient to machine the radius. The as-forged surface at 360 MPa (52 ksi) maximum working stress would not ensure satisfactory life because the recalculated maximum stress was 390 MPa (57 ksi). However, the machined surface with a maximum working stress of 475 MPa (69 ksi) gives a safe margin above the 390 MPa (57 ksi) requirement for design stress. Interpreting these values, the forged surface should have a life expectancy of 1,000,000 cycles of stress. However, because the load cycle was somewhat uncertain, the machined radius was chosen to obtain a greater margin of safety. Redesigning eliminated the failures.
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Published: 01 January 2002
Fig. 13 Redesign of a casting to avoid waterfalling. (a) In this design, waterfalling results when casting is filled from the bottom. (b) Improved design provides a path for the metal to follow as it fills the mold.
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Published: 01 January 2002
Fig. 32 Redesign of castings to provide progressive solidification through the use of tapered walls. (a) Elbow design. (b) Valve fitting design. Source: Ref 31
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Published: 30 August 2021
Fig. 12 Redesign of castings to provide progressive solidification through the use of tapered walls. (a) Elbow design. (b) Valve fitting design. Source: Ref 15
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001522
EISBN: 978-1-62708-235-8
... Abstract In the EMD-2 Joint Directed Attack Munition (JDAM), the A357 aluminum alloy housing had been redesigned and cast via permanent mold casting, but did not meet the design strength requirements of the previous design. Mechanical tests on thick and thin sections of the forward housing...
Abstract
In the EMD-2 Joint Directed Attack Munition (JDAM), the A357 aluminum alloy housing had been redesigned and cast via permanent mold casting, but did not meet the design strength requirements of the previous design. Mechanical tests on thick and thin sections of the forward housing assembly revealed tensile properties well below the allowable design values. Radiology and CT evaluations revealed no casting defects. Optical microscopy revealed porosity uniformly distributed throughout the casting on the order of 0.1 mm pore diam. Scanning electron microscopy revealed elongated pores, which indicated turbulent filling of the mold. Spherical pores would have indicated the melt had been improperly degassed. Based on these findings, it was recommended that the manufacturer analyze and redesign the gating system to eliminate the turbulent flow problem during the permanent mold casting process.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0091622
EISBN: 978-1-62708-230-3
...-SCC in an area of debris buildup. It appeared the original casting suffered SCC in a low-oxygen area high in chlorides from repeated wet/dry cycles where there was a buildup of debris. Recommendations included redesigning the neck liner to eliminate the abrupt change where there was debris buildup...
Abstract
A CF-8M (cast type 316) neck liner or manway was removed from the top of a digester vessel. Repeated attempts to repair the part in the field during its life cycle of many years had failed to keep the unit from leaking. The casting was a CF-8M modified with the molybdenum level at the top end of the range. The plate was standard 317L material. The filler metal was type 316, although marginal in molybdenum content. Investigation (visual inspection, chemical analysis, micrographs, and metallographic examination) supported the conclusion that the damage to the neck liner was due to Cl-SCC in an area of debris buildup. It appeared the original casting suffered SCC in a low-oxygen area high in chlorides from repeated wet/dry cycles where there was a buildup of debris. Recommendations included redesigning the neck liner to eliminate the abrupt change where there was debris buildup. If redesign was impossible, an alloy more resistant to Cl-SCC, such as a duplex stainless steel or a high-molybdenum (4 to 6%) austenitic stainless steel, should be used.
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in Fatigue Fracture of a C130 Aircraft Main Landing Gear Wheel Flange
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1992
Fig. 2 Schematic of the redesigned C130 aircraft main landing gear wheel, showing the double flange used to strengthen the wheel.
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in Brittle Fracture of a Rephosphorized, Resulfurized Steel Check-Valve Poppet
> ASM Failure Analysis Case Histories: Mechanical and Machine Components
Published: 01 June 2019
Fig. 1 Check-valve poppet that was redesigned to eliminate breakage in service caused by the pressure of nonmetallic inclusions in a rephosphorized, resulfurized steel. (a) Original design of the poppet showing origin of fracture and subsequent complete fracture between two opposing holes
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in Fatigue Fracture of an Aluminum Alloy 7075-T73 Landing-Gear Torque Arm
> ASM Failure Analysis Case Histories: Air and Spacecraft
Published: 01 June 2019
Fig. 1 Aluminum alloy 7075-T73 landing-gear torque-arm assembly that was redesigned to eliminate fatigue fracture at a lubrication hole. (a) Configuration and dimensions (given in inches). (b) Fracture surface showing fatigue beach marks. Approximately 2×
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0046160
EISBN: 978-1-62708-224-2
.... Axial shift of the crane wheel during operation, because of insufficient interference fit, was the major cause of fatigue cracking. Recommendations included redesigning the axle to increase the critical diameter from 140 to 150 mm (5.5 to 6 in.) and to add a narrow shoulder to keep the drive wheel from...
Abstract
A stepped drive axle (hardened and tempered resulfurized 4150 steel forging) used in a high-speed electric overhead crane (rated at 6800 kg, or 7 tons, and handling about 220 lifts/day with each lift averaging 3625 to 5440 kg, or 4 to 6 tons) broke after 15 months of service. Visual examination of the fracture surface revealed three fracture regions. The primary fracture occurred approximately 50 mm (2 in.) from the driven end of the large-diam keywayed section on the stepped axle and approximately 38 mm (1 in.) from one end of the keyway where the crane wheel was keyed to the axle. Macroscopic, microscopic, and chemical examination revealed composition that was basically within the normal range for 4150 steel. This evidence supports the conclusion that cracking initiated at a location approximately opposite the keyway, and final fracture was due to mixed ductile and brittle fracture. Axial shift of the crane wheel during operation, because of insufficient interference fit, was the major cause of fatigue cracking. Recommendations included redesigning the axle to increase the critical diameter from 140 to 150 mm (5.5 to 6 in.) and to add a narrow shoulder to keep the drive wheel from shifting during operation.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001032
EISBN: 978-1-62708-214-3
... the heat flux, redesigning the wick, and reducing the oxygen content of the sodium. Engine components Evaporators Fins Solar power generation Space flight Stirling engines 316 UNS S31600 Inconel 600 UNS N06600 Intergranular fracture Intergranular corrosion High-temperature corrosion...
Abstract
A Stirling engine heat pipe failed after only 2h of operation in a test situation. Cracking at the leading edge of an evaporator fin allowed air to enter the system and react with the sodium coolant. The fin was fabricated from 0.8 mm (0.03 in.) thick Inconel 600 sheet. The wick material was type 316 stainless steel. Macro- and microexaminations of specimens from the failed heat pipe were conducted. The fin cracking was caused by overheating that produced intergranular corrosion in both the fin and the wick. Recommendations for alleviating the corrosion problem included reducing the heat flux, redesigning the wick, and reducing the oxygen content of the sodium.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001052
EISBN: 978-1-62708-214-3
... degree of titanium-base stringers. Wall thickness was about 0.15 mm (0.006 in.) underside. It was concluded that the high vane pass frequency excited the natural vibration of the bellows to a higher resonance and cracked the bellows after a relatively short service period. The assembly was redesigned...
Abstract
A failure analysis was conducted to determine the cause of recurring failure of flexible bellows in an exhaust hose assembly. The bellows were made of type 321 stainless steel. Visual examination showed that cracks followed a path along the seam weld in the bellows. Most of the cracks followed a multidirectional/circular pattern, occasionally chipping off the convolutions, an indication of high-resonance fatigue-type cracking. Scanning electron fractography showed fatigue striations throughout the fracture surface. The microstructure consisted of relatively large grains and an abnormal degree of titanium-base stringers. Wall thickness was about 0.15 mm (0.006 in.) underside. It was concluded that the high vane pass frequency excited the natural vibration of the bellows to a higher resonance and cracked the bellows after a relatively short service period. The assembly was redesigned, and no further cracking occurred.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001071
EISBN: 978-1-62708-214-3
... body juncture be redesigned to reduce stress levels. A method of maintenance and inspection in concert with a criterion for life prediction for this and other valves and components in the system was also recommended. Chemical processing equipment Gatevalves Sulfuric acid, environment Gray iron...
Abstract
A gray cast iron (ASTM 247 type A) gate valve in an oleum and sulfuric acid piping loop at a chemical process plant fractured catastrophically after approximately 10 years of service. The valve was a 150 mm (6 in.) bolted flange type rated to conform to ANSI B16.1 for service at 1034 kPa (150 psi) and 120 deg C (250 deg F) maximum in 93 to 99% sulfuric acid. The fracture originated at stress-corrosion cracks that occurred in a high-stress transition region at the valve body-to-flange juncture. The mechanical properties of the failed valve were below those of the manufacturer's cited specification, and the wall thickness through which the fracture occurred exceeded the minimum 9.5 mm (38 in.) thickness cited by the manufacturer The valve flange had been unbolted and rebolted to a maintenanced piping coil immediately prior to failure. It was recommended that the flange-to-valve body juncture be redesigned to reduce stress levels. A method of maintenance and inspection in concert with a criterion for life prediction for this and other valves and components in the system was also recommended.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001074
EISBN: 978-1-62708-214-3
... of shrinkage cavities, which lowered the load-bearing capability. The failure occurred at the location where there was an abrupt change in the section thickness. A redesign to provide a smooth contour at the section junction was recommended along with optimization of casting parameters to avoid shrinkage...
Abstract
A cast housing, part of a multi-shaft yoking mechanism, failed during assembly and installation of the equipment in which it was to be used. The housing, or yoke body, was cast from AISI 420 grade ferritic stainless steel. Analysis revealed that the failure was caused by the presence of shrinkage cavities, which lowered the load-bearing capability. The failure occurred at the location where there was an abrupt change in the section thickness. A redesign to provide a smooth contour at the section junction was recommended along with optimization of casting parameters to avoid shrinkage cavities.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001080
EISBN: 978-1-62708-214-3
... was responsible for the loosening of the nut. It was recommended that the locking mechanism be redesigned and changed in all existing turbines. Locking Nuts (fasteners) Turbine disks Turbine steel (Other, miscellaneous, or unspecified) failure Background A290 mm (10 in.) diam horizontal steam...
Abstract
A steam turbine developed excessive noise and vibration during routine operation. It was found that the nut that locked the turbine disk In place had worked its way out from the threads and the disk had come of the shaft. Examination of the locking mechanism indicated that its design was responsible for the loosening of the nut. It was recommended that the locking mechanism be redesigned and changed in all existing turbines.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001082
EISBN: 978-1-62708-214-3
... of solutions involving material selection and impeller redesign were recommended. Castings Chlorides, environment Propellers Repair welding Vibratory stresses 304L UNS S30403 Stress-corrosion cracking Fatigue fracture Background Several large-diameter impeller/propeller blades...
Abstract
Several large-diameter type 304L stainless steel impeller/propeller blades in a circulating water pump failed after approximately 8 months of operation. The impeller was a single casting that had been modified with a fillet weld buildup at the blade root. Visual examination indicated that the fracture originated near the blade-to-hub attachment in the area of the weld buildup. Specimens from four failed castings and from an impeller that had developed cracks prior to design modification were subjected to a complete analysis. A number of finite-element-method computer models were also constructed. It was determined that the blades failed by fatigue that had been accelerated by stress-corrosion cracking. The mechanism of failure was flow-induced vibration, in which the vortex-shedding frequencies of the blades were attuned to the natural frequency of the blade/hub configuration. A number of solutions involving material selection and impeller redesign were recommended.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001286
EISBN: 978-1-62708-215-0
... that yields a compressive residual stress in the fillet, appropriate heat treatment of stamped discs, or redesign of the disc and/or transmission assembly was recommended. Mechanical transmissions Residual stress Stampings Stress concentration Winches 1015 UNS G10150 Fatigue fracture...
Abstract
Failure of AISI 1015 steel brake discs used in power transmissions in emergency winches was investigated using various testing methods. The failed discs were stampings that had replaced cast discs. Residual stresses in the fillets of new cast and new stamped brake discs were measured by x-ray diffraction. The results indicated that the stamped brake discs had failed by fatigue caused by a tensile residual stress pattern in the fillet. The residual stress pattern was attributed to the change in manufacturing process from casting to stamping. Use of a manufacturing process that yields a compressive residual stress in the fillet, appropriate heat treatment of stamped discs, or redesign of the disc and/or transmission assembly was recommended.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001267
EISBN: 978-1-62708-215-0
... marks on the inside edge of the spring. An investigation of loads encountered in service indicated that the springs had been loaded to a large fraction of the yield strength. Redesign of the spring mechanism was recommended. Springs (elastic) Woody fracture ASTM A228 UNS K08501 Fatigue...
Abstract
Music wire springs used in a printer return mechanism failed near the bend in the hook portion of the spring during qualification testing. Samples were examined in a scanning electron microscope equipped with an energy-dispersive x-ray microprobe. Fatigue fractures originated at rub marks on the inside edge of the spring. An investigation of loads encountered in service indicated that the springs had been loaded to a large fraction of the yield strength. Redesign of the spring mechanism was recommended.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001005
EISBN: 978-1-62708-215-0
..., revealed that fatigue crack initiation occurred from the tip of oxide scale inclusions forged into the U-shaped arm at the inside radius. Corrective action involved redesigning the steering arm to increase the minimum forging radius and reduce the stress level at the inner-bend radius, and reducing...
Abstract
Several heavy truck Cr-Mo steel steering arms in service less than three years fractured during stationary or low-speed turning maneuvers that required power-assisted steering. Metallographic examination of the cracked AISI 4135 arms, heat treated to a hardness of 285 to 341 HB, revealed that fatigue crack initiation occurred from the tip of oxide scale inclusions forged into the U-shaped arm at the inside radius. Corrective action involved redesigning the steering arm to increase the minimum forging radius and reduce the stress level at the inner-bend radius, and reducing the level of power assistance to the wheels to encourage the driver to put the vehicle in motion prior to turning.
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