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Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006837
EISBN: 978-1-62708-329-4
... Abstract Because of the tough engineering environment of the railroad industry, fatigue is a primary mode of failure. The increased competitiveness in the industry has led to increased loads, reducing the safety factor with respect to fatigue life. Therefore, the existence of corrosion pitting...
Abstract
Because of the tough engineering environment of the railroad industry, fatigue is a primary mode of failure. The increased competitiveness in the industry has led to increased loads, reducing the safety factor with respect to fatigue life. Therefore, the existence of corrosion pitting and manufacturing defects has become more important. This article presents case histories that are intended as an overview of the unique types of failures encountered in the freight railroad industry. The discussion covers failures of axle journals, bearings, wheels, couplers, rails and rail welds, and track equipment.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c9001585
EISBN: 978-1-62708-231-0
... Abstract On 15 March 2000, a National Railroad Passenger Corporation (Amtrak) train traveling from Chicago to Los Angeles derailed in Carbondale, KS. After the initial on-scene investigation, 12 pieces of rail were sent to the materials laboratory for examination. Ten of them were from...
Abstract
On 15 March 2000, a National Railroad Passenger Corporation (Amtrak) train traveling from Chicago to Los Angeles derailed in Carbondale, KS. After the initial on-scene investigation, 12 pieces of rail were sent to the materials laboratory for examination. Ten of them were from the point of derailment (POD). A vertical crack was observed in the head of the rail (vertical split head). The crack was at least 233 in. (591 cm) long, continuing through the entire lengths of most pieces recovered from the POD. The vertical fracture surface had features consistent with overstress fracture with short-term exposure to an oxygen-rich environment. Fracture features emanated from longitudinally-aligned inclusions rich in aluminum.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c9001531
EISBN: 978-1-62708-231-0
... to the performance of cartwheel. Dynamic fracture toughness Fatigue property Performance evaluation Railroad wheels Static mechanical property Fe-0.55C-0.73Mn Fe-0.60C-0.85Mn Fe-0.5C-0.7Mn Rolling-contact wear Spalling wear Fatigue fracture 1. Introduction The railway system in China plays...
Abstract
In this study, the failure modes of cartwheel and mechanical properties of materials have been analyzed. The results show that rim cracking is always initiated from stringer-type alumina cluster and driven by a combination effect of mechanical and thermal load. The strength, toughness, and ductility are mainly determined by the carbon content of wheel steels. The fatigue crack growth resistance is insensitive to composition and microstructure, while the fatigue crack initiation life increases with the decrease of austenite grain size and pearlite colony size. The dynamic fracture toughness, KID, is obviously lower than static fracture toughness, KIC, and has the same trend as KIC. The ratio of KID/sigma YD is the most reasonable parameter to evaluate the fracture resistance of wheel steels with different composition and yield strength. Decreasing carbon content is beneficial to the performance of cartwheel.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c9001659
EISBN: 978-1-62708-231-0
... Abstract A failure analysis case study on railroad rails is presented. The work, performed under the sponsorship of the Department of Transportation, addresses the problem of shell and detail fracture formation in standard rails. Fractographic and metallographic results coupled with hardness...
Abstract
A failure analysis case study on railroad rails is presented. The work, performed under the sponsorship of the Department of Transportation, addresses the problem of shell and detail fracture formation in standard rails. Fractographic and metallographic results coupled with hardness and residual stress measurements are presented. These results suggest that the shell fractures form on the plane of maximum residual tensile stresses. The formation of the shells is aided by the presence of defects in the material in these planes of maximum residual stress. The detail fracture forms as a perturbation from the shell crack under cyclic loading and is constrained to develop as an embedded flaw in the early stages of growth because the crack is impeded at the gage side and surface of the rail head by compressive longitudinal stresses.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001845
EISBN: 978-1-62708-241-9
... stress in ( a ) steady clamp and ( b ) splint; ( c ) distribution of axial stress in splint Discussion In this study, cracks were detected in two steady clamps applied in an electrified railway. The cracks were all observed in splints. Microfractography revealed the brittle nature...
Abstract
Two clamps that support overhead power lines in an electrified rail system fractured within six months of being installed. The clamps are made of CuNiSi alloy, a type of precipitation-strengthening nickel-silicon bronze. To identify the root cause of failure, the rail operator led an investigation that included fractographic and microstructural analysis, hardness testing, inductively coupled plasma spectroscopy, and finite-element analysis. The fracture was shown to be brittle in nature and covered with oxide flakes, but no other flaws relevant to the failure were observed. The investigation results suggest that the root cause of failure was a forging lap that occurred during manufacturing. Precracks induced by the forging defect and the influence of preload stress (due to bolt torque) caused the premature failure.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001382
EISBN: 978-1-62708-215-0
... Abstract A trunnion bolt that was part of a coupling in a metropolitan railway system failed in service, causing cars to separate. The bolt had been in service for more than ten years prior to failure. Visual examination showed that the failure resulted from complete fracture at the grease port...
Abstract
A trunnion bolt that was part of a coupling in a metropolitan railway system failed in service, causing cars to separate. The bolt had been in service for more than ten years prior to failure. Visual examination showed that the failure resulted from complete fracture at the grease port and surface groove located at midspan. Drillings machined from the bolt underwent chemical analysis, which confirmed that the material was AISI 1045 carbon steel, in accordance with specifications. Two sections cut from the bolt were subjected to metallographic examination and hardness testing. The fracture origin was typical of fatigue. The ultimate tensile strength of the bolt was in excess of requirements. Wear patterns indicated that the bolt had been frozen in position for a protracted period and subjected to repeated bending stresses, which resulted in fatigue cracking and final complete fracture. It was recommended that proper lubrication procedures be maintained to allow free rotation of the bolts while in service.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c9001665
EISBN: 978-1-62708-231-0
... Shepherdsville, Kentucky, causing substantial damage to a printing works adjacent to the tracks. In the ensuing litigation, the Louisville and Nashville Railroad Company was forced to pay compensation for the damage caused by the derailment. The railroad carried out an investigation of the mishap and found...
Abstract
Following a freight train derailment, part of a fractured side frame was retained for study because a portion of its fracture surface exhibited a rock candy appearance and black scale. It was suspected of having failed, thereby precipitating the derailment. Metallography, scanning electron microscopy, EDXA, and x-ray mapping were used to study the steel in the vicinity of this part of the fracture surface. It was found to be contaminated with copper. Debye-Scherrer x-ray diffraction patterns obtained from the scale showed that it consisted of magnetite and hematite. It was concluded that some copper was accidentally left in the mold when the casting was poured. Liquid copper, carrying with it oxygen in solution, penetrated the austenite grain boundaries as the steel cooled. The oxygen reacted with the steel producing a network of scale outlining the austenite grain structure. When the casting fractured as a result of the derailment, the fracture followed the scale in the contaminated region thus creating the “rock candy” fracture.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001347
EISBN: 978-1-62708-215-0
... Abstract A 127 cu m (4,480 cu ft) pressurized railroad tank car burst catastrophically. The railroad tank was approximately 18 m (59 ft) long (from 2:1 elliptical heads), 3 m (10 ft) in OD, and 16 mm (0.63 in.) thick. The chemical and material properties of the tank were to comply with AAR M...
Abstract
A 127 cu m (4,480 cu ft) pressurized railroad tank car burst catastrophically. The railroad tank was approximately 18 m (59 ft) long (from 2:1 elliptical heads), 3 m (10 ft) in OD, and 16 mm (0.63 in.) thick. The chemical and material properties of the tank were to comply with AAR M-128 Grade B. As a result of the explosive failure of the tank car, fragments were ejected from the central region of the car between the support trucks from ground zero to a maximum of approximately 195 m (640 ft). The mode of failure was a brittle fracture originating at a preexisting lamination and crack in the tank wall adjacent to the tank nozzle. The mechanism of failure was overpressurization of the railroad tank car caused by a chemical reaction of the butadiene contents. The interrelationship of the mode, mechanism, and consequences of failure is reviewed to reconstruct the sequence of events that led up to the breach of the railroad tank car. Means to prevent similar reoccurrences are discussed.
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in Mechanisms and Appearances of Ductile and Brittle Fracture in Metals
> Failure Analysis and Prevention
Published: 01 January 2002
Fig. 72 Fracture surface of a railroad coupler that failed in bending. The dark, irregular region is a region of shrinkage porosity. The black “thumbnail” is the region of fatigue crack initiation. Chevrons (pointing to the black “fingernail”) are visible in the overload region.
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Image
in Mechanisms and Appearances of Ductile and Brittle Fracture in Metals
> Failure Analysis and Prevention
Published: 15 January 2021
Fig. 72 Fracture surface of a railroad coupler that failed in bending. The dark, irregular region is a region of shrinkage porosity. The black “thumbnail” is the region of fatigue crack initiation. Chevrons (pointing to the black fingernail) are visible in the overload region.
More
Image
in Brittle Fracture Explosive Failure of a Pressurized Railroad Tank Car
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1993
Fig. 1 Dimensional drawing of railroad tank car
More
Image
in Brittle Fracture Explosive Failure of a Pressurized Railroad Tank Car
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1993
Fig. 2 Fragment distribution of railroad tank car after rupture
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Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001305
EISBN: 978-1-62708-215-0
... Abstract An ASTM A 504 carbon steel railway car wheel that was used on a train in a metropolitan railway system failed during service, causing derailment. The wheel was completely fractured from rim to hub. Macrofractography of the fracture surface showed road grime, indicating that the crack...
Abstract
An ASTM A 504 carbon steel railway car wheel that was used on a train in a metropolitan railway system failed during service, causing derailment. The wheel was completely fractured from rim to hub. Macrofractography of the fracture surface showed road grime, indicating that the crack had existed for a considerable time prior to derailment and initiated in the flange. Failure propagated from the flange across the rim and down the plate to the bore of the hub. Two zones that exhibited definite signs of heating were observed. The fracture initiation site was typical of fatigue fracture. No defects were found that could have contributed to failure. The wheel conformed to the chemical, microstructural, and hardness requirements for class A wheels. Failure was attributed to repeated severe heating and cooling of the rim and flange due to brake locking or misapplication of the hand brake. It was recommended that the brake system on the car be examined and replaced if necessary.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0090974
EISBN: 978-1-62708-235-8
... Abstract A cast steel bracket manufactured in accordance with ASTM A 148 grade 135/125 steel failed in railroad maintenance service. Ancillary property requirements included a 285 to 331 HB hardness range and minimum impact energy of 27 J (20 ft·lbf) at -40 deg C (-40 deg F). The conditions...
Abstract
A cast steel bracket manufactured in accordance with ASTM A 148 grade 135/125 steel failed in railroad maintenance service. Ancillary property requirements included a 285 to 331 HB hardness range and minimum impact energy of 27 J (20 ft·lbf) at -40 deg C (-40 deg F). The conditions at the time of failure were characterized as relatively cold. Investigation (visual inspection, chemical analysis, and unetched 119x and 2% nital etched 119x SEM images) supported the conclusion that the bracket failed through brittle overload fracture due to a number of synergistic factors. The quenched-and-tempered microstructure contained solidification shrinkage, inherently poor ductility, and type II Mn-S inclusions that are known to reduce ductility. The macro and microscale fracture features confirmed that the casting was likely in low-temperature service at the time of failure. The composition and mechanical properties of the casting did not satisfy the design requirements. Recommendations included exerting better composition control, primarily with regard to melting, deoxidation, and nitrogen control. Better deoxidation practice was recommended to generate the more desirable Mn-S inclusion morphology, and reevaluation of the casting design was suggested to minimize shrinkage.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c0089716
EISBN: 978-1-62708-231-0
... Abstract A railway tank car developed a fracture in the region of the sill and shell attachment during operation at -34 deg C (-30 deg F). On either side of the sill-support member, cracking initiated at the weld between a 6.4 mm thick frontal cover plate and a 1.6 mm thick side support plate...
Abstract
A railway tank car developed a fracture in the region of the sill and shell attachment during operation at -34 deg C (-30 deg F). On either side of the sill-support member, cracking initiated at the weld between a 6.4 mm thick frontal cover plate and a 1.6 mm thick side support plate. The crack then propagated in a brittle manner upward through the side plate, through the welds attaching the side plate to a 25 mm (1 in.) thick shell plate (ASTM A212, grade B steel), and continued for several millimeters in the shell plate before terminating. Other plates involved were not positively identified but were generally classified as semi-killed carbon steels. Investigation (visual inspection, hardness testing, chemical analysis, Charpy V-notch testing, and drop-weight testing) supported the conclusions that the fracture was initiated by weld imperfections and propagated in a brittle manner as a result of service stresses acting on the plate having low toughness at the low service temperatures encountered. Recommendations included that the specifications for the steel plates be modified to include a toughness requirement and that improved welding and inspection practices be performed to reduce the incidence of weld imperfections.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003566
EISBN: 978-1-62708-180-1
.... The macrostructure and microstructure of spall cavities are described, along with some aspects of the numerous specifications for striking/struck tools. The article also describes the availability of spall-resistant metals and the safety aspects of striking/struck tools in railway applications. fractography...
Abstract
This article briefly reviews the analysis methods for spalling of striking tools with emphasis on field tests conducted by A.H. Burn and on the laboratory tests of H.O. McIntire and G.K. Manning and of J.W. Lodge. It focuses on the metallography and fractography of spalling. The macrostructure and microstructure of spall cavities are described, along with some aspects of the numerous specifications for striking/struck tools. The article also describes the availability of spall-resistant metals and the safety aspects of striking/struck tools in railway applications.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001376
EISBN: 978-1-62708-215-0
... Abstract An AISI 9260 steel railroad spike maul failed after a relatively short period of service. The maul head fractured in two pieces when struck against a rail. Visual, fractographic, metallographic, and chemical analyses were conducted on sections taken from the maul head, which was found...
Abstract
An AISI 9260 steel railroad spike maul failed after a relatively short period of service. The maul head fractured in two pieces when struck against a rail. Visual, fractographic, metallographic, and chemical analyses were conducted on sections taken from the maul head, which was found to have fractured across both sides of the eye. Failure occurred in at least three separate events: formation of two cracks immediately adjacent to the eye, extension of one of the original cracks over a portion of one of the eye sides, and abrupt extension of the original crack across the eye sides, resulting in separation into two halves.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0001822
EISBN: 978-1-62708-180-1
... fracture face and origin. Failures of locomotive axles due to overheated friction bearings are rather common in the railroad industry and have been observed for more than 100 years. Because of this, such failures are usually diagnosed merely by visual inspection of the damage. Comprehensive...
Abstract
This article provides a background of friction-bearing failures due to overheating. The failures of locomotive axles caused by overheated traction-motor support bearings are discussed. The article also describes liquid-metal embrittlement (LME) in steel. It examines the results of various axle studies, with illustrations and concludes with information on the simulation of the LME mechanism.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c9001719
EISBN: 978-1-62708-231-0
... into locomotive axle failures during the last century. A few relevant cases will be reviewed here: The first failure of this kind was reported and investigated in 1914 1 . The failed part was a Krupp Railroad Axle that failed in service. The study concluded that bronze metal was apparent on the fracture...
Abstract
Metallography is an important component of failure analysis. In the case of a liquid metal embrittlement (LME) failure it is usually conclusive if a third phase constituent can be formed inside of the cracks after failure. In the case where it is necessary to characterize the third phase material, one can use various x-ray spectrographic techniques in conjunction with a scanning electron microscope (SEM). This study describes those metallographic and SEM analysis techniques for determining the mode of failure for a locomotive traction motor by LME.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c9001694
EISBN: 978-1-62708-222-8
.... Austenite Bicycles Chromium plating Grain boundaries Metallography Chromium-plated steel Hydrogen damage and embrittlement Surface treatment related failures A number of vehicle accidents and failures have been evaluated over the years. These range from aircraft accidents, to railroad locomotive...
Abstract
The outer tube, or stem, on a bicycle frame fractured after two years of use. Detailed investigation revealed that the lower stem bearing had been loose for some time and the bottom bearing cup contained many cracks. Metallographic examination of the chromium-plated cup confirmed the brittle nature of the cracks, located along prior austenite boundaries. The failure was attributed to hydrogen embrittlement due to improper manufacturing procedures following chromium plating. The cracking led to looseness in the bearing and consequent scoring, cracking, and overloading of the stem.
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