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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001491
EISBN: 978-1-62708-217-4
... procedures and resumed production of nozzle liners with more tightly controlled fiber/fabric materials. Proof stress Quality control Silica-phenolic (Other, general, or unspecified) fracture (Other, general, or unspecified) processing-related failures I. Introduction This report describes...
Abstract
Two silica phenolic nozzle liners cracked during proof testing. The test consisted of pressuring the nozzles to 14.1 MPa (2050 psia) for 5 to 20 s. It was concluded that the failure was due to longitudinal cracking in the convergent exhaust-nozzle insulators, stemming from the use of silica phenolic tape produced from flawed materials that went undetected by the quality control tests, which at the time, assessed tape strength properties in the warp rather than the bias direction. Once the nozzle manufacturer and its suppliers identified the problem, they changed their quality control procedures and resumed production of nozzle liners with more tightly controlled fiber/fabric materials.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047641
EISBN: 978-1-62708-235-8
... into the gas channel. Thermal stresses cracked the embrittled weld, exposing the crack surfaces to oxidation before cooling. One of these cracks caused a stress concentration so severe that failure of the vessel wall during the proof test was inevitable. A sealing system at the split-line region...
Abstract
A Ti-6Al-4V alloy pressure vessel failed during a proof-pressure test, fracturing along the center girth weld. The girth joints were welded with the automatic gas tungsten arc process utilizing an auxiliary trailing shield attached to the welding torch to provide inert-gas shielding for the exterior surface of the weld. A segmented backup ring with a gas channel was used inside the vessel to shield the weld root. The pressure vessel failed due to contamination of the fusion zone by oxygen, which resulted when the gas shielding the root face of the weld was diluted by air that leaked into the gas channel. Thermal stresses cracked the embrittled weld, exposing the crack surfaces to oxidation before cooling. One of these cracks caused a stress concentration so severe that failure of the vessel wall during the proof test was inevitable. A sealing system at the split-line region of the segmented backup ring was provided, and a fine-mesh stainless steel screen diffuser was incorporated in the channel section of the backup ring to prevent air from leaking in. A titanium alloy color chart was furnished to permit correlation of weld-zone discoloration with the degree of atmospheric contamination.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001906
EISBN: 978-1-62708-217-4
... testing, scanning electron microscopy, and energy-dispersive x-ray spectroscopy. It was determined that the failures were due to forging defects. Both forging laps and seams acted as stress concentrators when the lugs were loaded during proof testing. Bombs (weapons) Suspension lugs Forging...
Abstract
Suspension lugs fabricated from AISI 4340 steel used to facilitate loading of bombs onto the underside of military aircraft could not sustain required loads during routine proof load testing. Three failed lugs underwent visual examination, chemical analysis, metallography, hardness testing, scanning electron microscopy, and energy-dispersive x-ray spectroscopy. It was determined that the failures were due to forging defects. Both forging laps and seams acted as stress concentrators when the lugs were loaded during proof testing.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001054
EISBN: 978-1-62708-214-3
... Abstract Silver solid-state bonded components containing uranium failed under zero or low applied load several years after manufacture. The final operation in their manufacture was a proof loading that applied a sustained tensile stress to the bond, which all components passed. The components...
Abstract
Silver solid-state bonded components containing uranium failed under zero or low applied load several years after manufacture. The final operation in their manufacture was a proof loading that applied a sustained tensile stress to the bond, which all components passed. The components comprised circular cylinders fabricated by plating a thin layer of silver on each of the contact surfaces (uranium and stainless steel) and pressing the parts together at elevated temperature to solid-state bond the two silver surfaces. The manufacturing process produced a high level of residual stress at the bond. The failures appeared to be predominantly located between the silver layer and the uranium substrate. Normal fracture location of specimens taken from similar components was at the silver/silver bond interface. Laboratory testing revealed that the uranium/silver joint was susceptible to premature failure by stress-corrosion cracking under sustained loading if the atmosphere was saturated with water vapor.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c0090457
EISBN: 978-1-62708-222-8
... design change. Because of the configuration of the parts, standard mechanical testing could not be performed. Instead, a proof load test was devised to directly assess the stress required to produce failure within the tab, at an area consistent with the failure latch assembly. A direct comparison...
Abstract
Components of a latch assembly used in a consumer safety restraint exhibited a relatively high failure rate. The failures were occurring after installation but prior to actual field use when failure could result in severe injury. Cracking occurred within retaining tabs used to secure a metal slide on an older design, whereas newer components showed no signs of failure. The latch assembly components were injection molded from an unfilled commercial grade of a polyacetal copolymer. Investigation of failed parts (including visual inspection, a specially designed proof load test, 59x SEM images, micro-FTIR in the ATR mode, and DSC/TGA/MFR analysis) showed no evidence of contamination or degradation from the molding process. The conclusion was that the parts failed via brittle fracture associated with stress overload. The stress overload was accompanied by severe apparent embrittlement resulting from a relatively high strain rate event and/or significant stress concentration. A relatively sharp corner formed by a retaining tab on the older design was shown to be a primary cause of the failures.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001558
EISBN: 978-1-62708-217-4
.... At this point, it is necessary to examine the processing, proof testing and operating history of the valve to correlate the stresses and environments with the fractographic observations. Material and Processing The valve body was produced from Ti-5Al-2.5Sn ELI (extra low interstitial) and had 0.095...
Abstract
A liquid hydrogen main fuel control valve for a rocket engine failed by fracture of the Ti-5Al-2.5Sn body during the last of a series of static engine test firings. Fractographic, metallurgical, and stress analyses determined that a combination of fatigue and unexpected aqueous stress-corrosion cracking initiated and propagated the crack which caused failure. The failure analysis approach and its results are described to illustrate how fractography and fracture mechanics, together with a knowledge of the crack initiation and propagation mechanisms of the valve material under various stress states and environments, helped investigators to trace the cause of failure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0046044
EISBN: 978-1-62708-235-8
... Abstract A rocket-motor case made of consumable-electrode vacuum arc remelted D-6ac alloy steel failed during hydrostatic proof-pressure testing. Close visual examination, magnetic-particle inspection, and hardness tests showed cracks that appeared to have occurred after austenitizing...
Abstract
A rocket-motor case made of consumable-electrode vacuum arc remelted D-6ac alloy steel failed during hydrostatic proof-pressure testing. Close visual examination, magnetic-particle inspection, and hardness tests showed cracks that appeared to have occurred after austenitizing but before tempering. Microscopic examinations of ethereal picral etched sections indicated that the cracks appeared before or during the final tempering phase of the heat treatment and that cracking had occurred while the steel was in the as-quenched condition, before its 315 deg C (600 deg F) snap temper. Chemical analysis of the cracked metal showed a slightly higher level of carbon than in the component that did not crack. X-ray diffraction studies of material from the fractured dome showed a very low level of retained austenite, and chemical analysis showed a slightly higher content of carbon in the metal of the three cracked components. Bend tests verified the conclusion that the most likely mechanism of delayed quench cracking was isothermal transformation of retained austenite to martensite under the influence of residual quenching stresses. Recommendations included modifying the quenching portion of the heat-treating cycle and tempering in the salt pot used for quenching, immediately after quenching.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001512
EISBN: 978-1-62708-228-0
... Abstract When a large LPG low-carbon steel storage tank was put into service for the first time and filled beyond the proof testing level, a brittle fracture crack initiated at a fillet weld between a stiffener ring and the wall. The crack propagated to a length of 5.5 m and arrested. Analysis...
Abstract
When a large LPG low-carbon steel storage tank was put into service for the first time and filled beyond the proof testing level, a brittle fracture crack initiated at a fillet weld between a stiffener ring and the wall. The crack propagated to a length of 5.5 m and arrested. Analysis showed that the plates satisfied the criteria of BS 4741. It was concluded that the cause of crack initiation was the lack of a mouse hole at the junction between the stiffening ring and the wall of the tank. The tank was repaired and put back in service. When it was filled beyond the proof test level, again a brittle crack was initiated at a horizontal weld defect and propagated vertically, destroying the tank and the liquefaction plant. The initiation site was a thumbnail elliptical crack in a horizontal weld, having a depth of 1.5 mm, and a length of 4.5 mm. This showed that as late the mid-1970s, misunderstanding of brittle fracture led to the wrong design and construction of an LPG storage tank. The best design specification is to use a correlation between LAST, the Lowest Anticipated Service Temperature, and the DBTT measured by either Charpy tests or DTT.
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in Fracture of Welds in a Pressure Vessel Because of Atmospheric Contamination
> ASM Failure Analysis Case Histories: Processing Errors and Defects
Published: 01 June 2019
cracks in the fusion zone and HAZ. 3x. (b) Fracture origin (top) formed by welding stresses on the contaminated weld metal. The light region below the origin is the rupture that occurred during the proof test. Approximately 5x
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001724
EISBN: 978-1-62708-234-1
... commences. Stress-relieving, prior to final machining, by heating for 5 hr. at 750° F. and cooling in the furnace.” By the above manufacturing routine, end bells were produced to meet the specification's minimum tensile requirements, namely, 112,000-psi. yield (0.5% proof stress), 128,000-psi...
Abstract
Forged austenitic steel rings used on rotor shafts in two 100,000 kW generators burst from overstressing in a region of ventilation holes. A variety of causes contributed to the brittle fractures in the ductile austenitic alloy, including stress concentration by holes, work hardened metal in the bores, and a variable pattern of residual stress.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001670
EISBN: 978-1-62708-217-4
... case. Questions arose as to how the softening occurred and whether or not it had contributed to the failures. This report contains the results of a study which resolved that inner wall softening could not have been present in the failed missile cases. Missile cases Proof testing Softening 18Ni...
Abstract
Failure occurred in two TOW flight missile cases in unrelated launchings. After an extensive investigation, it was concluded that stress corrosion was the most likely cause of failure. Subsequent to this conclusion, inner wall softening was observed in an unfired TOW flight missile case. Questions arose as to how the softening occurred and whether or not it had contributed to the failures. This report contains the results of a study which resolved that inner wall softening could not have been present in the failed missile cases.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001287
EISBN: 978-1-62708-215-0
... are reproducible and typical for steel of this composition. Tensile testing results Table 2 Tensile testing results Specimen identification (a) Reduction of area, Elongation, Yield stress 0.2% proof stress Ultimate tensile strength % % MPa tonf/in. 2 MPa tonf/in. 2 MPa tonf...
Abstract
A recurring piston shaft failure problem on the billet-loading tray of an extrusion press was investigated. Two shafts fractured within a period of 10 days. The shaft was machined from normalized EN3 (AISI C1022) steel stock without further treatment. Visual, microstructural, chemical, and mechanical (hardness and tensile properties) analyses of failed shaft specimens were conducted. The examinations showed that the shafts had failed by fatigue. It was recommended that a low-alloy steel (e.g., 3% Ni-Cr) in the hardened and tempered condition and subjected to shot-peening surface-hardening treatment be used. The provision of a stop to reduce bending stresses was also recommended.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0006440
EISBN: 978-1-62708-234-1
... and proof tested. It was recommended that the water system consisting of deionized water and formaldehyde be replaced with water having a low oxygen content and a cathodic inhibitor (oxygen scavenger). Brazed joints Mirrors Molybdenum Erosion - corrosion Intergranular corrosion A failed laser...
Abstract
A failed laser mirror and another complete mirror of the same construction were analyzed. The laser mirror consisted of three layers of material brazed together to form channels through which the cooling water flows. Samples were analyzed with light optical and scanning electron microscopy. The corrosion product contained molybdenum and copper with a trace of gold. The base material was analyzed as molybdenum with negligible alloying additions. The primary mode of corrosion attack on the base material appeared to be intergranular, although uniform corrosion was evident also. It was concluded that corrosion attack sufficiently weakened the base material and the brazed joints, allowing catastrophic failure of the mirror due to the pressure of the cooling water. It was recommended that the mirrors be cleaned of all corrosion products present as a result of past service conditions and proof tested. It was recommended that the water system consisting of deionized water and formaldehyde be replaced with water having a low oxygen content and a cathodic inhibitor (oxygen scavenger).
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001142
EISBN: 978-1-62708-228-0
... produced by deep drawing, a bottom plate is welded to the another CUP, and these cups are welded to each other at the edges of these cups. Then. the cylinder is annealed again after welding, and pressure proof test is carried out. Then the cylinder is painted and LPG cylinder is manufactured. 2...
Abstract
Several newly developed liquid propane gas (LPG) cylinders made from Fe-0.13C-0.42Mn steel failed, each fracturing in the longitudinal direction. One of the cylinders was thoroughly analyzed to determine the cause. Deep-drawing flaws were observed on the inner wall of the cylinder, oriented in the direction of the fracture and roughly equal in length. Flaws about 1.3 mm deep, steps, and a chevron pattern were observed on the fractured surface as were cleavage facets, revealed by SEM. Hardness was relatively high and the microstructure near the fracture surface appeared elongated. In addition, the stress intensity factor KI calculated from the value of the internal pressure was lower than that estimated by the fracture toughness test. All of this suggests that the tanks were not sufficiently annealed and prone to brittle fracture. The analysis thus proves that cracks initiated by deep-drawing flaws were the primary cause of failure.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001455
EISBN: 978-1-62708-234-1
...% was indicated as being necessary to ensure that the treatment conferred virtual immunity to exfoliation corrosion. As is usually found, most advantages introduce concomitant disadvantages and over-ageing leads to a reduction in proof stress and tensile strength values, but for the time and temperature...
Abstract
Aluminum alloy BS.1476-HE.15 by virtue of its high strength and low density finds application in the form of bars or sections for cranes, bridges, and other such structures where a reduction in dead weight load and inertia stresses is advantageous. Bars and sections in H.15 alloy are mostly produced by extrusion. Some material processed this way has been prone to exfoliation corrosion. Extended aging for 24 h at a temperature of 185 deg C (365 deg F) virtually suppresses the tendency for exfoliation corrosion to develop. Also, the use of a sprayed coating, either of aluminum or Al-1Zn alloy, was effective in halting and preventing this form of attack. While alarming, the appearance of exfoliation corrosion provides a valuable warning to the engineer or inspector before a severe weakening of the particular sections has occurred.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001383
EISBN: 978-1-62708-215-0
...− Conclusion and Recommendations Most Probable Cause The potential for cracking a hardened carburized case in a high-strength stud is significant, considering the common use of either air impact wrenches or the possibility of exceeding the proof stress with a wrench. A cracked case enables moisture...
Abstract
Several case-hardened and zinc-plated carbon-manganese steel wheel studs fractured in a brittle manner after very limited service life. The fracture surfaces of both front and rear studs showed no sign of fatigue beach marks or deformation in the form of shear lips that would indicate either a fatigue mechanism or ductile overload failure. SEM analysis revealed that the mode of fracture was intergranular decohesion, which indicates an environmental influence in the fracture mechanism. The primary fracture initiated at a thread root and propagated by environmentally-assisted slow crack growth until final fracture. The natural stress concentration at the thread root, when tightened to the required clamp load concomitant with the presence of cracks in the carburized case, was sufficient to exceed the critical stress intensity for hydrogen-assisted stress cracking (HASC). The zinc plating exacerbated the situation by providing a strong local corrosion cell in the form of a sacrificial anode region adjacent to the cracked thread. The enhanced generation of hydrogen in a corrosive environment subsequently lead to HASC of the wheel studs.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001668
EISBN: 978-1-62708-232-7
... the specified proof load. However, this value was still below the actual yield point of the material even with a biaxial tension/torsion load. Bolt Strengths and Specifications Table 2 Bolt Strengths and Specifications Property Measured Values Specified Mean Std Dev Value (a) Yield...
Abstract
A detailed investigative failure analysis was conducted on an autoclave which blew apart in a furnace for no apparent reason. Bolt failure resulted in separation of the autoclave lid and subsequent destruction of the furnace. Analysis using metallography, fractography, mechanical testing and exemplar tests were performed on the bolt material. Mechanical engineering analysis and leak-before-break criteria were extensively analyzed. Results led to only one possible conclusion: that an explosion occurred within the autoclave. Suggestions for autoclave design are presented as a result of the analysis.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001432
EISBN: 978-1-62708-221-1
... the appropriate qualification tests. In many instances production tests plates may be called for and it is the usual practice for the item to be finally examined by non-destructive methods and a proof carried out. To the uninitiated on the other hand, welding appears on obviously simple process...
Abstract
During the pre-test inspection following the stress calculation check on a 7-ton capacity Scotch derrick crane, it was noted that threads on the back stay anchorage bolts were of unusually fine pitch (11 tpi) and that the machined faces of the nuts showed irregular pits or depressions disposed in an annular manner. When sectioned, the nuts showed a surprising method of construction. The nuts for the bolts had been made by using conventional pipe couplings inserted into sleeves made from hexagonal bar and the coupling secured to the sleeve by welding at each outer face. The ends of the sleeve bore were chamfered to form a weld preparation. After welding, the faces were machined which resulted in the removal of most of the weld metal and revealed a pronounced lack of penetration. All bolts used to anchor derrick crane back stays should be designed in accordance with the recommendations of British Standard 327:1964 (Clauses 10 and 18).
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c9001426
EISBN: 978-1-62708-224-2
... welding. As the welding across the major portion of the section was satisfactory, the chain would be capable of passing the normal proof test, but the discontinuities that were present acted as stress-raisers that extended in the form of cracks following loading in service ultimately a link failed...
Abstract
Following three similar failures of load chains on manually operated geared pulley-blocks of 1-ton capacity, a portion of one of the chains was obtained for examination. The chain was made of mild steel and the links had been electrically butt-welded at one side. In the case of the sample obtained, the failure in service had resulted from fracture of one of the links in the plane of the weld. Six of the other links in the vicinity showed cracks in the welds in various stages of development. Microscope examination showed a crack in an early stage of development and also from an apparently sound link, the prepared surfaces lying in the planes of the links. This examination revealed that the welds were initially defective. Discontinuities were present in both cases adjacent to the insides of the links, of a type indicative of either inadequate fusion or incomplete expulsion of oxide, etc., at the time of the upset, i.e. the pressing together of the ends of the links to complete the welding. It was evident from the examination that the service failures were due to the use of chain that was initially defective.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001140
EISBN: 978-1-62708-227-3
... alloys for storage of compressed breathing gasses, increases constantly. The design of most of these cylinders is based on classical “strength of materials” considerations i.e. employing thin wall cylinder equations and requiring that the proof hoop stress (1.5× service hoop stress) in the thinnest...
Abstract
Several pressurized air containers (i.e., diving tanks) made of non-heat-treatable Al-5Mg aluminum alloy failed catastrophically. Catastrophic failure occurred when a subcritical stress corrosion crack reached a critical size. Critical crack size for unstable propagation was reached prior to wall penetration, which could have led to subsequent loss of pressure, resulting in explosion of the cylinder. It was recommended that more stress corrosion resistant alloys be used for sea diving applications. Furthermore, cylinders should have a reduced wall thickness that can be determined employing the “leak-before-break” design philosophy, developed using fracture mechanics, to eliminate the possibility of catastrophic ruptures.
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