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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0046956
EISBN: 978-1-62708-232-7
... Abstract A brazing-furnace muffle 34 cm (13 in.) wide, 26 cm (10 in.) high, and 198 cm (78 in.) long, was fabricated from nickel-base high-temperature alloy sheet and installed in a gas-fired furnace used for copper brazing of various assemblies. The operating temperature of the muffle...
Abstract
A brazing-furnace muffle 34 cm (13 in.) wide, 26 cm (10 in.) high, and 198 cm (78 in.) long, was fabricated from nickel-base high-temperature alloy sheet and installed in a gas-fired furnace used for copper brazing of various assemblies. The operating temperature of the muffle was reported to have been closely controlled at the normal temperature of 1175 deg C (2150 deg F); a hydrogen atmosphere was used during brazing. After about five months of continuous operation, four or five holes developed on the floor of the muffle, and the muffle was removed from service. Analysis (visual inspection, x-ray spectrometry, and metallographic examination) supported the conclusion that the muffle failed by localized overheating in some areas to temperatures exceeding 1260 deg C (2300 deg F). The copper found near the holes had dripped to the floor from assemblies during brazing. The copper diffused into the nickel-base alloy and formed a grain-boundary phase that was molten at the operating temperature. The presence of this phase caused localized liquefaction and weakened the alloy sufficiently to allow formation of the holes. No recommendations were made.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003555
EISBN: 978-1-62708-180-1
... to be controlled by the temperature and the carbon-monoxide-to-carbon-dioxide ratio in the gas ( Ref 15 ). Nickel-base alloys are more resistant to carbon diffusion than most other alloys, and alloys with higher nickel content are superior to low-content nickel alloys. Carburization appears to be appreciable...
Abstract
High temperature corrosion may occur in numerous environments and is affected by factors such as temperature, alloy or protective coating composition, time, and gas composition. This article explains a number of potential degradation processes, namely, oxidation, carburization and metal dusting, sulfidation, hot corrosion, chloridation, hydrogen interactions, molten metals, molten salts, and aging reactions including sensitization, stress-corrosion cracking, and corrosion fatigue. It concludes with a discussion on various protective coatings, such as aluminide coatings, overlay coatings, thermal barrier coatings, and ceramic coatings.
Book Chapter
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003545
EISBN: 978-1-62708-180-1
..., but they may reduce impact strength. Indirectly, compositional changes in the vicinity of carbides can alter rupture strength. In general, acicular M 6 C carbides are not believed to affect the properties of nickel-base high-temperature alloys greatly, unless the alloying elements involved in the carbide...
Abstract
This article reviews the applied aspects of creep and stress-rupture failures. It discusses the microstructural changes and bulk mechanical behavior of classical and nonclassical creep behavior. The article provides a description of microstructural changes and damage from creep deformation, including stress-rupture fractures. It also describes metallurgical instabilities, such as aging and carbide reactions, and evaluates the complex effects of creep-fatigue interaction. The article concludes with a discussion on thermal fatigue and creep fatigue failures.
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006780
EISBN: 978-1-62708-295-2
... (such as lead, tin, and high-purity aluminum) can deform by creep at or a little above room temperature. In contrast, refractory body-centered cubic metals (such as tungsten and molybdenum) and nickel-base superalloys require temperatures near 1000 °C (1830 °F) to activate the onset of creep deformation...
Abstract
The principal types of elevated-temperature mechanical failure are creep and stress rupture, stress relaxation, low- and high-cycle fatigue, thermal fatigue, tension overload, and combinations of these, as modified by environment. This article briefly reviews the applied aspects of creep-related failures, where the mechanical strength of a material becomes limited by creep rather than by its elastic limit. The majority of information provided is applicable to metallic materials, and only general information regarding creep-related failures of polymeric materials is given. The article also reviews various factors related to creep behavior and associated failures of materials used in high-temperature applications. The complex effects of creep-fatigue interaction, microstructural changes during classical creep, and nondestructive creep damage assessment of metallic materials are also discussed. The article describes the fracture characteristics of stress rupture. Information on various metallurgical instabilities is also provided. The article presents a description of thermal-fatigue cracks, as distinguished from creep-rupture cracks.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0046995
EISBN: 978-1-62708-232-7
... of the burners. The tubes had an original wall thickness of 3.0 mm (0.120 in.) and were made of three different alloys: the first was Hastelloy X; the second alloy was RA 333, a wrought nickel-base heat-resistant alloy; and the third was experimental alloy 634, which contained 72% Ni, 4% Cr, and 3.5% Si...
Abstract
Three radiant tubes, made of three different high-temperature alloys, were removed from a carburizing furnace after approximately eight months of service when they showed evidence of failure by collapsing (telescoping) in a region 30 cm (12 in.) from the tube bottoms in the vicinity of the burners. The tubes had an original wall thickness of 3.0 mm (0.120 in.) and were made of three different alloys: the first was Hastelloy X; the second alloy was RA 333, a wrought nickel-base heat-resistant alloy; and the third was experimental alloy 634, which contained 72% Ni, 4% Cr, and 3.5% Si. The three radiant tubes had been operated at a temperature of about 1040 deg C (1900 deg F) to maintain furnace temperatures of 900 to 925 deg C (1650 to 1700 deg F). Analysis (visual inspection and micrographic examination) supported the conclusion that all three tubes failed by corrosion. Recommendations included replacing the material with an alloy, such as RA 333, with a higher chromium content and with an additional element, like silicon, resistant to carburization-oxidation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001239
EISBN: 978-1-62708-232-7
... upon formation of tight oxide layers are not stable. Heat distributing units Heating coils Overheating 80Ni-20Cr High-temperature corrosion and oxidation A coil made of the nickel-chromium alloy NiCr 80 20 (Material No. 2.4869) with approx. 80 % Ni and 20% Cr had burnt through...
Abstract
A coil made of a nickel-chromium alloy (Material No. 2.4869) with approx. 80Ni and 20Cr had burned through after a brief period of operation as a heating element in a brazing furnace. The protective atmosphere consisted of an incompletely combusted coal gas. Furnace temperature reached 1150 deg C. This type of selective oxidation at which the easily oxidized chromium burns, while the nickel is not attacked, is caused by mildly oxidizing gases and is sometimes designated as green rot. Under these conditions, chromium-containing steels and alloys whose oxidation resistance is based upon formation of tight oxide layers are not stable.
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006787
EISBN: 978-1-62708-295-2
... 980 1795 3 Hastelloy X nickel-base superalloy 1205 2200 3 HX (17Cr-66Ni-bal Fe) 1150 2100 3 (a) Seamless tube. (b) Electric-resistance-welded tube The effects of oxygen concentration and temperature are specific to each alloy. Scale growth rate increases...
Abstract
High-temperature corrosion can occur in numerous environments and is affected by various parameters such as temperature, alloy and protective coating compositions, stress, time, and gas composition. This article discusses the primary mechanisms of high-temperature corrosion, namely oxidation, carburization, metal dusting, nitridation, carbonitridation, sulfidation, and chloridation. Several other potential degradation processes, namely hot corrosion, hydrogen interactions, molten salts, aging, molten sand, erosion-corrosion, and environmental cracking, are discussed under boiler tube failures, molten salts for energy storage, and degradation and failures in gas turbines. The article describes the effects of environment on aero gas turbine engines and provides an overview of aging, diffusion, and interdiffusion phenomena. It also discusses the processes involved in high-temperature coatings that improve performance of superalloy.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003517
EISBN: 978-1-62708-180-1
... assessment methods life fraction rule metallurgical instabilities microstructural evaluation nickel-base superalloys oxide-scale-based life prediction parameter-based assessments power plant piping power plant tubing steel-based alloys thermal-mechanical fatigue ELEVATED-TEMPERATURE FAILURE...
Abstract
This article focuses on the life assessment methods for elevated-temperature failure mechanisms and metallurgical instabilities that reduce life or cause loss of function or operating time of high-temperature components, namely, gas turbine blade, and power plant piping and tubing. The article discusses metallurgical instabilities of steel-based alloys and nickel-base superalloys. It provides information on several life assessment methods, namely, the life fraction rule, parameter-based assessments, the thermal-mechanical fatigue, coating evaluations, hardness testing, microstructural evaluations, the creep cavitation damage assessment, the oxide-scale-based life prediction, and high-temperature crack growth methods.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0046969
EISBN: 978-1-62708-227-3
... been applied in 1966, when these coatings were relatively new. It is evident that maintaining the integrity of a protective coating could significantly increase the life of a nickel-base alloy blade operating in a hot and corrosive environment. Corrosion products Diffusion coatings Turbine...
Abstract
Aluminide-coated and uncoated IN-713 turbine blades were returned for evaluation after service in a marine environment because of severe corrosion. Based on service time, failure of these blades by corrosive deterioration was considered to be premature. Analysis (visual inspection, 2.7x micrographic examination on sections etched with ferric chloride and hydrochloric acid in methanol) supported the conclusions that the blades failed by hot-corrosion attack. Variation in rate of attack on coated blades was attributed to variation in integrity of the aluminide coating, which had been applied in 1966, when these coatings were relatively new. It is evident that maintaining the integrity of a protective coating could significantly increase the life of a nickel-base alloy blade operating in a hot and corrosive environment.
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006828
EISBN: 978-1-62708-329-4
... filler metals, such as nickel-base and precious metals, brazing could take place at high temperatures that were compatible with the annealing temperatures. These suggested braze filler metals do not contain zinc, which is the prime candidate in the silver braze filler metal for producing LMIE. Alloying...
Abstract
The various methods of furnace, torch, induction, resistance, dip, and laser brazing are used to produce a wide range of highly reliable brazed assemblies. However, imperfections that can lead to braze failure may result if proper attention is not paid to the physical properties of the material, joint design, prebraze cleaning, brazing procedures, postbraze cleaning, and quality control. Factors that must be considered include brazeability of the base metals; joint design and fit-up; filler-metal selection; prebraze cleaning; brazing temperature, time, atmosphere, or flux; conditions of the faying surfaces; postbraze cleaning; and service conditions. This article focuses on the advantages, limitations, sources of failure, and anomalies resulting from the brazing process. It discusses the processes involved in the testing and inspection required of the braze joint or assembly.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001638
EISBN: 978-1-62708-228-0
... and/or aluminum to form a protective layer of chromium or aluminum oxide (Cr 2 O 3 or Al 2 O 3 ) scale to resist oxidation and other forms of high-temperature corrosion. These oxide scales are slow growing. When an alloy is under sulfidation attack, sulfides of chromium, iron, and nickel are likely to form...
Abstract
An Incoloy 800H (UNS N08810) transfer line on the outlet of an ethane-cracking furnace failed during decoking of the furnace tubes after nine years in service. A metallographic examination using optical and scanning electron microscopy as well as energy-dispersive x-ray spectroscopy revealed that the failure was due to sulfidation. The source of the sulfur in the furnace effluent was either dimethyl disulfide, injected into the furnace feed to prevent coke formation and carburization of the furnace tubes, or contamination of the feed with sulfur bearing oil.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001046
EISBN: 978-1-62708-214-3
... of 590 to 925 °C (1100 to 1700 °F), the nickel-base alloys are essential because of their resistance to 705 °C (1300 °F) liquid-phase corrosion. These alloys—600, 601, 617, 625, and 690—do well, with alloys 600 and 625 showing the best resistance to corrosion at more elevated temperatures. The field...
Abstract
The thin plates within a type 309 stainless steel chlorinated solvent combustion preheater/heat exchanger designed to process fumes from a solvent coating process showed severe corrosion within 6 months of service. Within a year corrosion had produced holes in the plates, allowing gases to shunt across the preheater/exchanger. Metallographic examination of the plates showed that accelerated internal oxidation had been the cause of failure. Corrosion racks of candidate alloys (types 304, 309, and 316 stainless steels, Inconel 600, Inconel 625, Incoloy 800, Incoloy 825, and Inco alloy C-276) were placed directly in the hot gas stream, containing HCl and Cl2, for in situ testing. Results of this investigation showed that nickel-chromium corrosion-resistant alloys, such as Inconel 600, Inconel 625, and Inco alloy C-276, performed well in this environment. Laboratory testing of the same alloys, along with Inconel alloys 601, 617, and 690 and stainless steel type 347 was also conducted in a simulated waste incinerator nitrogen atmosphere containing 10% Co2, 9% O2, 4% HCl, 130 ppm HBr and 100 ppm SO2 at 595, 705, 815, and 925 deg C (1100, 1300,1500, and 1700 deg F). The tests confirmed the suitability of the nickel-chromium alloys for such an environment. Inconel 625 was selected for fabrication of a new preheater/exchanger.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001824
EISBN: 978-1-62708-241-9
... nickel-base alloy). This unfavorable area ratio (small anode and large cathode) aggravated the corrosion process [ 1 , 2 , 6 ]. The corrosion was accelerated by the presence of high level of chloride ions in addition to the action of H 2 S, CO 2 , and oxygen at high working temperature of 82 °C...
Abstract
Nineteen out of 26 bolts in a multistage water pump corroded and cracked after a short time in a severe working environment containing saline water, CO 2 , and H 2 S. The failed bolts and intact nuts were to be made from a special type of stainless steel as per ASTM A 193 B8S and A 194. However, the investigation (which included visual, macroscopic, metallographic, SEM, and chemical analysis) showed that austenitic stainless steel and a nickel-base alloy were used instead. The unspecified materials are more prone to corrosion, particularly galvanic corrosion, which proved to be the primary failure mechanism in the areas of the bolts directly exposed to the working environment. Corrosion damage on surfaces facing away from the work environment was caused primarily by chloride stress-corrosion cracking, aided by loose fitting threads. Thread gaps constitute a crevice where an aggressive chemistry is allowed to develop and attack local surfaces.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001827
EISBN: 978-1-62708-241-9
... components made of various high-temperature-resistant alloys. Type I hot corrosion was observed on buckets and nozzles. Hot corrosion type I attacks both nickel- and cobalt-based superalloys, e.g., GTD 111 for buckets and FSX414 for nozzles. In the case of buckets, hot corrosion was observed in the form...
Abstract
Gas turbines and other types of combustion turbomachinery are susceptible to hot corrosion at elevated temperatures. Two such cases resulting in the failure of a gas turbine component were investigated to learn more about the hot corrosion process and the underlying failure mechanisms. Each component was analyzed using optical and scanning electron microscopy, energy dispersive spectroscopy, mechanical testing, and nondestructive techniques. The results of the investigation provide insights on the influence of temperature, composition, and microstructure and the contributing effects of high-temperature oxidation on the hot corrosion process. Preventative measures are also discussed.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c0091756
EISBN: 978-1-62708-236-5
... Abstract An alloy IN-690 (N06690) incinerator liner approximately 0.8 mm (0.031 in.) thick failed after only 250 h of service burning solid waste. Investigation supported the conclusion that the root cause of the failure was overfiring during startup and sulfidation of the nickel-base alloy...
Abstract
An alloy IN-690 (N06690) incinerator liner approximately 0.8 mm (0.031 in.) thick failed after only 250 h of service burning solid waste. Investigation supported the conclusion that the root cause of the failure was overfiring during startup and sulfidation of the nickel-base alloy. No recommendations were made.
Book Chapter
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003552
EISBN: 978-1-62708-180-1
... focuses on the types of hydrogen embrittlement that occur in all the major commercial metal and alloy systems, including stainless steels, nickel-base alloys, aluminum and aluminum alloys, titanium and titanium alloys, copper and copper alloys, and transition and refractory metals. The specific types...
Abstract
This article provides an overview of the classification of hydrogen damage. Some specific types of the damage are hydrogen embrittlement, hydrogen-induced blistering, cracking from precipitation of internal hydrogen, hydrogen attack, and cracking from hydride formation. The article focuses on the types of hydrogen embrittlement that occur in all the major commercial metal and alloy systems, including stainless steels, nickel-base alloys, aluminum and aluminum alloys, titanium and titanium alloys, copper and copper alloys, and transition and refractory metals. The specific types of hydrogen embrittlement discussed include internal reversible hydrogen embrittlement, hydrogen environment embrittlement, and hydrogen reaction embrittlement. The article describes preservice and early-service fractures of commodity-grade steel components suspected of hydrogen embrittlement. Some prevention strategies for design and manufacturing problem-induced hydrogen embrittlement are also reviewed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001599
EISBN: 978-1-62708-236-5
... revealed the presence of an alloy containing nickel and molybdenum in several ingots found on the bottom of the melter and on a drip which had solidified on the electrode sheath. This indicates that a major portion of the electrode assembly was exposed to a temperature of at least 1317 deg C, the nickel...
Abstract
Failure of a pilot scale test melter resulted from severe overheating of an Inconel 690 (690) jacketed molybdenum electrode. Extreme temperatures were required to melt the glass during this campaign because the feed material contained a very high waste loading. Metallurgical evaluation revealed the presence of an alloy containing nickel and molybdenum in several ingots found on the bottom of the melter and on a drip which had solidified on the electrode sheath. This indicates that a major portion of the electrode assembly was exposed to a temperature of at least 1317 deg C, the nickel/molybdenum eutectic temperature. Small regions on the end of the 690 sheath showed evidence of melting, indicating that this localized region exceeded 1345 deg C, the melting point of 690. In addition to nickel, antimony was found on the grain boundaries of the molybdenum electrode. This also contributed to the failure of the electrode. The source of the antimony was not identified but is believed to have originated from the feed material. Metallurgical evaluation also revealed that nickel had attacked the grain boundaries of the molybdenum/tungsten drain valve. This component did not fail in service; however, intergranular attack led to degradation of the mechanical properties, resulting in the fracture of the drain valve tip during disassembly. Antimony was not observed on this component.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0091757
EISBN: 978-1-62708-232-7
... the chemical makeup of these phases. Fig. 1 Sulfidation and chloridation attack on nickel alloy of charcoal-regeneration kiln. See also Fig. 2 . Region 1 is an area of chromium sulfide islands (dark phase) interspersed in chromium-depleted region (bright phase). Region 2 has angular phase (consisting...
Abstract
A kiln, 7.6 m (25 ft) long with a 1 m (3 ft) internal diameter and a 6.3 mm (0.25 in.) wall thickness, is used to regenerate spent charcoal returned by water utilities. This charcoal contains up to 0.57% S and 2.04% Cl. The kiln is made of Inconel 601 (N06601) welded using Inconel 617 (N06617) as a filler alloy. Wet charcoal is fed in at one end of the kiln and travels while being tumbled within the inclined rotating vessel. Temperatures range from 480 deg C (900 deg F) (Zone 1) to 900 deg C (1650 deg F) (Zones 2 and 3). Steam is introduced at the discharge end at 95 g/s (750 lb/h), 34 to 69 kPa (5 to 10 psi), and 125 deg C (260 deg F). The kiln developed perforations within eight months of operation. Investigation (visual inspection, metallurgical analysis, energy-dispersive spectroscopy, and 44X micrographs) supported the conclusion that the sulfur and chlorine in the charcoal attacked the Inconel 601, forming various sulfides and chlorides. Recommendations included on-site testing, and installation of test coupons of various alloys before fabricating another kiln. The suggested alloys were RA85H, 800HT, HR-120, Haynes 556, and HR-160.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003540
EISBN: 978-1-62708-180-1
... forms of environmentally induced embrittlement of the grain boundaries include neutron embrittlement, SMIE, and LMIE. Intergranular fracture processes, whether hydrogen or stress-corrosion enhanced, are frequently observed in high-strength steels, aluminum alloys, and nickel-base alloys...
Abstract
This article briefly reviews the various metallurgical or environmental factors that cause a weakening of the grain boundaries and, in turn, influence the occurrence of intergranular (IG) fractures. It discusses the mechanisms of IG fractures, including the dimpled IG fracture, the IG brittle fracture, and the IG fatigue fracture. The article describes some typical embrittlement mechanisms that cause the IG fracture of steels.
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006784
EISBN: 978-1-62708-295-2
... it is most noticeable at low strain rates. Internal reversible hydrogen embrittlement has also been observed in a wide variety of other materials, including nickel-base alloys and austenitic stainless steels, provided they are severely charged with hydrogen. However, most attention has been given...
Abstract
Hydrogen damage is a term used to designate a number of processes in metals by which the load-carrying capacity of the metal is reduced due to the presence of hydrogen. This article introduces the general forms of hydrogen damage and provides an overview of the different types of hydrogen damage in all the major commercial alloy systems. It covers the broader topic of hydrogen damage, which can be quite complex and technical in nature. The article focuses on failure analysis where hydrogen embrittlement of a steel component is suspected. It provides practical advice for the failure analysis practitioner or for someone who is contemplating procurement of a cost-effective failure analysis of commodity-grade components suspected of hydrogen embrittlement. Some prevention strategies for design and manufacturing problem-induced hydrogen embrittlement are also provided.
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