Skip Nav Destination
Close Modal
Search Results for
Martensitic stainless steels
Update search
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
NARROW
Format
Topics
Book Series
Date
Availability
1-20 of 161
Search Results for Martensitic stainless steels
Follow your search
Access your saved searches in your account
Would you like to receive an alert when new items match your search?
1
Sort by
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001352
EISBN: 978-1-62708-215-0
... Abstract Repeated failures of high-pressure ball valves were reported in a chemical plant. The ball valves were made of AFNOR Z30C13 martensitic stainless steel. Initial examination of the valves showed that failure occurred in a weld at the ball/stem junction end of austenitic stainless steel...
Abstract
Repeated failures of high-pressure ball valves were reported in a chemical plant. The ball valves were made of AFNOR Z30C13 martensitic stainless steel. Initial examination of the valves showed that failure occurred in a weld at the ball/stem junction end of austenitic stainless steel sleeves that had been welded to the valve stem at both ends. Metallographic examination showed that a crack had been introduced into the weld by improper weld heat treatment. Stress concentration at the weld location resulting from an abrupt change in cross section facilitated easy propagation of the crack during operation. Proper weld heat treatment was recommended, along with avoidance of abrupt change in cross section near the weld. Due penetrant testing at the ball stem junction before and after heat treatment was also suggested.
Image
Published: 01 January 2002
Fig. 2 Vibratory cavitation erosion of CA-6NM martensitic stainless steel. (a) Deformation rumpling and pitting at lath boundaries. (b) Early stage of material removal
More
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001094
EISBN: 978-1-62708-214-3
... Abstract Cadmium-coated type 410 martensitic stainless steel 1 4 -14 self-drilling tapping screws fractured during retorquing tests within a few weeks after installation. The screws were used to assemble structural steel frames for granite panels that formed the outer skin of a high...
Abstract
Cadmium-coated type 410 martensitic stainless steel 1 4 -14 self-drilling tapping screws fractured during retorquing tests within a few weeks after installation. The screws were used to assemble structural steel frames for granite panels that formed the outer skin of a high-rise building. Fractographic and metallographic examination showed that the fractures occurred in a brittle manner from intergranular crack propagation. Laboratory and simulated environmental tests showed that an aqueous environment was necessary for the brittle fracture/cracking phenomenon. The cracks were singular and intergranular with little branching. Secondary subsurface cracks suggested possible hydrogen embrittlement. The 410 screws had been introduced to replace conventional case-hardened carbon steel screws that conform to SAE specification J78. Carbon steel screws had a proven record of acceptable performance for the intended application. It was recommended that use of the 410 screws be discontinued in preference to the case-hardened carbon steel screws.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001386
EISBN: 978-1-62708-215-0
... Abstract Two type 420 martensitic stainless steel load cell bodies, which had been installed under two of the four legs of a milk storage tank failed in service. The failure occurred near a change in section and involved fracture of the entire cross section. Examination showed a brittle...
Abstract
Two type 420 martensitic stainless steel load cell bodies, which had been installed under two of the four legs of a milk storage tank failed in service. The failure occurred near a change in section and involved fracture of the entire cross section. Examination showed a brittle fracture that was preceded by a small fatigue region. Pitting corrosion was evident at the fracture origin. The areas around the load cells had been subjected to regular washdowns using high-pressure hot water, and the pitting was attributed to crevice corrosion between the load cell and the holddown bolts. Prevention of such corrosion by the use of a flexible sealant to eliminate the crevice was recommended.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001372
EISBN: 978-1-62708-215-0
... Abstract A coupling in a line-shaft vertical turbine pump installed in a dam foundation fractured after a very short time. The coupling material was ASTM A582 416 martensitic stainless steel. Visual, macrofractographic, and scanning electron microscopic examination of the coupling showed...
Abstract
A coupling in a line-shaft vertical turbine pump installed in a dam foundation fractured after a very short time. The coupling material was ASTM A582 416 martensitic stainless steel. Visual, macrofractographic, and scanning electron microscopic examination of the coupling showed that the fracture was brittle and was initiated by an intergranular cracking mechanism. The mode of fracture outside the crack initiation zone was transgranular cleavage. No indication of fatigue was found. The failure was attributed to improper heat treatment during manufacture, which resulted in a brittle microstructure susceptible to corrosion. The crack initiated either by stress-corrosion or hydrogen cracking. It was recommended that the couplings in the system be examined for surface cracking and, if present, corrective measures be taken.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006448
EISBN: 978-1-62708-217-4
... Abstract Three wing flap hinge bearings were received by the laboratory for analysis. The bearings were fabricated from chromium-plated type 440C martensitic stainless steel. The intergranular fracture pattern seen in the electron fractographs, coupled with the corrosion pits observed...
Abstract
Three wing flap hinge bearings were received by the laboratory for analysis. The bearings were fabricated from chromium-plated type 440C martensitic stainless steel. The intergranular fracture pattern seen in the electron fractographs, coupled with the corrosion pits observed on the inner diam of the bearings, strongly suggested that failure initiated by pitting and progressed by SCC or hydrogen embrittlement from the plating operation. It was recommended that the extent of the flap hinge bearing cracking problem be determined by using nondestructive inspection because it is possible to crack hardened type 440C during the chromium plating process. An inspection for pitting on the bearing inner diam was also recommended. It was suggested that electroless nickel be used as a coating for the entire bearing. A review of the chromium plating and baking sequence was recommended also to ensure that a source of hydrogen is not introduced during the plating operation.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001086
EISBN: 978-1-62708-214-3
... in a highly sensitized state. The sensitized material lost corrosion resistance, became embrittled along the grain boundaries, and finally failed by intergranular cracking. Use of type 410 martensitic stainless steel was recommended. Embrittlement Heat-affected zone Sensitizing Vanes Welded joints...
Abstract
Two Z-shape impeller vanes failed. The vane material was 14-hard type 301 stainless steel. The vanes were of two-piece construction, with a longitudinal weld. Analyses indicated that the vanes had not been solution annealed after welding, leaving the heat-affected zone above the welds in a highly sensitized state. The sensitized material lost corrosion resistance, became embrittled along the grain boundaries, and finally failed by intergranular cracking. Use of type 410 martensitic stainless steel was recommended.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001115
EISBN: 978-1-62708-214-3
.... Chemical analysis of the base metal and corrosion deposits did not detect iron or nickel sulfides, however Replacement of the remaining pipe strings according to a scheduled program was recommended. Because 9% Ni steel was not available, 13% Cr martensitic stainless steel was recommended as a replacement...
Abstract
During a work over of an oil well, the 9% Ni steel production tubing parted three times as it was being pulled from the well. The tubing had performed satisfactorily for more than 30 years in the well A representative failure, a circumferential fracture in a connection, was analyzed. Reported to be a hydril CS connection, the pin end parted near the last threads. The external surface exhibited mechanical damage marks from the fishing operation. No signs of external corrosion or damage were detected. Visual surface examination revealed shear lips at the outside pipe, indicating that the fracture initiated at the inside surface and grew across the wall. Longitudinal cross sections revealed heavy corrosion damage to the inside pipe surface. Metallographic examination indicated that the tubing failed as a result of severe weakening from internal corrosion. Gray-colored corrosion deposits, which penetrated the pipe throughout the grain boundaries of the material and concentrated in the matrix in a layer near the inside surface of the pipe, were observed. The presence of H2S in the produced fluids and the appearance of the gray deposit indicated that the tube suffered H2S corrosion. Chemical analysis of the base metal and corrosion deposits did not detect iron or nickel sulfides, however Replacement of the remaining pipe strings according to a scheduled program was recommended. Because 9% Ni steel was not available, 13% Cr martensitic stainless steel was recommended as a replacement.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001081
EISBN: 978-1-62708-214-3
... Abstract Several compressor disks in military fighter and trainer aircraft gas turbine engines cracked prematurely in the bolt hole regions. The disks were made of precipitation-hardened AM355 martensitic stainless steel. Experimental and analytical work was performed on specimens from...
Abstract
Several compressor disks in military fighter and trainer aircraft gas turbine engines cracked prematurely in the bolt hole regions. The disks were made of precipitation-hardened AM355 martensitic stainless steel. Experimental and analytical work was performed on specimens from the fifth-stage compressor disk (judged to be the most crack-prone disk in the compressor) to determine the cause of the failures. Failure was attributed to high-strain low-cycle fatigue during service. It was also determined that the cyclic engine usage assumed in the original life calculations had been under estimated, which led to low-cycle fatigue cracking earlier than expected. Fracture mechanics analysis of the disks was carried out to assess their damage tolerance and to predict safe inspection intervals.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001084
EISBN: 978-1-62708-214-3
... Abstract Failure analysis was performed on a fractured impeller from a boiler feed pump of a fossil fuel power plant. The impeller was a 12% Cr martensitic stainless steel casting. The failure occurred near the outside diameter of the shroud in the vicinity of a section change at the shroud...
Abstract
Failure analysis was performed on a fractured impeller from a boiler feed pump of a fossil fuel power plant. The impeller was a 12% Cr martensitic stainless steel casting. The failure occurred near the outside diameter of the shroud in the vicinity of a section change at the shroud/vane junction. Sections cut from the impeller were examined visually and by SEM fractography. Microstructural, chemical, and surface analyses and surface hardness tests were conducted on the impeller segments. The results indicated that the impeller failed in fatigue with casting defects increasing stress and initiating fracture. In addition, the composition and hardness of the impeller did not meet specifications. Revision of the casting process and institution of quality assurance methods were recommended.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001355
EISBN: 978-1-62708-215-0
... Abstract A cracked, martensitic stainless steel, low-pressure turbine blade from a 623 MW turbine generator was found to exhibit fatigue cracks during a routine turbine inspection. The blade was cracked at the first notch of the fir tree and the cracks initiated at pits induced by chloride...
Abstract
A cracked, martensitic stainless steel, low-pressure turbine blade from a 623 MW turbine generator was found to exhibit fatigue cracks during a routine turbine inspection. The blade was cracked at the first notch of the fir tree and the cracks initiated at pits induced by chloride attack. Examination of the blade microstructure at the fracture origins revealed oxide-filled pits and transgranular cracks. The oxide filled cracks appeared to have originated at small surface pits and probably propagated in a fatigue or corrosion-fatigue fracture mode. It was recommended that the sources of the chlorides be eliminated and that the remaining blades be inspected at regular maintenance intervals for evidence of cracking.
Image
Published: 01 January 2002
Fig. 15 Accelerated cavitation erosion and cracking associated with austenitic stainless steel weld deposits on a martensitic stainless steel (CA-15) impeller vane
More
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001358
EISBN: 978-1-62708-215-0
... Several compressor diaphragms from five gas turbines cracked after a short time in service. The vanes were made from type 403 martensitic stainless steel. Welding was performed using type 309L austenitic stainless steel filler metal. Applications The compressor is part of the combustion system...
Abstract
Several compressor diaphragms from five gas turbines cracked after a short time in service. The vanes were constructed of type 403 stainless steel, and welding was performed using type 309L austenitic stainless steel filler metal. The fractures originated in the weld heat-affected zones of inner and outer shrouds. A complete metallurgical analysis was conducted to determine the cause of failure. It was concluded that the diaphragms had failed by fatigue. Analysis suggests that the welds contained high residual stresses and had not been properly stress relieved. Improper welding techniques may have also contributed to the failures. Use of proper welding techniques, including appropriate prewelding and postwelding heat treatments, was recommended.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003570
EISBN: 978-1-62708-180-1
... specification is ASTM A-27, grade 70-40; other applicable specifications for carbon steel in turbines and pumps are A-216, grade WCB; A-516, grade 60; and A-283, grades A, B, C, and D. When higher strength is needed, cast martensitic stainless steels are specified. Many machines, especially high-head pumps...
Abstract
Erosion of solid surfaces can be brought about solely by liquids in two ways: from damage induced by formation and subsequent collapse of voids or cavities within the liquid, and from high-velocity impacts between a solid surface and liquid droplets. The former process is called cavitation erosion and the latter is liquid-droplet erosion. This article emphasizes on manifestations of damage and ways to minimize or repair these types of liquid impact damage, with illustrations.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001805
EISBN: 978-1-62708-241-9
... delamination brittle cleavage SEM/EDS analysis tensile yield strength 420 (martensitic stainless steel) UNS S42000 AMS 2404E (electroless nickel plating) Background Surgical tools are defined as any device or instrument used during a surgical procedure. These tools range from simple knives...
Abstract
Several surgical tool failures were analyzed to understand why they occur and how to prevent them. The study included drills, catheters, and needles subjected to the rigors of biomedical applications such as corrosive environments, high stresses, sterilization, and improper cleaning procedures. Given the extreme conditions to which surgical tools can be exposed, and the potential for misuse, failures are inevitable and systematic methods for analyzing them are necessary to keep them in check.
Image
in Failure Investigations of PH 13-8 Mo Aircraft Components
> ASM Failure Analysis Case Histories: Air and Spacecraft
Published: 01 June 2019
Fig. 12 Tempered martensite microstructure of the PH 13-8 Mo stainless steel and transgranular internal crack from the shrink link cylinder wall (Vilella's etchant, ×1000).
More
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001371
EISBN: 978-1-62708-215-0
... for a quenched and tempered martensitic stainless steel. In general, these observations were made at the fracture origin as well as at locations remote from the primary fracture, indicating that the material was homogeneous, appeared to have been properly heat treated to obtain the specified mechanical...
Abstract
A type 410 stainless steel circulating water pump shaft used in a fossil power steam generation plant failed after more than 7 years of service. Visual examination showed the fracture surface to be coated with a thick, spalling, rust-colored scale, along with evidence of pitting. Samples for SEM fractography, EDS analysis, and metallography were taken at the crack initiation site. Hardness testing produced a value of approximately 27 HRC. The examinations clearly established that the shaft failed by fatigue. The fatigue crack originated at a localized region on the outside surface where pitting and intergranular cracking had occurred. The localized nature of the initial damage indicated that a corrosive medium had concentrated on the surface, probably due to a leaky seal. Reduction of hardness to 22 HRC or lower and inspection of seals were recommended to prevent future failures.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047566
EISBN: 978-1-62708-235-8
... stainless steel filler metal to form a fillet between the handle and the cover. The structure was found to contain a zone of brittle martensite in the portion of the weld adjacent to the low-carbon steel handle; fracture had occurred in this zone. The brittle martensite layer in the weld was the result...
Abstract
Handles welded to the top cover plate of a chemical-plant downcomer broke at the welds when the handles were used to lift the cover. The handles were fabricated of low-carbon steel rod; the cover was of type 502 stainless steel plate. The attachment welds were made with type 347 stainless steel filler metal to form a fillet between the handle and the cover. The structure was found to contain a zone of brittle martensite in the portion of the weld adjacent to the low-carbon steel handle; fracture had occurred in this zone. The brittle martensite layer in the weld was the result of using too large a welding rod and too much heat input, melting of the low-carbon steel handle, which diluted the austenitic stainless steel filler metal and formed martensitic steel in the weld zone. Because it was impractical to preheat and postheat the type 502 stainless steel cover plate, the low-carbon steel handle was welded to low-carbon steel plate, using low-carbon steel electrodes. This plate was then welded to the type 502 stainless steel plate with type 310 stainless steel electrodes. This design produced a large weld section over which the load was distributed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001609
EISBN: 978-1-62708-229-7
... in fully martensitic 12% Cr alloy 410 stainless steel ( Fig. 5 ). Fig. 5 Hardness vs. tempering temperature, Alloy 410 tempered for 2 h 17 Postweld heat treatment (PWHT) of alloy 430 at 760 °C (1400 °F) tempers martensite and replenishes Cr to depleted areas surrounding Cr carbide...
Abstract
Alloy 430 stainless steel tube-to-header welds failed in a heat recovery steam generator (HRSG) within one year of commissioning. The HRSG was in a combined cycle, gas-fired, combustion turbine electric power plant. Alloy 430, a 17% Cr ferritic stainless steel, was selected because of its resistance to chloride and sulfuric acid dewpoint corrosion under conditions potentially present in the HRSG low-pressure feedwater economizer. Intergranular corrosion and cracking were found in the weld metal and heat-affected zones. The hardness in these regions was up to 35 HRC, and the weld had received a postweld heat treatment (PWHT). Metallographic examination revealed that the corroded areas contained undertempered martensite. Fully tempered weld areas with a hardness of 93 HRB were not attacked. No evidence of corrosion fatigue was found. Uneven temperature control during PWHT was the most likely cause of failure.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0047579
EISBN: 978-1-62708-234-1
... deposits were of type 347 stainless steel, and the flanges were type 304 stainless steel. Metallographic examination of the failed studs revealed that the HAZs contained regions of martensite and that intergranular cracks, which initiated at the stud surfaces during welding, propagated to complete...
Abstract
Several fractures occurred in flange studs used for remote handling of radioactive equipment. The studs, of quenched-and-tempered type 414 stainless steel, fractured in the HAZs produced in the studs during the circumferential welding that joined the studs to the flanges. The weld deposits were of type 347 stainless steel, and the flanges were type 304 stainless steel. Metallographic examination of the failed studs revealed that the HAZs contained regions of martensite and that intergranular cracks, which initiated at the stud surfaces during welding, propagated to complete separation under subsequent loading. The studs fractured under service loads as a result of intergranular crack propagation in the HAZ. Rapid heating and cooling during attachment welding produced a martensitic structure in the HAZ of the stud, which cracked circumferentially from the combination of thermal-gradient and phase-change stresses. Joining the studs to the flanges by welding should be discontinued. They should be attached by screw threads, using a key and keyway to prevent turning in service.
1