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Book Chapter

Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0090994
EISBN: 978-1-62708-225-9
... Abstract Two large tension springs fractured during installation. The springs were manufactured from a grade 9254 chromium-silicon steel spring wire. The associated material specification allows wire in the cold-drawn or oil-tempered (quenched-and-tempered) condition. The specified wire tensile...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001227
EISBN: 978-1-62708-235-8
... Abstract An elbow of 70 mm OD and 10 mm wall thickness made from St 35.29, and exposed to 315 atmospheres internal pressure in an oil hydraulic shear installation, cracked lengthwise after a short operating period. Because the stress was not sufficient to explain the fracture of this elbow...
Book Chapter

Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c0090929
EISBN: 978-1-62708-236-5
... Abstract Size M5 x 0.8 mm, class 8.8 metric screws were failing during application, reportedly at the normal installation torque. Investigation (visual inspection, metallographic analysis, and unetched 8.9x fractographs) supported the conclusion that the fasteners failed via ductile overload...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001172
EISBN: 978-1-62708-220-4
... hydrogen attack and oxygen decarburization. A ring specimen was cut off from a high pressure line of unalloyed steel St 55.25 and was tested for hydrogen attack. The high pressure line was used for a gas mixture leaving the pressure vessel of an ammonia synthesis installation. The pressure...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001211
EISBN: 978-1-62708-235-8
Image
Published: 01 January 2002
Fig. 1 Typical inspections. (a) Automated inspection installation for the fluorescent penetrant inspection of large workpieces, such as castings. The installation incorporates a complex roller conveyor system. (b) Retirement-for-Cause (RFC) inspection facility More
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Published: 01 January 2002
Fig. 2 Ball mill liner plates. (a) New condition, before installation. (b) Worn condition, with partially worn grinding belt More
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Published: 01 January 2002
Fig. 2(a) Ruptured 305-mm (12-in.) carbon steel pipe, inadvertently installed in a 1.25Cr-0.5Mo circuit, that was severely damaged by hydrogen embrittlement. On-stream failure caused extensive fire damage. More
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Published: 01 June 2019
Fig. 1 Pipe coupling with cracks before installation. 1× More
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Published: 01 June 2019
Fig. 2 Schematic of installation of three service water pumps, where one pump is held in standby More
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Published: 01 June 2019
Fig. 6 The LANSCE window “insert” assembly prior to installation and radiation exposure More
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Published: 01 June 2019
Fig. 2 Failed outer ejector piston installed through the swaybrace assembly from an ejector rack. More
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Published: 01 June 2019
Fig. 4 Correct installation position of bracket. More
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Published: 01 June 2019
Fig. 5 Relative orientation of bracket depends on direction of installation. More
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Published: 01 December 1993
Fig. 1 View of load cell installation More
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Published: 01 June 2019
Fig. 2 Chipper knife being installed in a 75 in. Morbark total tree harvester More
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Published: 30 August 2021
Fig. 4 (a) Ruptured 305 mm (12 in.) carbon steel pipe, inadvertently installed in a 1.25Cr-0.5Mo circuit, that was severely damaged by hydrogen embrittlement. On-stream failure caused extensive fire damage. (b) Outside-diameter surface of the failed pipe. Hydrogen attack had progressed through More
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Published: 01 December 2019
Fig. 5 Another balance weight installed on long end of fractured roll More
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Published: 01 December 2019
Fig. 8 Balance weight that had been installed on short end of fractured roll; Arrow points to fractured screw originally located at origin of fracture More
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Published: 01 December 2019
Fig. 14 Crack shown in Fig. 13 now opened to expose screw as-installed and related fatigue crack surface More