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Victor K. Champagne, Gary Wechsler, Marc Pepi
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V.K. Champagne
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R.J.H. Wanhill
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J.W. Hutchinson
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Martin Roth, Karen Sander
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Richard H. McSwain
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D.S. Parker
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Helicopters
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Book Chapter
Failure of a Helicopter Rotor
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006444
EISBN: 978-1-62708-217-4
... Abstract Helicopter rotor blade components that included the horizontal hinge pin, the associated nut, and the locking washer were examined. Visual examination of the submitted parts revealed that the hinge pin, fabricated from 4340 steel, was broken and that the fracture face showed a flat...
Abstract
Helicopter rotor blade components that included the horizontal hinge pin, the associated nut, and the locking washer were examined. Visual examination of the submitted parts revealed that the hinge pin, fabricated from 4340 steel, was broken and that the fracture face showed a flat beach mark pattern indicative of a preexisting crack. The threaded area of the pin had an embedded thread that did not appear to come from the pin. A chemical analysis was conducted on the embedded thread and on an associated attachment to determine the origin of the thread. Analysis showed that the thread and nut were 4140 steel. Scanning electron fractographic examination of the fracture initiation site strongly suggested that the fracture progressed by fatigue. It was concluded that the failure of the horizontal hinge pin initiated at areas of localized corrosion pits. The pits in turn initiated fatigue cracks, resulting in a failure mode of corrosion fatigue. It was recommended that all of the horizontal hinge pins be inspected. Those pins determined to be satisfactory for further use should be stripped of cadmium, shot peened, and coated with cadmium to a minimum thickness of 0.0127 mm (0.0005 in.).
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001024
EISBN: 978-1-62708-214-3
... Abstract A Marine Corps helicopter crash was investigated. Efforts were directed to the failure of one of the main rotor blades that had apparently separated in the air. The apparent failure of a blade integrity monitor (BIM) system was also considered. The rotor blade comprised a long, hollow...
Abstract
A Marine Corps helicopter crash was investigated. Efforts were directed to the failure of one of the main rotor blades that had apparently separated in the air. The apparent failure of a blade integrity monitor (BIM) system was also considered. The rotor blade comprised a long, hollow 6061-T651 aluminum alloy extrusion and 26 fiberglass “pockets” that provided the trailing-edge airfoil shape. Visual examination of the fracture surface of the aluminum extrusion indicated fatigue crack growth followed by ductile overload separation. Examination of the fatigue fracture region revealed several pits that appeared to have acted as fracture origin sites. Time to failure was determined using fracture mechanics. It was concluded that failure was caused by a fatigue crack that grew to critical length without detection. The crack originated at pits that resulted from the use of an improperly designed heating element used to cure fiberglass repairs.
Book Chapter
Fatigue Fracture of a Spindle for a Helicopter Blade
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0046222
EISBN: 978-1-62708-217-4
... Abstract The spindle of a helicopter-rotor blade fractured after 7383 h of flight service. At every overhaul (the spindle that failed was overhauled six times and reworked twice), any spindle that showed wear was reworked by grinding the shank to 0.1 mm (0.004 in.) under the finished diam...
Abstract
The spindle of a helicopter-rotor blade fractured after 7383 h of flight service. At every overhaul (the spindle that failed was overhauled six times and reworked twice), any spindle that showed wear was reworked by grinding the shank to 0.1 mm (0.004 in.) under the finished diam. The spindle was then shot peened with S170 shot to an Almen intensity of 0.010 to 0.012 A. Following shot peening, the shank was nickel sulfamate plated to 0.05 mm (0.002 in.) over the finished diam, ground to finished size, and cadmium plated. Visual and stereomicroscopic exam showed faint grinding marks and circumferential grooves on the surface near the fillet at the junction of the shank and fork, which should have been peened over and covered with peening dimples. Evidence found supports the conclusions that the spindle failed in fatigue that originated near the junction of the shank and fork. The nonuniformity of the shot-peened effect on the shank and fillet portions of the spindle resulted from incomplete peeing. The fracture was of the low-stress high-cycle type, initiated by stresses well below the gross yield strength and propagated by thousands of load cycles. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001742
EISBN: 978-1-62708-217-4
... Abstract In a helicopter engine connecting rod, high-cycle, low-stress fatigue fractures in bolts and arms progressed about 75% across the section before the final rupture. Factors involved were insufficient specified preload, inadequate tightening during assembly, and engine overspeed...
Abstract
In a helicopter engine connecting rod, high-cycle, low-stress fatigue fractures in bolts and arms progressed about 75% across the section before the final rupture. Factors involved were insufficient specified preload, inadequate tightening during assembly, and engine overspeed. The assigned main causes were design deficiency, improper maintenance during overhaul, and abnormal service operation. The problem can be solved by proper overhauling that ensures bolted assemblies are tightened evenly and accurately, in accordance with recommended torque values. Also, the manufacturer made various modifications, such as a thicker rod, fatigue resistant bolts, and more accurate preload measurements. The configuration of these rods were changed to a tongue-and-groove design to increase service life.
Book Chapter
Failure Analysis of a Helicopter Main Rotor Bolt
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001381
EISBN: 978-1-62708-215-0
... Abstract A helicopter main rotor bolt failed in the black-coated region between the threads and the taper section of the shank during assembly. The torque applied was approximately 100 N·m (900 in.·lbf) when the bolt sheared. No other bolts were reported to have failed. The failed bolt material...
Abstract
A helicopter main rotor bolt failed in the black-coated region between the threads and the taper section of the shank during assembly. The torque applied was approximately 100 N·m (900 in.·lbf) when the bolt sheared. No other bolts were reported to have failed. The failed bolt material conformed to AISI E4340 steel, as specified. The microstructure was tempered martensite, with hardness ranging from 41 to 45 HRC. Failure was in the shear ductile mode. The crack initiated in the area of slag inclusions. Inspection of other bolts from the same shipment was recommended.
Book Chapter
Failed Mixer Pivot Support of An Army Attack Helicopter
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001293
EISBN: 978-1-62708-215-0
... Abstract A forged, cadmium-plated electroslag remelt (ESR) 4340 steel mixer pivot support of the rotor support assembly located on an Army attack helicopter was found to be broken in two pieces during an inspection. Visual inspection of the failed part revealed significant wear on surfaces...
Abstract
A forged, cadmium-plated electroslag remelt (ESR) 4340 steel mixer pivot support of the rotor support assembly located on an Army attack helicopter was found to be broken in two pieces during an inspection. Visual inspection of the failed part revealed significant wear on surfaces that contacted the bushing and areas at the machined radius where the cadmium coating had been damaged, which allowed corrosion pitting to occur. Optical microscopy showed that the crack origin was located at the machined radius within a region that was severely pitted. Electron microscopy revealed that most of the fracture surface failed in an intergranular fashion. Energy dispersive spectroscopy determined that deposits of sand, corrosion and salts were found within the pits. The failure started by hydrogen charging as a result of corrosion, and was aggravated by the stress concentration effects of pitting at the radius and the high notch sensitivity of the material. The failure mechanism was hydrogen-assisted and was most likely a combination of stress-corrosion cracking and corrosion fatigue. Recommendations were to improve the inspection criteria of the component in service and the material used in fabrication.
Book Chapter
Fatigue Fracture of an Aluminum Main Support Bridge for a Helicopter
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001600
EISBN: 978-1-62708-217-4
... Abstract This paper summarizes the results of a failure analysis investigation of a fractured main support bridge made of 7075 aluminum alloy from an army helicopter. The part, manufactured by “Contractor IT,” failed component fatigue testing while those of the original equipment manufacturer...
Abstract
This paper summarizes the results of a failure analysis investigation of a fractured main support bridge made of 7075 aluminum alloy from an army helicopter. The part, manufactured by “Contractor IT,” failed component fatigue testing while those of the original equipment manufacturer (OEM) passed. Metallurgical data collected during this investigation indicated that the difference in fatigue life between the components fabricated by IT and by OEM may be attributable to a difference in dimensions at the web where fatigue crack initiation occurred. The webs of the two OEM parts examined had cross-sectional thicknesses significantly larger than the web cross-sectional thicknesses of the IT components. Recommendations included changing the web reference dimension of 0.38 in. to include a tolerance range based upon a fracture mechanics model. Also, the shot peening process should be controlled especially at the critical areas of the web, to assure complete coverage and proper compressive residual stresses.
Book Chapter
Material-Based Failure Analysis of a Helicopter Rotor Hub
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001636
EISBN: 978-1-62708-217-4
... Abstract A Lynx helicopter from the Royal Netherlands Navy lost a rotor blade during preparation for take-off. The blade loss was due to failure of a rotor hub arm by fatigue. The arm was integral to the titanium alloy rotor hub. An extensive material based failure analysis covered the hub...
Abstract
A Lynx helicopter from the Royal Netherlands Navy lost a rotor blade during preparation for take-off. The blade loss was due to failure of a rotor hub arm by fatigue. The arm was integral to the titanium alloy rotor hub. An extensive material based failure analysis covered the hub manufacture, service damage, and estimates of service stresses. There was no evidence for failure due to poor material properties. However, fractographic and fracture mechanics analyses of the service failure, a full scale test failure, and specimen test failures indicated that the service fatigue stress history could have been more severe than anticipated. This possibility was subsequently supported by a separate investigation of the assumed and actual fatigue loads and stresses.
Book Chapter
Helicopter Main Rotor Transmission Output Shaft Failure
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001505
EISBN: 978-1-62708-217-4
... Abstract A helicopter had just taken off when there was a loud bang and the engine started to overspeed. After landing and inspection, the transmission was disassembled. It was discovered that the assembly containing the output shaft to the main rotor had failed. The output shaft assembly...
Abstract
A helicopter had just taken off when there was a loud bang and the engine started to overspeed. After landing and inspection, the transmission was disassembled. It was discovered that the assembly containing the output shaft to the main rotor had failed. The output shaft assembly was made up of two parts: the output shaft with an integral 10 in. diam upper disc at approximately mid-section; and a 10 in. diam lower disc. During manufacture, the lower disc was attached to the output shaft by an electron beam weld. The fracture had a single fatigue initiation site, coincident with the annular zone of remelted material on the inner surface of the disc. In the lower disc, the fracture was also 80% fatigue, but high stress, low cycle in nature and contained multiple initiation sites coincident with an electron beam weld bead. It was concluded that fatigue in the upper disc resulted from the presence of a metallurgical stress concentration caused by the electron weld beam impingement on the inner surface of the upper disc. An Airworthiness Directive was issued, and the manufacturer issued a mandatory service bulletin outlining a periodic inspection for the output shaft assembly.
Book Chapter
Fatigue Failure of a Carburized Steel Gear From a Helicopter Transmission
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001077
EISBN: 978-1-62708-214-3
... Abstract The failure of a spiral bevel gear from the transmission of a helicopter was discovered when the transmission was removed after an in-flight incident. Two adjacent teeth from the carburized AISI 9310 steel gear were found to have undergone fatigue failure. Internal initiation occurred...
Abstract
The failure of a spiral bevel gear from the transmission of a helicopter was discovered when the transmission was removed after an in-flight incident. Two adjacent teeth from the carburized AISI 9310 steel gear were found to have undergone fatigue failure. Internal initiation occurred in a region depleted of chromium and nickel. This condition coincides with a microstructural inhomogeneity consisting of large, soft ferrite grains. Its origin was probably contamination of the solidifying ingot during the consumable vacuum arc remelting operation.
Book Chapter
Processing-Induced Fatigue Fracture of a Helicopter Tail Rotor Blade
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001298
EISBN: 978-1-62708-215-0
... Abstract A helicopter tail rotor blade spar failed in fatigue, allowing the outer section of the blade to separate in flight. The 7075-T7351 aluminum alloy blade had fiberglass pockets. The blade spar was a hollow “D” shape, and corrosion pits were present on the inner surface of the hollow...
Abstract
A helicopter tail rotor blade spar failed in fatigue, allowing the outer section of the blade to separate in flight. The 7075-T7351 aluminum alloy blade had fiberglass pockets. The blade spar was a hollow “D” shape, and corrosion pits were present on the inner surface of the hollow spar A single corrosion pit, 0.38 mm (0.015 in.) deep, led to a fatigue failure of the spar The failure initiated on the pylon side of the blade. Dimensional analysis of the spar near the failure revealed measurements within engineering drawing tolerances. Though corrosion pitting was present, there was an absence of significant amounts of corrosion product and all of the pits were filled with corrosion-preventative primer. This indicated that the pitting occurred during spar manufacture, prior to the application of the primer The pitting resulted from multiple nickel plating and defective plating removal by acid etching. Post-plating baking operations subsequently reduced the fatigue strength of the spar.
Book Chapter
Analysis of a Helicopter Blade Fatigue Fracture by Digital Fractographic Imaging Analysis
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001144
EISBN: 978-1-62708-217-4
... Abstract A helicopter was hovering approximately 10 ft above a ship when one spar section failed explosively. Visual inspection revealed a crack had progressed through one member of a dual spar plate assembly at a fold pin lug hole. The remaining spar plate carried the blade load until...
Abstract
A helicopter was hovering approximately 10 ft above a ship when one spar section failed explosively. Visual inspection revealed a crack had progressed through one member of a dual spar plate assembly at a fold pin lug hole. The remaining spar plate carried the blade load until the aircraft was landed. The helicopter main rotor blade spar fracture was analyzed by conventional and advanced computerized fractographic techniques. Digital fractographic Imaging Analysis of theoretical and actual fracture surfaces was applied for automatic detection of fatigue striation spacing. The approach offered a means of quantification of fracture features, providing for objective fractography.
Book Chapter
Analysis of a Failed UH-1N Helicopter Main Rotor Blade Grip
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001510
EISBN: 978-1-62708-217-4
... direction that must be considered of primary importance in material selection for design configuration. A Navy UH-1N helicopter main rotor blade grip manufactured from a 2014-T6 aluminum alloy forging failed because of a design flaw that left a high residual tensile stress along the short transverse plane...
Abstract
Proper stress analysis during component design is imperative for accurate life and performance prediction. The total stress on a part is comprised of the applied design stress and any residual stress that may exist due to forming or machining operations. Stress-corrosion cracking may be defined as the spontaneous failure of a metal resulting from the combined effects of a corrosive environment and the effective component of tensile stress acting on the structure. However, because of the orientation dependence in aluminum, it is the residual stress occurring in the most susceptible direction that must be considered of primary importance in material selection for design configuration. A Navy UH-1N helicopter main rotor blade grip manufactured from a 2014-T6 aluminum alloy forging failed because of a design flaw that left a high residual tensile stress along the short transverse plane; this in turn provided the necessary condition for stress corrosion to initiate. A complete failure investigation to ascertain the exact cause of the failure was conducted utilizing stereomicroscopic examination, scanning electron microscopy, metallographic inspection and interpretation, energy-dispersive chemical analysis, physical and mechanical evaluation. Stereomicroscopic examination of the opened crack fracture surface revealed one large fan-shaped region that had propagated radially through the thickness of the material from two distinct origin areas on the internal diam of the grip. Higher magnification inspection near the origin area revealed a flat, wood-like appearance. Scanning electron microscopy divulged the presence of substantial mud cracking and intergranular separation on the fracture surface. Metallographic examination revealed intergranular cracking and substantial leaf separation along the elongated grains parallel to the fracture surface. Chemical composition and hardness requirements were found to be as specified. The blade grip failed due to a stress corrosion crack which initiated on the inner diam and propagated in the short transverse direction through the thickness of the component. The high residual tensile stress in the part resulting from the forging and exposed after machining of the inner diam, combined with the presence of moisture, provided the necessary conditions to facilitate crack initiation and propagation.
Book Chapter
Failed Main Rotor Pitch Horn Bolt from an Army Attack Helicopter
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001380
EISBN: 978-1-62708-215-0
... to be broken during a maintenance procedure on an Army attack helicopter. Applications The bolt is illustrated in Fig. 1 . Two pitch horn bolts are inserted into the pitch horn assembly which controls the pitch of the helicopter blades during flight. If one of these bolts were to fail in service...
Abstract
One of the two AISI 4340 steel pitch horn bolts from the main rotor hub assembly failed while in service. Optical microscope revealed evidence of corrosion pitting in regions adjacent to the fracture. Fractographic examination utilizing a scanning electron microscope revealed multiple crack origins which assumed a “thumbnail” shape and displayed surface morphologies which resulted from intergranular decohesion. Many of the crack sites initiated from corrosion pits. Energy dispersive spectroscope performed on areas within the crack initiation site showed the presence of chlorides. The failure was attributed to stress-corrosion cracking. Short- and long-term recommendations to prevent future failures are given.
Book Chapter
Fatigue Fracture of a Helicopter Tail Rotor Blade Due to Field-Induced Corrosion
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001297
EISBN: 978-1-62708-215-0
... Abstract A helicopter tail rotor blade spar failed in fatigue, allowing the blade to separate during flight. The 2014-T652 aluminum alloy blade had a hollow spar shank filled with lead wool ballast and a thermoset polymeric seal. A corrosion pit was present at the origin of the fatigue zone...
Abstract
A helicopter tail rotor blade spar failed in fatigue, allowing the blade to separate during flight. The 2014-T652 aluminum alloy blade had a hollow spar shank filled with lead wool ballast and a thermoset polymeric seal. A corrosion pit was present at the origin of the fatigue zone and numerous trails of corrosion pits were located on the spar cavity's inner surfaces. The corrosion pitting resulted from the failure of the thermoset seal in the spar shank cavity. The seal failure allowed moisture to enter into the cavity. The moisture then served as an electrolyte for galvanic corrosion between the lead wool ballast and the aluminum spar inner surface. The pitting initiated fatigue cracking which led to the spar failure.
Image
Fatigue cracking of a helicopter tail rotor blade. (a) Scanning electron mi...
Available to PurchasePublished: 01 January 2002
Fig. 6 Fatigue cracking of a helicopter tail rotor blade. (a) Scanning electron micrograph of the blade showing lead wool ballast in contact with the 2014-T652 aluminum spar bore cavity wall at the failure origin ∼13×. (b) Greater magnification (∼63×) in this same area shows the multiple pits
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Image
Cracked main rotor yoke from military helicopter. Arrow indicates the crack...
Available to PurchasePublished: 01 December 1992
Fig. 1 Cracked main rotor yoke from military helicopter. Arrow indicates the crack. ∼0.02×.
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Image
Remaining portion of helicopter tail rotor blade after spar failure and out...
Available to Purchase
in Processing-Induced Fatigue Fracture of a Helicopter Tail Rotor Blade
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1993
Fig. 1 Remaining portion of helicopter tail rotor blade after spar failure and outboard section separation. Approximately. 0.14×
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Image
Eyebolt which attaches rear lift strut to right wing of helicopter failed i...
Available to Purchase
in Corrosion-Induced Failures in Aircraft Components
> ASM Failure Analysis Case Histories: Air and Spacecraft
Published: 01 June 2019
Fig. 1 Eyebolt which attaches rear lift strut to right wing of helicopter failed in service. Note severe corrosion at and near fatigue failure origins in the last (run-out) thread root.
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Image
Corrosion fatigue of a 4340 steel helicopter rotor assembly. (a) Horizontal...
Available to PurchasePublished: 01 June 2019
Fig. 1 Corrosion fatigue of a 4340 steel helicopter rotor assembly. (a) Horizontal hinge pin. (b) Nut. (c) Locking washers. (d) and (e) Views of the hinge pin fracture surface. A beach mark is visible in (e). (f) Dent on one of the threaded surfaces of the horizontal hinge pin. (g) Corrosion
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