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Grain flow
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Image
Published: 01 January 2002
Fig. 29 Parting-line location and its influence on grain-flow pattern in a channel section forging. (a) Parting lines resulting in metal-flow patterns that cause forging defects. (b) Parting lines resulting in smooth flow lines at stressed sections
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Image
Published: 01 December 1993
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in Fatigue Fracture of Aluminum Wires in High-Voltage Electrical Cables in Alaska
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1992
Fig. 5 Metallographic cross section showing the grain flow characteristics and intergranular corrosion adjacent to fracture edge (arrow).
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Image
Published: 30 August 2021
Fig. 37 Section of a forged steel crankshaft showing beneficial grain flow around the geometrical features
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Image
in Failure of Steel Missile Launcher Attachment Bolts
> ASM Failure Analysis Case Histories: Air and Spacecraft
Published: 01 June 2019
Fig. 1 Macrograph showing grain flow within the threads of the LAU-7 bolt. Note the flow does not follow the contour of the threads, indicating the threads were cut (machined) rather than rolled. (12.5× magnification)
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047169
EISBN: 978-1-62708-217-4
... for aluminum alloy 2014-T6 and the hardness surpassed the minimum hardness required for aluminum alloy 2014-T6. An abrupt change in the direction of grain flow across the fracture plane indicated that the wall had buckled during forging. This evidence supported the conclusion that the wheel half failed...
Abstract
The flange on an outboard main-wheel half (aluminum alloy 2014-T6 forging) on a commercial aircraft fractured during takeoff. The failure was discovered later during a routine enroute check. The flange section that broke away was recovered at the airfield from which the plane took off and was thus available for examination. Failure occurred after 37 landings (about 298 roll km, or 185 roll miles). Examination of the fracture surfaces revealed that a forging defect was present in the wall of the wheel half. The anodized coating showed distinct twin-parallel and end-grain patterns between which the fracture occurred. The periphery of the defect was the site of several small fatigue cracks that eventually progressed through the remaining wall. Rapid fatigue then progressed circumferentially. Metallographic examination using Keller's reagent showed that the microstructure was normal for aluminum alloy 2014-T6 and the hardness surpassed the minimum hardness required for aluminum alloy 2014-T6. An abrupt change in the direction of grain flow across the fracture plane indicated that the wall had buckled during forging. This evidence supported the conclusion that the wheel half failed in the flange by fatigue as the result of a rather large subsurface forging defect. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001124
EISBN: 978-1-62708-214-3
... established that the fractures were caused by fatigue loading attributable to wind/thermal factors at the joints. The grain flow at the joints was transverse to the wire axis, rendering the notches of the joints sensitive to fatigue loading. An additional contributory factor was intergranular corrosion, which...
Abstract
Several wires in aluminum conductor cables fractured within 5 to 8 years of, service in Alaskan tundra. The cables were comprised of 19-wire strands; the wires were aluminum alloy 6201-T81. Visual and metallographic examinations of the cold-upset pressure weld joints in the wires established that the fractures were caused by fatigue loading attributable to wind/thermal factors at the joints. The grain flow at the joints was transverse to the wire axis, rendering the notches of the joints sensitive to fatigue loading. An additional contributory factor was intergranular corrosion, which assisted fatigue crack initiation/propagation. The failure was attributed to the departure of conductor quality from the requirements of ASTM B 398 and B 399, which specify that “no joints shall be made during final drawing or in the finished wire” and that the joints should not be closer than 15 m (50 ft). The failed cable did not meet either criterion. It was recommended that the replacement cable be inspected for strict compliance to ASTM requirements.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0046182
EISBN: 978-1-62708-218-1
... of the fracture surface revealed grain flow normal for this type of forging, but no visible defects. 400x metallographic examination of a section through the fracture surface showed that the microstructure was an acceptable tempered martensite. However, oxide inclusions were present at the fracture surface...
Abstract
A connecting cap from a truck engine fractured after 65,200 km (40,500 mi) of normal service. The cap was made from a 15B41 steel forging and was hardened to 29 to 35 HRC. Visual examination of the fracture surface disclosed an open forging defect across one of the outer corners of the cap. The defect extended approximately 9.5 mm (3/8 in.) along the side of the cap. The fracture surface exhibited beach marks typical of fatigue. The surface of the defect was stained, indicating that oxidation occurred either in heat treatment or in heating during forging. Deep etching of the fracture surface revealed grain flow normal for this type of forging, but no visible defects. 400x metallographic examination of a section through the fracture surface showed that the microstructure was an acceptable tempered martensite. However, oxide inclusions were present at the fracture surface. This evidence supported the conclusion that fatigue fracture initiated at a corner of the cap from a forging defect that extended to the surface. Fatigue cracking was propagated by cyclic loading inherent in the part. Recommendations included more careful fluorescent magnetic-particle inspection of the forged surfaces before machining and before putting the part into service.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047165
EISBN: 978-1-62708-217-4
... inspection, and micrographs with deep etching in aqueous 20% sodium hydroxide) supported the conclusion that failure on both wheel halves was by fatigue caused by a forging defect resulting from abnormal transverse grain flow. The crack in the first wheel half occurred during service, and the surfaces became...
Abstract
Two outboard main-wheel halves (aluminum alloy 2014-T6 forged) from a commercial aircraft were removed from service because of failure. One wheel half was in service for 54 days and had made 130 landings (about 1046 roll km, or 650 roll mi) when crack indications were discovered during eddy-current testing. The flange on the second wheel half failed after only 31 landings, when about 46 cm (18 in.) of the flange broke off as the aircraft was taxiing. Stains on the fracture surfaces were used to determine when cracking was initiated. The analysis (visual inspection, liquid penetrant inspection, and micrographs with deep etching in aqueous 20% sodium hydroxide) supported the conclusion that failure on both wheel halves was by fatigue caused by a forging defect resulting from abnormal transverse grain flow. The crack in the first wheel half occurred during service, and the surfaces became oxidized. Because the fracture surface of the second wheel half had chromic acid stains, it was obvious that the forging defect was open to the surface during anodizing. No recommendations were made except to notify the manufacturer.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001907
EISBN: 978-1-62708-217-4
... bolts Grain flow Carburizing Hy-Tuf UNS K325599 Heat treating related failures Metalworking related failures Stress-corrosion cracking Introduction Component: LAU-7 missile launcher attachment bolts Manufacturing defects: Machining rather than forging/inadvertent carburization...
Abstract
Aircraft missile launcher attachment bolts fabricated from cadmium-coated Hy-tuf steel were found broken. Subsequent analysis of the broken bolts indicated three causes of failure. First, the bolts had been carburized, which was not in conformance with the heat treating requirements. Second, macroetching showed that the bolts has been machined from stock rather than forged, and the threads cut rather than rolled. It was also determined that hydrogen-assisted stress-corrosion cracking also played a part in the failure of the high-strength bolts.
Image
Published: 30 August 2021
Fig. 5 Section through the forged head of a threaded fastener. The uniform grain flow minimizes stress raisers and unfavorable shear planes. Source: Ref 7
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Published: 01 January 2002
Fig. 6 Section through the forged head of a threaded fastener. The uniform grain flow minimizes stress raisers and unfavorable shear planes. Source: Ref 4
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Published: 01 June 2019
. Grain flow in this area was at an angle to applied stress, which resulted in end grain exposure. 105x. (d) SEM fractograph taken between the arrows in (b). Note intergranular fracture pattern indicative of SCC. 95x. (e) SEM taken near the termination of the fracture showing the crack still progressing
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Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001268
EISBN: 978-1-62708-215-0
..., as required. Fig. 2 Failed detent spring in the as-received condition. 0.2×. Metallography Microstructural Analysis Specimens taken from each of the nine leafs were sectioned and metallographically prepared to determine the direction of grain flow. The engineering drawing stated...
Abstract
A missile detached from a Navy fighter jet during a routine landing on an aircraft carrier deck because of a faulty missile launcher detent spring. Visual inspection of Inconel 718 detent spring assembly revealed that four of the nine spring leafs comprising the assembly were plastically deformed while two of the deformed leafs did not meet minimal hardness or tensile requirements. Liquid penetrant testing revealed no cracks or other surface discontinuities on the leaf springs. Material sectioned from the soft spring leafs was heat-treated according to specifications in the laboratory. The resultant increase in mechanical properties of the re-heat-treated material indicated that the original heat treatment was not performed correctly. The failure was attributed to improper heat treatment. Recommendations focused on more stringent quality control of the heat-treat operations.
Image
Published: 15 January 2021
Fig. 35 (a) Ti-6Al-4V forging. (b) Section through indication. ASTM 186 etch. (c) Tip of fold showing oxide and alpha case. 2% HF etch. (d) Steel fastener showing multiple laps in threads. (e) Section through lap showing grain flow around tip. ASTM 186 etch. Original magnification: 200×
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in Cracks in Forged Aircraft Wheel Halves That Originated From Forging Defects
> ASM Failure Analysis Case Histories: Air and Spacecraft
Published: 01 June 2019
on light gray fracture area). (c) Section through the crack and the disrupted grain flow. Etched with sodium hydroxide. Approximately 8 1 2 ×
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Book Chapter
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003507
EISBN: 978-1-62708-180-1
... formed parts cracking cracks forging grain flow heat treatment hydrogen content imperfections ingot pipe laminations metalworking nonmetallic inclusions pits porosity scabs seams sheet metal forming unmelted electrodes workability WROUGHT FORMS are produced by a wide variety...
Abstract
This article describes the general root causes of failure associated with wrought metals and metalworking. This includes a brief review of the discontinuities or imperfections that may be the common sources of failure-inducing defects in bulk working of wrought products. The article discusses the types of imperfections that can be traced to the original ingot product. These include chemical segregation; ingot pipe, porosity, and centerline shrinkage; high hydrogen content; nonmetallic inclusions; unmelted electrodes and shelf; and cracks, laminations, seams, pits, blisters, and scabs. The article provides a discussion on the imperfections found in steel forgings. The problems encountered in sheet metal forming are also discussed. The article concludes with information on the causes of failure in cold formed parts.
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006760
EISBN: 978-1-62708-295-2
... with circumferential lathe or grinding marks, the deformation may be difficult to see. Components with longitudinal features that have been subject to torsional overload, such as Fig. 11 , are readily identifiable. Altered grain flow and cold work are usually visible in the etched metallographic section. Fig. 11...
Abstract
Visual examination, using the unaided eye or a low-power optical magnifier, is typically one of the first steps in a failure investigation. This article presents the guidelines for selecting samples for scanning electron microscope examination and optical metallography and for cleaning fracture surfaces. It discusses damage characterization of metals, covering various factors that influence the damage, namely stress, aggressive environment, temperature, and discontinuities.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006406
EISBN: 978-1-62708-217-4
...). Suspected multiple initiation sites are located between arrows. 1.5x. (c) Section of flange with surface at right. Grain flow in this area was at an angle to applied stress, which resulted in end grain exposure. 105x. (d) SEM fractograph taken between the arrows in (b). Note intergranular fracture pattern...
Abstract
A crack was found in an aircraft main wing spar flange fabricated from 7079-T6 aluminum alloy during a routine nondestructive x-ray inspection after the craft had logged 300 h. Scanning electron microscopy (SEM) revealed an intergranular fracture pattern indicative of stress-corrosion cracking (SCC) and fatigue striations near the crack origin. Visual examination of the crack edge revealed that the installation of the fasteners produced a fit up stress. Further inspection of the opened fracture showed that the crack had been present for some time because a heavy buildup of corrosion products was seen on the fractured surface. Metallographic examination of the flange in the area of fracture initiation showed the presence of end grain exposure, which would promote SCC. Electron optical examination of the fracture clearly showed the flange was cracking by a mixed mode of stress corrosion and fatigue. The cracking was accelerated because of an inadvertent fit up stress during installation. The age of the crack could not be established. However, a reevaluation of prior x-ray inspections in this area would result in some close estimate of the age of the crack. End grain exposure further promoted SCC.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048757
EISBN: 978-1-62708-234-1
... by subjecting the overheated tube to a flattening test that the tube no longer met ASTM B 337 specifications. Large grain size and numerous needlelike hydride particles were disclosed in the microstructure of the overheated tube. Heating to approximately 815 deg C was revealed by the presence of the flaky oxide...
Abstract
Brief overheating of the 89 mm OD 6.4 mm wall thickness titanium heater tubes (ASTM B337, grade 2) was caused by a flow stoppage in a leach heater. Blue-tinted areas and patches of flaky white, yellow, and brown oxide scale was revealed on visual examination. It was disclosed by subjecting the overheated tube to a flattening test that the tube no longer met ASTM B 337 specifications. Large grain size and numerous needlelike hydride particles were disclosed in the microstructure of the overheated tube. Heating to approximately 815 deg C was revealed by the presence of the flaky oxide and increased grain size. Hydrogen and oxygen absorption was revealed by the presence of hydrides and the shallow surface embrittlement and thus susceptibility to cracking at ambient temperatures was observed. It was concluded that the titanium tubes were embrittled due to overheating the tubes and the severe surface embrittlement resulted from oxygen absorption which made the surface layers susceptible to cracking under start up and shutdown. Replacement tubes made of a heat-resistant alloy (e.g., Hastelloy C-276) were recommended.
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