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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0046227
EISBN: 978-1-62708-217-4
... Abstract The floors (fabricated from aluminum alloy 7178-T6 sheet, with portions of the sheet chemically milled to reduce thickness) of the fuel tanks in two aircraft failed almost identically after 1076 and 1323 h of service, respectively. Failure in both tanks occurred in the rear chemically...
Abstract
The floors (fabricated from aluminum alloy 7178-T6 sheet, with portions of the sheet chemically milled to reduce thickness) of the fuel tanks in two aircraft failed almost identically after 1076 and 1323 h of service, respectively. Failure in both tanks occurred in the rear chemically milled section of the floor. An alkaline etch-type cleaner was used on the panels before chemical milling and before painting. Various tests and measurements indicated that the aluminum alloy used for the fuel-tank floors conformed to the specifications for 7178-T6. Low power magnification, fractographs taken with a scanning electron, and optical microscopic examination of the milled sections revealed extensive pitting on both sides of the floors. Evidence found supports the conclusions that the floors failed by fatigue cracking that initiated near the center of the fuel-tank floor and ultimately propagated as rapid ductile-overload fractures. The fatigue cracks originated in pits on the fuel-cell side of the tank floors. The pits were attributed to attack caused by the alkaline-etch cleaning process. Recommendations included monitoring of the alkaline-etch cleaning to avoid the formation of pits and careful inspection following alkaline-etch cleaning, to be scheduled before release of the floor panels for painting.
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Published: 01 January 2002
Fig. 21 Cracking in floor-beam-girder connection plates. (a) Cracks in the outside web surface. (b) Cracks from the inside web surface
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Published: 01 January 2002
Fig. 29 Cracking in a floor-beam web above the end of the riveted angle end connection. (a) Floor beam/tie girder connection. (b) Crack along the web-flange weld above the end connection
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Published: 01 January 2002
Fig. 3 View of an isolated pit on the outside of the floor tank of a liquid asphalt tank. The asphalt had been leaking for some time as the surrounding area was covered with deposits and the wall thinning was significant. Courtesy of S.R. Freeman, Millennium Metallurgy, Ltd.
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in Failure Analysis of an Automobile Weldment
> ASM Failure Analysis Case Histories: Automobiles and Trucks
Published: 01 June 2019
Fig. 2 Buckled floor pan with crimp just behind rear seat. Note (arrow) seat belt retractor anchor bolt just to left of crimp.
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in Failure Analysis of an Automobile Weldment
> ASM Failure Analysis Case Histories: Automobiles and Trucks
Published: 01 June 2019
Fig. 6 Matching sections of lower floor sill and rocker panel weld assembly. Arrow shows only sight of weld nugget “pull out”
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in Fatigue Fracture of Aluminum Alloy 7178-T6 Aircraft Fuel-Tank Floors
> ASM Failure Analysis Case Histories: Air and Spacecraft
Published: 01 June 2019
Fig. 1 Aluminum alloy 7178-T6 floor of an aircraft fuel tank that failed by fatigue because of alkaline cleaning of the metal before painting. (a) Floor of the fuel tank showing extent of fracture. Dimensions given in inches. (b) Fracture surface showing fatigue marks and dimples indicating
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in Analysis of a Corrosion Failure of an Aboveground Storage Tank
> ASM Failure Analysis Case Histories: Chemical Processing Equipment
Published: 01 June 2019
Fig. 1 View of an isolated pit on the outside of the floor tank of a liquid asphalt tank. The asphalt had been leaking for some time as the surrounding area was covered with deposits and the wall thinning was significant. Courtesy of S.R. Freeman, Millennium Metallurgy, Ltd.
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001514
EISBN: 978-1-62708-218-1
... Abstract A front-wheel drive hatchback automobile was involved in a severe front end impact. Failure analysis of the automobile revealed only a single sound spot weld in each of two 66 cm (26 in.) sections of both upper and lower floor sill flanges. Consequently, upon impact, the floor pan...
Abstract
A front-wheel drive hatchback automobile was involved in a severe front end impact. Failure analysis of the automobile revealed only a single sound spot weld in each of two 66 cm (26 in.) sections of both upper and lower floor sill flanges. Consequently, upon impact, the floor pan separated from the rocker panel, buckled and rotated upward and forward. This introduced slack in the seat belts since their retractors, being anchored to the floor pan, also rotated forward. Although not contributory to the accident itself, the faulty welds were responsible in part for the severity of the injuries sustained by the driver. The faulty welds in the unit body were apparently a consequence of improper settings of parameters on a multihead electrical resistance spot welding machine. Lack of appreciation of the hazard associated with failure of this weldment may have contributed to the low frequency of their physical inspection during production. A similar case involving faulty welds in a fuel delivery truck is also discussed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0091208
EISBN: 978-1-62708-220-4
... Abstract A failure of an aboveground storage tank occurred due to external corrosion of the tank floor. The liquid asphalt tank operated at elevated temperatures (approximately 177 deg C, or 350 deg F) and had been in service for six years. Cathodic protection (rectifiers) had been installed...
Abstract
A failure of an aboveground storage tank occurred due to external corrosion of the tank floor. The liquid asphalt tank operated at elevated temperatures (approximately 177 deg C, or 350 deg F) and had been in service for six years. Cathodic protection (rectifiers) had been installed since start-up of the tank operation. It was noted, however, that some operational problems with the rectifier may have interrupted its protection. Investigation (visual inspection, on-site examination and testing, EDS analysis of scale deposits, and MIC testing of the soil) supported the conclusion that corrosion may have been caused by an interruption in cathodic protection. The effectiveness of cathodic protection on established microbial deposits is questionable. Recommendations included ultrasonically testing the tank floor and replacing portions based on the remaining wall thickness. Doubling the wall thickness of the floor plates was also recommended.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0001821
EISBN: 978-1-62708-180-1
... Abstract This article illustrates the defects, which result because of poor-quality welds in the bridge components. The cracks resulting from the use of low fatigue strength details are also discussed. The article describes the effect of out-of-plane distortion in floor-beam-girder connection...
Abstract
This article illustrates the defects, which result because of poor-quality welds in the bridge components. The cracks resulting from the use of low fatigue strength details are also discussed. The article describes the effect of out-of-plane distortion in floor-beam-girder connection plates, multiple-girder diaphragm connection plate, and tied-arch floor beams.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0046956
EISBN: 978-1-62708-232-7
... was reported to have been closely controlled at the normal temperature of 1175 deg C (2150 deg F); a hydrogen atmosphere was used during brazing. After about five months of continuous operation, four or five holes developed on the floor of the muffle, and the muffle was removed from service. Analysis (visual...
Abstract
A brazing-furnace muffle 34 cm (13 in.) wide, 26 cm (10 in.) high, and 198 cm (78 in.) long, was fabricated from nickel-base high-temperature alloy sheet and installed in a gas-fired furnace used for copper brazing of various assemblies. The operating temperature of the muffle was reported to have been closely controlled at the normal temperature of 1175 deg C (2150 deg F); a hydrogen atmosphere was used during brazing. After about five months of continuous operation, four or five holes developed on the floor of the muffle, and the muffle was removed from service. Analysis (visual inspection, x-ray spectrometry, and metallographic examination) supported the conclusion that the muffle failed by localized overheating in some areas to temperatures exceeding 1260 deg C (2300 deg F). The copper found near the holes had dripped to the floor from assemblies during brazing. The copper diffused into the nickel-base alloy and formed a grain-boundary phase that was molten at the operating temperature. The presence of this phase caused localized liquefaction and weakened the alloy sufficiently to allow formation of the holes. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001274
EISBN: 978-1-62708-215-0
... deflection of the tray handles that had occurred in the failed tray. Full distortion of the handles was obtained experimentally only by dropping a full hot tray on its end onto the floor. The test results indicated that the tray had slipped from the hand of the user. Bending Deflection Food packaging...
Abstract
A laminated-paper microwave food tray collapsed with hot food in it. Microscopic examination of the failed tray revealed no structural or material defects. Five additional trays of like construction were also tested to determine the conditions necessary to simulate the permanent deflection of the tray handles that had occurred in the failed tray. Full distortion of the handles was obtained experimentally only by dropping a full hot tray on its end onto the floor. The test results indicated that the tray had slipped from the hand of the user.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0045909
EISBN: 978-1-62708-232-7
... Abstract A hot rolled, low-carbon steel pot used to melt magnesium alloys leaked, releasing about 35 kg (80 lb) of molten magnesium onto the foundry floor and causing an extensive fire. Due to the fire, the original leakage hole could not be investigated. Samples of the failed pot were polished...
Abstract
A hot rolled, low-carbon steel pot used to melt magnesium alloys leaked, releasing about 35 kg (80 lb) of molten magnesium onto the foundry floor and causing an extensive fire. Due to the fire, the original leakage hole could not be investigated. Samples of the failed pot were polished and etched and were found to be composed of ferrite and pearlite mixtures, as would be expected. However, the sample taken from a location about 75 mm (3 in.) from the hole contained a cluster of unusually large inclusions. By removing the beryllium window from in front of the detector, EPMA spectra were obtained from the inclusions and from the steel matrix. The inclusion spectrum contained primarily iron and oxygen, whereas the matrix spectrum contained primarily iron. X-ray maps were made to show the distribution of iron and oxygen. These results indicated that the inclusions were iron oxide. A similar inclusion at the failure site in the melting pot may have reacted violently with the molten magnesium, causing the leak.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0046998
EISBN: 978-1-62708-232-7
... in.). Failure occurred where the tube passed through the refractory hearth (floor) of the furnace. Although the furnace atmosphere was neutral with respect to the work, it had a carburizing potential relative to the radiant tubes. Analysis (visual inspection, 250x spectroscopic examination of specimens etched...
Abstract
One of 14 vertical radiant tubes (RA 333 alloy) in a heat-treating furnace failed when a hole about 5 x 12.5 cm (2 x 5 in.) corroded completely through the tube wall. The tube measured 183 cm (72 in.) in length and 8.9 cm (3 in.) in OD and had a wall thickness of about 3 mm (0.120 in.). Failure occurred where the tube passed through the refractory hearth (floor) of the furnace. Although the furnace atmosphere was neutral with respect to the work, it had a carburizing potential relative to the radiant tubes. Analysis (visual inspection, 250x spectroscopic examination of specimens etched with mixed acids, metallographic examination, and chemical analysis) supported the conclusions that the premature failure of the tube by perforation at the hearth level resulted from (1) corrosion caused by sulfur contamination from the refractory cement in contact with the tube and (2) severe local overheating at the same location. Recommendations included replacing all tubes using a low sulfur refractory cement in installation and controlling burner positioning and regulation more closely to avoid excessive heat input at the hearth level.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c9001444
EISBN: 978-1-62708-231-0
...) was dropped from a height of approximately 6 ft on to a concrete floor and it fractured into 11 pieces, each break occurring at a slot. The sample piece submitted for examination showed a wholly brittle fracture at each end, the fractures having originated at the sharp corners of the slots. During flame...
Abstract
To permit bolting of a 90 lb/yd. flat-bottomed rail to a steel structure, rectangular slots 2 in. wide x 1 in. deep were flame-cut in the base of the rail at 2 ft intervals to suit existing bolt holes. During subsequent handling, one of the rails (which were about 25 ft long) was dropped from a height of approximately 6 ft on to a concrete floor and it fractured into 11 pieces, each break occurring at a slot. The sample piece submitted for examination showed a wholly brittle fracture at each end, the fractures having originated at the sharp corners of the slots. During flame-cutting, a narrow band of material on each side of the cut was raised above the hardening temperature. When the torch had passed the rate of abstraction of heat from this zone by conduction into the cold mass of the rail was sufficiently rapid to amount to a quench and thus cause local hardening. The steel in the regions of the slots possessed little capacity for deformation, and fracturing of the martensitic layer, under cooling or impact stresses, would be likely to occur. The slots should have been cut mechanically.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0047113
EISBN: 978-1-62708-219-8
... Abstract A portion of a 19 mm (0.75 in.) diam structural steel bolt was found on the floor of a manufacturing shop. This shop contained an overhead crane system that ran on rails supported by girders and columns. Inspection of the crane system revealed that the bolt had come from a joint...
Abstract
A portion of a 19 mm (0.75 in.) diam structural steel bolt was found on the floor of a manufacturing shop. This shop contained an overhead crane system that ran on rails supported by girders and columns. Inspection of the crane system revealed that the bolt had come from a joint in the supporting girders and could be considered one of the principal fasteners in the track system. Analysis (visual inspection, metallographic exam, and hardness testing) supported the conclusions that fatigue induced by the overhead movement of the crane produced failure of the bolt. The bolt was deficient in strength for the cyclic applied loads in this case and probably was not tightened sufficiently. Recommendations included removing the remaining bolts in the crane support assembly and replacing them with a higher-strength, more fatigue-resistant bolt, for example, SAE grade F, 104 to 108 HRB. The bolts should be tightened according to the specifications of the manufacturer, and the system should be periodically inspected for correct tightness.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0091330
EISBN: 978-1-62708-234-1
... Abstract At a power plant, C-276 nickel alloy welds (N10276) on a C-276 duct floor completely disappeared in less than half a year. A continuous supply of flue gas came in contact with the closed bypass duct. The unscrubbed combustion products condensed on the cold duct, then the closed damper...
Abstract
At a power plant, C-276 nickel alloy welds (N10276) on a C-276 duct floor completely disappeared in less than half a year. A continuous supply of flue gas came in contact with the closed bypass duct. The unscrubbed combustion products condensed on the cold duct, then the closed damper conducted heat from the chimney and reheated the condensate. Investigation (visual inspection and welded coupon testing) supported the conclusion that the corrosion was caused by “Green Death,” a corrosive medium used to test for pitting resistance (11.9% H2SO4 + 1.3% HCl + 1% FeCl3 + 1% CuCl2) at 103 deg C (217 deg F). Such conditions exist at power plants. Recommendations included repairing the C-276 plates with a 686CPT weld alloy, and if that did not correct the situation, replacing the plates with 686 plate (N06686) welded with 686 CPT.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0048091
EISBN: 978-1-62708-224-2
... Abstract A section from a stop-block guide fell to the floor on a crane runway after it failed. A brittle crystalline-type break was disclosed by examination of the fracture surface. The point of initiation was in a hardened heat-affected layer that had developed during flame cutting...
Abstract
A section from a stop-block guide fell to the floor on a crane runway after it failed. A brittle crystalline-type break was disclosed by examination of the fracture surface. The point of initiation was in a hardened heat-affected layer that had developed during flame cutting and welding. The metal was identified to be 1020 steel. It was indicated by the coarse as-rolled structure (grain size of ASTM 00 to 4) of the base metal that the weldment (stop block and guide) had not been normalized. The brittle failure was evaluated to have been initiated at a metallurgical and mechanical notch produced by flame cutting and welding. As corrective measures, fully silicon-killed 1020 steel with a maximum grain size of ASTM 5 were used to make new stop-block weldments. The weldments were normalized at 900 deg C after flame cutting and welding to improve microstructure and impact strength. All flame-cut surfaces were ground to remove notches.
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in Avoiding Plastic Product Failure by Proper Plastic Selection and Design
> Characterization and Failure Analysis of Plastics
Published: 15 May 2022
Fig. 6 Computer simulation of a weighted glass-reinforced polycarbonate chassis being dropped onto a concrete floor
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