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Disintegration
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c9001223
EISBN: 978-1-62708-233-4
... been applied. Microscopic examination showed grain disintegration was promoted by the thickness of the weld bead and the amount of heat required to produce it. If nonstabilized austenitic sheet is to be used in the future, one of the particularly low-carbon steels, X2 CrNi 18 9 or X2 CrNiMo 18 10...
Abstract
The corner of a welded sheet construction made from austenitic corrosion-resistant chromium-nickel steel showed corrosive attack of the outer sheet. This attack was most severe at the points subjected to the greatest heat during welding. Particularly large amounts of weld metal had been applied. Microscopic examination showed grain disintegration was promoted by the thickness of the weld bead and the amount of heat required to produce it. If nonstabilized austenitic sheet is to be used in the future, one of the particularly low-carbon steels, X2 CrNi 18 9 or X2 CrNiMo 18 10, is recommended.
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in Failure of a Type 317L Stainless Steel Clad Bottom Cone of an Acid Sulfite Pulping Batch Digester
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1992
Fig. 4 Disintegration of stainless steel cladding from TGSCC, resulting in exposure of carbon steel base metal and hemispherical corrosion pits.
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in A Survey of the Causes of Failure of Rolling Bearings
> ASM Failure Analysis Case Histories: Mechanical and Machine Components
Published: 01 June 2019
Fig. 14 Showing Plastic distortion of rollers and disintegration of the cage of a roller bearing.
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in Screen Bars Destroyed by Intergranular Corrosion
> ASM Failure Analysis Case Histories: Chemical Processing Equipment
Published: 01 June 2019
Fig. 7 Transverse section through the transition zone between the disintegrated region and the corrosion-free region, unetched. 100 ×
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Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001106
EISBN: 978-1-62708-214-3
... Abstract Three radiant heating element tubes from an aluminum holding furnace failed after a few months of service. One side of each of the tubes had disintegrated, leaving large holes and thinned cross sections. Microstructural analysis showed that the surface of the tube had been oxidized...
Abstract
Three radiant heating element tubes from an aluminum holding furnace failed after a few months of service. One side of each of the tubes had disintegrated, leaving large holes and thinned cross sections. Microstructural analysis showed that the surface of the tube had been oxidized along the grain boundaries and had extensive precipitation inside the grains. Chemical analysis indicated that the steel used for the tubes was AISI type 316 stainless steel Specifications for the tubes had called for AISI type 310S to be used. It was recommended that other tubes made from the same batch of steel sheet be checked.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001778
EISBN: 978-1-62708-241-9
... to disintegration/failure of individual groups of wires. To understand the genesis of LCTR wire failures, a detailed metallurgical investigation of failed rope wires was made and included visual examination, optical microscopy, scanning electron microscopy (SEM), and electron probe microanalysis (EPMA). Two types...
Abstract
A locked coil track rope (LCTR) is essentially composed of wires (round and rail-shaped) laid helically in different layers. These wire ropes are sometimes used in conveyors carrying empty and loaded buckets in mining areas. During service, such wire ropes may fail prematurely due to disintegration/failure of individual groups of wires. To understand the genesis of LCTR wire failures, a detailed metallurgical investigation of failed rope wires was made and included visual examination, optical microscopy, scanning electron microscopy (SEM), and electron probe microanalysis (EPMA). Two types of failed wires were investigated; one is from a 40 mm diameter locked coil track rope and the other from a 53 mm locked coil track rope. Optical microscopy of failed round wires in the 53 mm diameter rope clearly revealed fully decarburized layers at the surface and a few grain-boundary cracks. From the location of the failure, it was clear that apart from static tensile loads, the wire ropes had been subjected to bending and unbending loads near the saddle, as fully loaded or empty buckets traveled access the conveyor. The SEM studies confirmed that the fracture had been caused by initiation of fatigue cracks in the decarburized zone under conditions of repeated bending and unbending stresses superimposed on the static tensile load.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001363
EISBN: 978-1-62708-215-0
... by excessive heating, causing cage disintegration, plastic flow of the races and balls, and eventual separation of inner and outer races. It was recommended that the bearing set be resized to accommodate the large thrust as and that a thermocouple be added to monitor the condition of the bearing during testing...
Abstract
An accidental overspeed condition during wind tunnel testing resulted in the destruction of a propeller rotor The occurrence was initially attributed to malfunction in the collective pitch control system. All fractured parts in the system were inspected. Highly suspect parts, including the pitch control thrust bearing set, head bolts, hub fork, and actuator rod end, were examined in more detail The thrust bearing set (52100 steel) was identified as the probable source of the uncommanded pitch angle change. A complete failure analysis of the bearing indicated that failure was precipitated by excessive heating, causing cage disintegration, plastic flow of the races and balls, and eventual separation of inner and outer races. It was recommended that the bearing set be resized to accommodate the large thrust as and that a thermocouple be added to monitor the condition of the bearing during testing.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048397
EISBN: 978-1-62708-226-6
... Abstract A large portion of the four-hole Lane plate disintegrated and consisted mainly of corrosion products after remaining in the body for 26 years. Transformation structures and carbides were exhibited by the plate which was made from chromium steel. Minimal corrosion was exhibited...
Abstract
A large portion of the four-hole Lane plate disintegrated and consisted mainly of corrosion products after remaining in the body for 26 years. Transformation structures and carbides were exhibited by the plate which was made from chromium steel. Minimal corrosion was exhibited by the soft austenitic 304 stainless steel used to make the screws. The corrosion products of the plate were revealed by microprobe analysis to impregnate the surrounding tissues. Improper material selection was concluded to be the reason for the general corrosion behavior.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001255
EISBN: 978-1-62708-232-7
... of this roll and the other broken rolls, the cracking and fracture were promoted by various casting defects. Investigation of the rolls showed that both the breaking off of the neck and the disintegration of the barrel edges was caused by material defects, more exactly casting defects. The fractures...
Abstract
Several back up rolls of 1400 mm barrel diam from a broad strip mill broke after a relatively short operating time as a result of bending stresses when the rolls were dismantled. The fracture occurred in the conical region of the neck at about 600 mm diam. The rolls were shaped steel castings with 0.8 to 1.0% C, 1% Mn, 1% Cr, 0.5% Mo and 0.4% Ni and were heat treated to a tensile strength of 950 N/sq mm. Because the bending stress on mounting was only 42 N/sq mm in the fracture cross section, it was evident at the outset that material defects had promoted the fracture. In the case of this roll and the other broken rolls, the cracking and fracture were promoted by various casting defects. Investigation of the rolls showed that both the breaking off of the neck and the disintegration of the barrel edges was caused by material defects, more exactly casting defects. The fractures on the other rolls examined were so badly rusted or contaminated that they were incapable of yielding any information.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001748
EISBN: 978-1-62708-225-9
... Abstract A pinion gear made of AMS 6470 steel, nitrided all over, lost internal splined teeth due to wear. Spline failure of the power turbine gear caused an engine overspeed and disintegration. Excessive spline wear resulted from a new coupling being mated during overhaul with a worn gear...
Abstract
A pinion gear made of AMS 6470 steel, nitrided all over, lost internal splined teeth due to wear. Spline failure of the power turbine gear caused an engine overspeed and disintegration. Excessive spline wear resulted from a new coupling being mated during overhaul with a worn gear spline. Wear on the spline teeth flanks of the coupling was attributed to severe wear on the mating gear (internal) spline teeth. The assigned cause was an inadequate maintenance procedure which resulted in a wear-damaged component being retained in the power train during engine overhaul. To prevent reoccurrence, specific inspection criteria were issued defining maximum limits for spline wear. A procedure and requirements were specified for installing the coupling and pinion gear at the next overhaul.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001469
EISBN: 978-1-62708-229-7
... for a sufficient number of cycles to produce an extensive system of fatigue cracks that resulted in partial disintegration of the ring. Microscopic examination of the material showed it to be a mild steel of satisfactory quality. The trouble was started by slight leakage, possibly resulting from a relaxation...
Abstract
In a main range in a power station, steam was conveyed at a pressure of 645 psi, and a temperature of 454 deg C (850 deg F). Pipe diameter was 9 in. and the joints were of the bolted type in which a thin steel ring, serrated on both sides, was inserted between plain flanges. Thin jointing material was interposed between the serrated faces and the flanges. The first intimation of trouble was the onset of a high pitched noise audible over a radius of a quarter of a mile. The noise arose from violent lateral vibration of the serrated ring, which attained an amplitude and persisted for a sufficient number of cycles to produce an extensive system of fatigue cracks that resulted in partial disintegration of the ring. Microscopic examination of the material showed it to be a mild steel of satisfactory quality. The trouble was started by slight leakage, possibly resulting from a relaxation of the interfacial pressure on the joint faces, which eroded away the joint material locally at one face of the serrated ring. This reduced interfacial pressure at the opposite face of the ring, with resultant leakage and erosion of the joint material on this side.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001180
EISBN: 978-1-62708-219-8
... Abstract A T-piece from a copper hot water system failed. Microscopic examination of a polished section revealed a main crack and branching transcrystalline cracks running from the outer surface of the pipe into the pipe wall. The crack appearance indicated disintegration by stress-corrosion...
Abstract
A T-piece from a copper hot water system failed. Microscopic examination of a polished section revealed a main crack and branching transcrystalline cracks running from the outer surface of the pipe into the pipe wall. The crack appearance indicated disintegration by stress-corrosion cracking. Although copper is not susceptible in the pure state, it is prone to stress-corrosion cracking under tensile stress in the presence of other elements in a damp ammoniacal atmosphere. The material was not defective, but a phosphorus-deoxidized copper type. The residual phosphorus combined with oxygen to form phosphorus pentoxide. Hard soldering in turn prevented the formation of cuprous oxide, and hydrogen embrittlement occurred.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001475
EISBN: 978-1-62708-234-1
... Abstract During periodic inspection of the tubes of a reformer furnace, a soapy water leak test with the tubes pressurized with nitrogen was being carried out by site personnel in a manner contrary to the policy of the organization when one of the tubes suddenly disintegrated with explosive...
Abstract
During periodic inspection of the tubes of a reformer furnace, a soapy water leak test with the tubes pressurized with nitrogen was being carried out by site personnel in a manner contrary to the policy of the organization when one of the tubes suddenly disintegrated with explosive violence. The tube approximately 30 ft. long by 6 in. diam, was constructed of three spun cast sections butt welded together. The material specified for tubes for this service was basically a 25% chromium, 20% nickel, cast stainless steel containing 0.4% carbon to optimize creep resistance. Failure initiated in the region of the tube where the dark fracture surface and columnar grain structure were evident. These features indicated the presence of a defective zone or progressive cracking which had occurred during service. Microscopic examination of sections through the zone revealed extensive creep cracking. The cracking was intergranular and followed the interdendritic columnar structure adjacent to the outer surface.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001160
EISBN: 978-1-62708-220-4
... with fine branching cracks and was flaking off. Microscopic examination showed that the unetched polished material had disintegrated to an average depth of 1 mm below the surface. A micrograph of the etched surface revealed numerous deformation lines and transgranular cracking. The failure was thus due...
Abstract
A corrosion resistant chromium nickel steel (X 2 Cr-Ni-Mo 18 10) worm drive used in a chemical plant at 80 deg C and 100 to 200 atm pressure to transport media containing chloride failed during normal operation. Visual inspections showed that the entire surface of the gear was covered with fine branching cracks and was flaking off. Microscopic examination showed that the unetched polished material had disintegrated to an average depth of 1 mm below the surface. A micrograph of the etched surface revealed numerous deformation lines and transgranular cracking. The failure was thus due to stress-corrosion cracking and additional corrosion due to ventilation elements. Because austenitic chromium nickel steels are prone to stress-corrosion cracking, particularly in the presence of chlorine compounds at high temperatures, and because austenitic rust- and acid-resistant steels are prone to smearing and work hardening during machining, it was recommended that these types of steels be machined only with sharp, short tools mounted in rigid structures. In addition, residual stresses should be eliminated by post-process annealing in a protective atmosphere.
Image
Published: 01 December 1992
Fig. 5 Corrosion of type 316 stainless steel wick and Inconel 600 at various locations within the fin. Locations A, B, and C are shown in Fig. 1 . (a) Location A: Severe intergranular corrosion and disintegration of the type 316 stainless steel screen near the leading edge of the fin. (b
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Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001290
EISBN: 978-1-62708-215-0
... of the pilot's seat, front view. (e) Hole in the plastic panel in the passenger cabin. Inside the toilet, the stainless steel washbasin and its fittings were severely mangled. The wastepaper receptacle, made of aluminum alloy sheets and kept under the washbasin, had disintegrated into a number of pieces...
Abstract
Damage to a passenger aircraft that resulted from a midair explosion and subsequent emergency landing was investigated to determine the cause and location of the explosion. Extensive damage had occurred in the front toilet and cockpit areas and to the undercarriage and underside of the aircraft. Fractographic and surface examination of metal fragments (stainless steel and aluminum alloy) from damaged areas indicated that the accident was caused by an explosion in the front toilet. A reconstruction exercise confirmed this conclusion. Damage to the undercarriage and underside resulted from the emergency landing.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001213
EISBN: 978-1-62708-220-4
... by corrosion or dissolved out ( Fig. 11 ), which causes the alloy to lose its cohesion. This type of corrosion is therefore known as grain disintegration or intergranular corrosion, The pronounced localized concentration of the attack on individual regions is noteworthy; it is characteristic in the corrosion...
Abstract
Fragments of screen bars which as structural elements of a condenser had come into contact with cooling water from the mouth of a river were received. The screen bars were made of stainless austenitic Cr-Ni-Mo steel X 5 Cr-Ni-Mo18 10 (Material No. 1.4401). The bars were fractured repeatedly. The ruptures did not occur exclusively or even preferentially at the loops, but just as frequently at locations between them. The mistake made in this case was annealing the steel at a temperature in the critical region. This was probably done to relieve stresses that originated during cold-forming and led to damage by stress corrosion. This would have been the correct method for a ferritic steel, but not austenitic steel, which requires the special heat treatment indicated. When an anneal in the critical region is unavoidable and the indicated additional treatment is impossible or difficult, a type of steel has to be chosen which is resistant to intergranular corrosion.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001473
EISBN: 978-1-62708-229-7
... fracture Introduction The violent disruption of a turbo-alternator is fortunately a rare occurrence, but the accident to be described, which concerns the complete disintegration of the gearbox of a turbo-alternator set, is unique in the Company's experience. The extent of the damage, as is evident...
Abstract
A combination of adverse factors was present in the disruption of a turbo-alternator gearbox. The major cause was the imposition of a gross overload far in excess of that for which the gearbox was designed. The contributory factors were a rim material (EN9 steel) that was inherently notch-sensitive and liable to rupture in a brittle manner. Discontinuities were present in the rims formed by the drain holes drilled in their abutting faces, and possibly enhanced by the stress-raising effect of microcracks in the smeared metal at their surfaces It is probable that the load reached a value in excess of the yield point within the delay time of the material so when the fracture was initiated, it was preceded by several microcracks giving rise to the propagation of a brittle fracture.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001069
EISBN: 978-1-62708-214-3
... Disintegration of stainless steel cladding from TGSCC, resulting in exposure of carbon steel base metal and hemispherical corrosion pits. Fig. 5 Unaffected cladding with minor etching approximately one grain deep. No TGSCC was found. The microstructure consisted of equiaxed austenitic grains...
Abstract
A segment of a stainless steel clad bottom cone of an acid sulfite pulping batch digester failed from severe corrosion loss. The digester was fabricated of 19 mm ( 3 4 in.) low-carbon steel with 3.8 mm (0.15 in.) type 317L stainless steel cladding. The manufacturing method for the cladding was unknown. Visual and metallographic analyses indicated that the failure was from transgranular stress-corrosion cracking (TGSCC), which caused extensive cracking and spalling of the cladding and was localized in a segment of the bottom cone. The remainder of the digester cladding was unaffected. The TGSCC was attributed to high, locked-in residual stresses from the cladding process. It was recommended that the bottom cone replacement segment be stress relieved prior to installation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001236
EISBN: 978-1-62708-218-1
... pace, As the body returns, vacuum bubbles form which implode on the next outward movement of the medium. This produces such a high pressure on a microscopically small area that the material disintegrates and finally particles of material are knocked out of the surface. The conditions for cavitation...
Abstract
A cast iron cylinder liner from a diesel engine suffered localized damage on the cooling water side leading to serration of the edges and heavy pitting. This heavy damage was cavitation damage, frequently observed in diesel motor cylinders. To combat such damage the following measures are recommended in the specialist literature: reduction in piston play; reduction in the amplitude by thicker-walled linings; hard chromizing of the cooling water side; and, addition of a protective oil to the cooling water. The effect of the protective oil is presumably based on a film of oil which forms on the cylinder surface and which is not so easily scoured off during vibration. The effect of the imploding vacuum bubbles is reduced by the oil film which can renew itself from the emulsion.
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