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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c9001582
EISBN: 978-1-62708-233-4
... Abstract This article discusses the failure of cylinder clamping rods in single cylinder diesel engines. The AISI 4140 hardened and tempered steel clamping rods were failing after 200 to 250 h of operation. The fatigue failures initiated at the root of the last thread on the clamping rod...
Abstract
This article discusses the failure of cylinder clamping rods in single cylinder diesel engines. The AISI 4140 hardened and tempered steel clamping rods were failing after 200 to 250 h of operation. The fatigue failures initiated at the root of the last thread on the clamping rod that was engaged in a blind hole in the cylinder block. The failures were caused by loose tolerances on the threads that resulted in a non-uniform distribution of load. The load was concentrated on the last threads to engage, thus causing fatigue crack nucleation at the thread root and propagation until the rod broke by overload. Changing the tolerance on the threads virtually eliminated the fatigue problem.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c9001418
EISBN: 978-1-62708-231-0
... Abstract The crankshaft of a six cylinder, 225-hp diesel engine driving a small locomotive was examined. About nine months after installation a fall in oil pressure was traced to damage to No. 5 crank pin bearing. A small lip present on one side of the discontinuity apparently served to scrape...
Abstract
The crankshaft of a six cylinder, 225-hp diesel engine driving a small locomotive was examined. About nine months after installation a fall in oil pressure was traced to damage to No. 5 crank pin bearing. A small lip present on one side of the discontinuity apparently served to scrape the bearing material. The defect was stoned smooth, a new bearing fitted, and the engine returned to service. The engine performed satisfactorily for a further twelve months until fracture of the crankshaft through the No. 5 crank pin supervened. The fracture revealed a complex torsional fatigue failure. Microscopic examination revealed that the pin had been hard chromium plated and that the plating followed the curved edge of the outer extremity of the defect. This crank pin contained an inherent defect in the form of a slag inclusion or crack situated at the surface. That the crack only showed itself after a period of service suggests that initially it may have been slightly below the surface of the machined pin and some slight extension outwards took place in service.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001417
EISBN: 978-1-62708-227-3
... in the longitudinal direction. Although the longitudinal crack preceded the transverse ones, it would appear that once initiated, the latter developed at a greater rate than the former. Diesel engines Nonmetallic inclusions Pins Steel Fatigue fracture Very few failures in general are attributable...
Abstract
A marine diesel running at 350 rpm had satisfactorily completed 13,000 h before failure of one of the piston pins took place. The pin, 17 in. long, with a central bore of 3 in. diam, failed transversely approximately 3 in. from one end. The characteristic conchoidal markings indicative of fatigue failure were present with origins at about the mid-thickness of the pin located each side of the step in the fracture surface. In addition, cracking was evident in the axial direction. The crack ran into one of the radial oil holes near the end of the pin. A further section was taken transverse to the crack surface and subsequent examination confirmed the presence of a slag inclusion on the edge of the crack. The inclusion ran the full length of the component. The stress raising effect of the inclusion in combination with the residual and service stresses served to initiate the cracking in the longitudinal direction. Although the longitudinal crack preceded the transverse ones, it would appear that once initiated, the latter developed at a greater rate than the former.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001612
EISBN: 978-1-62708-218-1
... Abstract The fan used to cool a diesel engine fractured catastrophically after approximately 100 h of operation. The fan failed at a spider, which was resistance spot welded to a shim placed between two circular spiders of 3 mm thickness. The detailed analysis of the fracture indicated...
Abstract
The fan used to cool a diesel engine fractured catastrophically after approximately 100 h of operation. The fan failed at a spider, which was resistance spot welded to a shim placed between two circular spiders of 3 mm thickness. The detailed analysis of the fracture indicated that the premature failure of the fan was due to inadequate bonding between the sheets at the weld nugget. The fracture was initiated from the nugget-plate interface. The inadequate penetration and lack of fusion between the steel sheets during resistance spot welding led to poor weld strength and the fracture during operation. The propensity to crack initiation and failure was accentuated by improper cleaning of the surfaces prior to welding and to inadequate nugget-to-sheet edge distance.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001486
EISBN: 978-1-62708-234-1
... Abstract Cavitation damage of diesel engine cylinder liners is due to vibration of the cylinder wall, initiated by slap of the piston under the combined forces of inertia and firing pressure as it passes top dead center. The occurrence on the anti-thrust side may possibly result from bouncing...
Abstract
Cavitation damage of diesel engine cylinder liners is due to vibration of the cylinder wall, initiated by slap of the piston under the combined forces of inertia and firing pressure as it passes top dead center. The occurrence on the anti-thrust side may possibly result from bouncing of the piston. The exact mechanism of cavitation damage is not entirely clear. Two schools of thought have developed, one supporting an essentially erosive, and the other an essentially corrosive, mechanism. Measures to prevent, or reduce, cavitation damage should be considered firstly from the aspect of design, attention being given to methods of reducing the amplitude of the liner vibration. Attempts have been made to reduce the severity of attack by attention to the environment. Inhibitors, such as chromates, benzoate/nitrite mixtures, and emulsified oils, have been tried with varying success. Attempts have been made to reduce or prevent cavitation damage by the application of cathodic protection, and this has been found to be effective in certain instances of trouble on propellers.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001377
EISBN: 978-1-62708-215-0
... Intergranular fracture Stress-corrosion cracking Background When the International Harvester Company was in existence, sudden unexplained bearing cap bolt fractures were experienced in a line of diesel engines manufactured at one of its overseas facilities. Examination of engines at various plants...
Abstract
Sudden and unexplained bearing cap bolt fractures were experienced with reduced-shank design bolts fabricated from 42 CrMo 4 steel, quenched and tempered to a nominal hardness of 38 to 40 HRC. Fractographic analysis provided evidence favoring stress-corrosion cracking as the operating transgranular fracture failure mechanism. Water containing H7S was subsequently identified as the aggressive environment that precipitated the fractures in the presence of high tensile stress. This environment was generated by the chemical breakdown of the engine oil additive and moisture ingress into the normally sealed bearing cap chamber surrounding the bolt shank. A complete absence of fractures in bolts from one of the two vendors was attributed primarily to surface residual compressive stresses produced on the bolt shank by a finish machining operation after heat treatment. Shot cleaning, with fine cast shot, produced a surface residual compressive stress, which eliminated stress-corrosion fractures under severe laboratory conditions.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0047121
EISBN: 978-1-62708-218-1
... of high stress. No recommendations were made. Crankshafts Diesel engines Forgings Inclusions 1050 UNS G10500 Fatigue fracture A 1050 steel crankshaft with 6.4-cm (2.5-in.) diam journals that measured 87 cm (34.25 in.) in length and weighed 31 kg (69 lb) fractured in service. The shaft had...
Abstract
A 1050 steel crankshaft with 6.4 cm (2.5 in.) diam journals that measured 87 cm (34.25 in.) in length and weighed 31 kg (69 lb) fractured in service. The shaft had been quenched and tempered to a hardness of 19 to 26 HRC, then selectively hardened on the journals to a surface hardness of 40 to 46 HRC. Visual inspection and 100x micrographs showed the fracture surface as having a complex type of fatigue failure initiated from subsurface inclusions in the transition zone between the induction-hardened surface and the softer core. The fractured shaft was examined for chemical composition and hardness, both of which were found to be within prescribed limits. This evidence supports the conclusions that the failure was caused by fatigue cracks that initiated in an area having an excessive amount of inclusions. The inclusions were located in a transition zone, which is a region of high stress. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001621
EISBN: 978-1-62708-227-3
... Abstract A crankshaft flange from a marine diesel engine illustrated a less-common case of fretting-fatigue cracking. The crankshaft was from a main engine of a sea-going passenger/vehicle ferry. The afterface of the flange was bolted to the flange of a shaft driving the gearbox. Cracks...
Abstract
A crankshaft flange from a marine diesel engine illustrated a less-common case of fretting-fatigue cracking. The crankshaft was from a main engine of a sea-going passenger/vehicle ferry. The afterface of the flange was bolted to the flange of a shaft driving the gearbox. Cracks observed were sharp, transgranular, and not associated with any decarburization or other microstructural anomalies in the steel. Cracking of this main engine crankshaft flange was very likely a consequence of fatigue cracking initiated at fretting damage. The cause of the fretting was from loosening of the bolts.
Image
Published: 01 January 2002
Image
Published: 01 January 2002
Fig. 21 Diesel-engine crankshaft that broke because of misalignment. (a) Fatigue marks on the fracture surface. (b) Micrograph of a section through the fracture origin showing a small crack (arrow) and some inclusions. Etched with nital. 500×
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Image
Published: 01 January 2002
Fig. 4 Failure of a connecting rod bolt in a diesel engine. In (a), the failed bolt is the upper one, having necked down in a nominally larger cross-sectional area. The lower bolt is another removed from the engine in unstretched condition. In (b), the stretched region of the bolt is shown
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Image
Published: 01 January 2002
Image
in Anomalous Fractures of Diesel Engine Bearing Cap Bolts[1]
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1993
Fig. 1 Broken bolt removed from diesel engine. Absence of plastic deformation close to the fracture indicates a low ductility failure. 2×
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Image
Published: 15 January 2021
Image
Published: 15 January 2021
Fig. 4 Failure of a connecting rod bolt in a diesel engine. In (a), the failed bolt is the upper one, having necked down in a nominally larger cross-sectional area. The lower bolt is another removed from the engine in unstretched condition. In (b), the stretched region of the bolt is shown
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0089651
EISBN: 978-1-62708-235-8
... Abstract Several diesel-engine rocker levers (malleable iron similar to ASTM A 602, grade M7002) failed at low hours in overspeed, over-fuel, highly loaded developmental engine tests. Identical rocker levers had performed acceptably in normal engine tests. The rocker levers were failing through...
Abstract
Several diesel-engine rocker levers (malleable iron similar to ASTM A 602, grade M7002) failed at low hours in overspeed, over-fuel, highly loaded developmental engine tests. Identical rocker levers had performed acceptably in normal engine tests. The rocker levers were failing through the radius of an adjusting screw arm. The typical fracture face exhibited two distinct modes of crack propagation: the upper portion indicated overload at final fracture, whereas the majority of the fracture suggested a fatigue fracture. Investigation (visual inspection, 1.5x/30x/60x magnification, and nital etched 300x magnification) supported the conclusion that the rocker levers failed in fatigue, with casting defects, or spiking, acting as stress raisers to initiate failures in highly loaded engine tests. Recommendations included shot peening of the levers as an interim measure to reduce the possibility of failure and redesign to increase the cross-sectional area of the levers.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c0047328
EISBN: 978-1-62708-231-0
... Abstract Cracks formed on cylinder inserts from a water-cooled locomotive diesel engine, on the water side in the neck between the cylindrical part and the collar. Cracks were revealed by magnetic-particle inspection. As a rule, several parallel cracks had appeared, some of which were very fine...
Abstract
Cracks formed on cylinder inserts from a water-cooled locomotive diesel engine, on the water side in the neck between the cylindrical part and the collar. Cracks were revealed by magnetic-particle inspection. As a rule, several parallel cracks had appeared, some of which were very fine. The part played by corrosion in the formation of the cracks was demonstrated with the help of metallographic techniques. The surface regions of the cracks widened into funnel form, which is a result of the corrosive influence of the cooling water. Actual corrosion pits could not be found indicating that the vibrational stresses had a greater share in the damage than the corrosive influence. Cracks appeared initially only in those engines in which no corrosion inhibitor had been added to the cooling water. The cracking was caused by corrosion fatigue. The combined presence of a corrosive medium and cyclical operating stress was needed to cause cracks. No cracks appeared when corrosion inhibitor was added to the cooling water.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001236
EISBN: 978-1-62708-218-1
... Abstract A cast iron cylinder liner from a diesel engine suffered localized damage on the cooling water side leading to serration of the edges and heavy pitting. This heavy damage was cavitation damage, frequently observed in diesel motor cylinders. To combat such damage the following measures...
Abstract
A cast iron cylinder liner from a diesel engine suffered localized damage on the cooling water side leading to serration of the edges and heavy pitting. This heavy damage was cavitation damage, frequently observed in diesel motor cylinders. To combat such damage the following measures are recommended in the specialist literature: reduction in piston play; reduction in the amplitude by thicker-walled linings; hard chromizing of the cooling water side; and, addition of a protective oil to the cooling water. The effect of the protective oil is presumably based on a film of oil which forms on the cylinder surface and which is not so easily scoured off during vibration. The effect of the imploding vacuum bubbles is reduced by the oil film which can renew itself from the emulsion.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001488
EISBN: 978-1-62708-236-5
... Abstract While an attempt was being made to start the diesel engine of a dragline type excavator, a severe explosion took place, the operator unfortunately being killed. The engine was normally started by compressed air from an air bottle or receiver charged to a pressure of 350 psi by a small...
Abstract
While an attempt was being made to start the diesel engine of a dragline type excavator, a severe explosion took place, the operator unfortunately being killed. The engine was normally started by compressed air from an air bottle or receiver charged to a pressure of 350 psi by a small auxiliary engine driven compressor fitted on the excavators. On an occasion when this had broken down, the air bottle was replenished by the engineer-in-charge from a cylinder of compressed air. The compressor engine remained unserviced and when the starting bottle again became depleted, the excavator operator re-charged it himself from another cylinder without the knowledge of the engineer. The engine was started satisfactorily, and the bottle charged again to 350 psi in readiness for the start on the following day. It was while an attempt was being made to start the engine on this occasion that the explosion took place. The cylinder used by the operator for re-charging the receiver contained not air but oxygen.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001761
EISBN: 978-1-62708-241-9
... Abstract An investigation of a damaged crankshaft from a horizontal, six-cylinder, in-line diesel engine of a public bus was conducted after several failure cases were reported by the bus company. All crankshafts were made from forged and nitrided steel. Each crankshaft was sent for grinding...
Abstract
An investigation of a damaged crankshaft from a horizontal, six-cylinder, in-line diesel engine of a public bus was conducted after several failure cases were reported by the bus company. All crankshafts were made from forged and nitrided steel. Each crankshaft was sent for grinding, after a life of approximately 300,000 km of service, as requested by the engine manufacturer. After grinding and assembling in the engine, some crankshafts lasted barely 15,000 km before serious fractures took place. Few other crankshafts demonstrated higher lives. Several vital components were damaged as a result of crankshaft failures. It was then decided to send the crankshafts for laboratory investigation to determine the cause of failure. The depth of the nitrided layer near fracture locations in the crankshaft, particularly at the fillet region where cracks were initiated, was determined by scanning electron microscope (SEM) equipped with electron-dispersive X-ray analysis (EDAX). Microhardness gradient through the nitrided layer close to fracture, surface hardness, and macrohardness at the journals were all measured. Fractographic analysis indicated that fatigue was the dominant mechanism of failure of the crankshaft. The partial absence of the nitrided layer in the fillet region, due to over-grinding, caused a decrease in the fatigue strength which, in turn, led to crack initiation and propagation, and eventually premature fracture. Signs of crankshaft misalignment during installation were also suspected as a possible cause of failure. In order to prevent fillet fatigue failure, final grinding should be done carefully and the grinding amount must be controlled to avoid substantial removal of the nitrided layer. Crankshaft alignment during assembly and proper bearing selection should be done carefully.
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