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Cr-Mo steel
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Published: 01 January 2002
Fig. 79 Globular carbides at the surface of a carburized 1% Cr-Mo steel (reheat quenched). 836×. Source: Ref 30
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Published: 01 January 2002
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in High-Temperature Stress Relaxation Cracking and Stress Rupture Observed in a Coke Gasifier Failure
> Handbook of Case Histories in Failure Analysis
Published: 01 December 2019
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Published: 01 January 2002
Fig. 50 ASTM A 356, grade 6 (1.25%Cr-0.5%Mo), cast steel turbine casing that failed by cracking. (a) Segment removed from the casing, showing the fracture surface at right. A large porosity defect can be seen at the upper right corner, near the broken-open tapped hole. (b) to (e) Transmission
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Published: 01 January 2002
Fig. 39 Distortion of JIS SCM 440 (0.4% C, 1.05% Cr, 0.22% Mo) steel pinion shafts after oil quenching from 850 °C (1560 °F) while vertically suspended and tempering at 600 °C (1110 °F)
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Published: 30 August 2021
Fig. 29 ASTM International A 356, grade 6 (1.25%Cr-0.5%Mo) cast steel turbine casing that failed by cracking. (a) Segment removed from the casing, showing the fracture surface at right. A large porosity defect can be seen at the upper-right corner, near the broken-open tapped hole. (b) to (e
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in Failure of a Thick-Wall Casing for a Steam Turbine by Cracking
> ASM Failure Analysis Case Histories: Power Generating Equipment
Published: 01 June 2019
Fig. 1 ASTM A 356, grade 6 (1.25%Cr-0.5%Mo), cast steel turbine casing that failed by cracking. (a) Segment removed from the casing, showing the fracture surface at right. A large porosity defect can be seen at the upper right corner, near the broken-open tapped hole. (b) to (e) Transmission
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001254
EISBN: 978-1-62708-225-9
... Abstract The specified elongation of 10% could not be achieved in several hollow pinion gear shafts made of cast Cr-Mo steel GS 35 Cr-Mo 5 3 that were heat treated to a strength of 90 kp/sq mm. The steel was melted in a basic 3 ton arc furnace and deoxidized in the furnace and in the pan...
Abstract
The specified elongation of 10% could not be achieved in several hollow pinion gear shafts made of cast Cr-Mo steel GS 35 Cr-Mo 5 3 that were heat treated to a strength of 90 kp/sq mm. The steel was melted in a basic 3 ton arc furnace and deoxidized in the furnace and in the pan with a total of 7 kg aluminum. Fracture of a tensile specimen occurred with low elongation and, apparently, also with low reduction of area. In some places it was coarse grained conchoidal. It was found that the exceptionally low elongation of the cast specimens was due to excessive deoxidation by aluminum.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0048835
EISBN: 978-1-62708-220-4
... by metallurgical examination of a cross section of a longitudinal crack. It was concluded that the damage was caused by a form of hydrogen attack. Installation of a used Cr-Mo steel vessel with a type 347 stainless steel weld overlay was suggested as a corrective action. Decarbuization Desulfurizer reactors...
Abstract
Welds in two CMo steel catalytic gas-oil desulfurizer reactors cracked under hydrogen pressure-temperature conditions that would not have been predicted by the June 1977 revision of the Nelson Curve for that material. Evidence of severe cracking was found in five weld-joint areas during examination of a naphtha desulfurizer by ultrasonic shear wave techniques. Defect indications were found in longitudinal and circumferential seam welds of the ASTM A204, grade A, steel sheet. The vessel was found to have a type 405 stainless steel liner for corrosion protection that was spot welded to the base metal and all vessel welds were found to be overlaid with type 309 stainless steel. Long longitudinal cracks in the weld metal, as well as transverse cracks were exposed after the weld overlay was ground off. A decarburized region on either side of the crack was revealed by metallurgical examination of a cross section of a longitudinal crack. It was concluded that the damage was caused by a form of hydrogen attack. Installation of a used Cr-Mo steel vessel with a type 347 stainless steel weld overlay was suggested as a corrective action.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001204
EISBN: 978-1-62708-219-8
... made from Cr-Mo steel (Material No. 1.7225) according to DIN 17200. It was found that the bolts were not made from a suitable alloy steel, but were welded together from two unsuitable steels, one of which lacked sufficient strength. The austenitic weld seams showed hot tears and were not welded through...
Abstract
Two bolts from the stressed structure of a church building that had broken during stressing were examined to establish the cause of fracture. The fracture of one of the first bolt occurred in a double-vee groove weld whose root was not completely welded. The second bolt had cracked outside of the weld seam closely under the head. Neither one had been particularly deformed before fracture. The composition of the head pieces corresponded approximately to manganese steel (Material No. 1 0845), a weldable construction steel with increased yield point and strength, while the shafts were made from Cr-Mo steel (Material No. 1.7225) according to DIN 17200. It was found that the bolts were not made from a suitable alloy steel, but were welded together from two unsuitable steels, one of which lacked sufficient strength. The austenitic weld seams showed hot tears and were not welded through to the root. Also, the pieces were not preheated before welding, so that stress cracks occurred in the transition zones. The second bolt was overstressed during the impact caused by the breaking of the first bolt.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001179
EISBN: 978-1-62708-228-0
... at 530 deg C. The connectors were made of SAE 4140 Cr-Mo steel. The material for the rod pipes was Fe-0.4C-1Mn steel. Structural stresses played a role in the cracking. Iron sulfide formed on the fracture planes and flake-like stress cracks occurred in the steel. The hydrogen sulfide content of the gas...
Abstract
During natural gas drilling in the EMS region in 1956, considerable numbers of longitudinal cracks and transverse fractures occurred in the connecting pieces of the bore rods. The connectors were screwed onto the rods by means of a fine thread and tightly joined with it by shrinkage at 530 deg C. The connectors were made of SAE 4140 Cr-Mo steel. The material for the rod pipes was Fe-0.4C-1Mn steel. Structural stresses played a role in the cracking. Iron sulfide formed on the fracture planes and flake-like stress cracks occurred in the steel. The hydrogen sulfide content of the gas was the cause of damage. Hydrogen liberated by reaction with the iron caused the formation of iron sulfide after penetration of the steel, which had an explosive effect during molecular separation under high pressure. This in turn caused the crack formation in conjunction with the external and residual stresses.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0006417
EISBN: 978-1-62708-234-1
... Abstract A cadmium-plated 4340 Ni-Cr-Mo steel ballast elbow assembly was submitted for failure analysis to determine the element or radical present in an oxidation product found inside the elbow assembly. Energy-dispersive x-ray analysis in the SEM showed that iron was the predominant species...
Abstract
A cadmium-plated 4340 Ni-Cr-Mo steel ballast elbow assembly was submitted for failure analysis to determine the element or radical present in an oxidation product found inside the elbow assembly. Energy-dispersive x-ray analysis in the SEM showed that iron was the predominant species, presumably in an oxide form. The inside surface had the appearance of typical corrosion products. Hardness measurements indicated that the 4340 steel was heat treated to a strength of approximately 862 MPa (125 ksi). It was concluded that the oxide detected on the ballast elbow was iron oxide. The possibility that the corrosion products would eventually create a blockage of the affected hole was great considering the small hole diameter (4.2 mm, or 0.165 in.). It was recommended that a quick fix to stop the corrosion would be to apply a corrosion inhibitor inside the hole. This, however, would cause the possibility of inhibitor buildup and the eventual clogging of the hole. A change in the manufacturing process to include a cadmium plating on the hole inside surface was recommended. This was to be accomplished in accordance with MIL specification QQ-P-416, Type II, Class 1. A material change to 300-series stainless steel was also recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001145
EISBN: 978-1-62708-217-4
... chamber assembly). Premature failures of steel breech chambers have been prevalent enough to cause serious concern. The breech chamber is fabricated from a 4340 Ni-Cr-Mo steel forging heat treated to a hardness in the range HRC 40 to 45. The failures have taken several forms, including fracture...
Abstract
Cartridge-pneumatic starter systems are used on military aircraft. In the cartridge mode used for alert starts, the starter turbine is driven by hot gases produced through the controlled burning of a solid propellant cartridge within a closed chamber (the breech chamber/cartridge chamber assembly). Premature failures of steel breech chambers have been prevalent enough to cause serious concern. The breech chamber is fabricated from a 4340 Ni-Cr-Mo steel forging heat treated to a hardness in the range HRC 40 to 45. The failures have taken several forms, including fracture and unzipping of the chamber dome, burn-through of the dome, and shearing of bayonet locking lugs. Factors identified as significant in the failures are the pressure developed in the chamber and internal corrosion of the chamber in an environment that can produce stress-corrosion cracking. The interior configuration of the chamber and the stress distribution also have a bearing upon the failure modes. Several failures are reviewed to illustrate the problems.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001820
EISBN: 978-1-62708-241-9
... cracking. Based on test data and cost, A217-WC9 cast Cr–Mo steel would be a better alloy for the application. valve body corrosion H2S exposure Cr-Mo steel pitting cracks chemical analysis corrosion resistance A216-WCC (cast carbon steel) UNS J02503 A217-WC9 cast Cr–Mo steel UNS K21590...
Abstract
A group of control valves that regulate production in a field of sour gas wellheads performed satisfactorily for three years before pits and cracks were detected during an inspection. One of the valves was examined using chemical and microstructural analysis to determine the cause of failure and provide preventive measures. The valve body was made of A216-WCC cast carbon steel. Its inner surface was covered with cracks stemming from surface pits. Investigators concluded that the failure was caused by a combination of hydrogen-induced corrosion cracking and sulfide stress-corrosion cracking. Based on test data and cost, A217-WC9 cast Cr–Mo steel would be a better alloy for the application.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001420
EISBN: 978-1-62708-220-4
... Abstract A hydroextractor installed new for the drying of sugar massecuite consisted of a metal basket fixed to a vertical spindle. Disruption occurred just after the machine had been run up to speed and was not preceded by any abnormal behavior. The basket assembly consisted of a Ni-Cr-Mo...
Abstract
A hydroextractor installed new for the drying of sugar massecuite consisted of a metal basket fixed to a vertical spindle. Disruption occurred just after the machine had been run up to speed and was not preceded by any abnormal behavior. The basket assembly consisted of a Ni-Cr-Mo steel shell and two end plates. It was designed to spin at 2200 rpm, using centrifugal force to expel liquids through nearly 3000 drilled holes in the shell wall. Investigators found that the shell separated completely from the bottom plate. The top plate, though it cracked radially, remained attached over most of its circumference. The basket also contained a 22-gauge Monel metal liner that had been perforated by stabbing, raising pronounced burrs that faced each hole. Apart from the local spots of corrosion due to the lining, the inner surface of the basket showed little evidence of general corrosion. What caused the basket to fail was the presence of corrosion-fatigue cracks or fissures radiating from the holes. A secondary cause was that the scantlings of the basket were too light.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001470
EISBN: 978-1-62708-220-4
... of the fractured surfaces showed that failure had been preceded by fatigue cracking. The material from which the dish plate was forged was a Ni-Cr-Mo steel in the oil hardened and tempered condition. Fractographic examination of the surface of the cracks showed striation markings indicative of the progress...
Abstract
One 49-in. impeller of a two-stage centrifugal air compressor disrupted without warning, causing extensive damage to the casings, the second impeller, and the driving gear box. Prior to the mishap, the machine had run normally, with no indications of abnormal vibration, temperature, or pressure. Initial failure had taken place in the floating dished inlet plate (eye plate) of the first-stage impeller. Failure occurred predominantly by tearing along the lines of rivet holes for the longer blades, these extended for practically the full radial width of the dished plate. Examination of the fractured surfaces showed that failure had been preceded by fatigue cracking. The material from which the dish plate was forged was a Ni-Cr-Mo steel in the oil hardened and tempered condition. Fractographic examination of the surface of the cracks showed striation markings indicative of the progress of fatigue cracks. Failure of the one impeller and the cracking of the others were attributed to “low-cycle high-strain fatigue” due to fluctuating circumferential (hoop) stresses.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001300
EISBN: 978-1-62708-215-0
... Abstract A bull gear from a coal pulverizer at a utility failed by rolling-contact fatigue as the result of continual overloading of the gear and a nonuniform, case-hardened surface of the gear teeth. The gear consisted of an AISI 4140 Cr-Mo steel gear ring that was shrunk fit and pinned onto...
Abstract
A bull gear from a coal pulverizer at a utility failed by rolling-contact fatigue as the result of continual overloading of the gear and a nonuniform, case-hardened surface of the gear teeth. The gear consisted of an AISI 4140 Cr-Mo steel gear ring that was shrunk fit and pinned onto a cast iron hub. The wear and pitting pattern in the addendum area of the gear teeth indicated that either the gear or pinion was out of alignment. Beach marks observed on the fractured surface of the gear indicated that fatigue was the cause of the gear failure. Similar gears should be inspected carefully for signs of cracking or misalignment. Ultrasonic testing is recommended for detection of subsurface cracks, while magnetic particle testing will detect surface cracking. Visual inspection can be used to determine the teeth contact pattern.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001005
EISBN: 978-1-62708-215-0
... Abstract Several heavy truck Cr-Mo steel steering arms in service less than three years fractured during stationary or low-speed turning maneuvers that required power-assisted steering. Metallographic examination of the cracked AISI 4135 arms, heat treated to a hardness of 285 to 341 HB...
Abstract
Several heavy truck Cr-Mo steel steering arms in service less than three years fractured during stationary or low-speed turning maneuvers that required power-assisted steering. Metallographic examination of the cracked AISI 4135 arms, heat treated to a hardness of 285 to 341 HB, revealed that fatigue crack initiation occurred from the tip of oxide scale inclusions forged into the U-shaped arm at the inside radius. Corrective action involved redesigning the steering arm to increase the minimum forging radius and reduce the stress level at the inner-bend radius, and reducing the level of power assistance to the wheels to encourage the driver to put the vehicle in motion prior to turning.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001556
EISBN: 978-1-62708-218-1
... Abstract A few Cr-Mo steel piston rods from different production batches were found identically cracked in the eye end near the radius after chrome plating and baking treatment. Two of them cracked in the plating stage itself instantly broke on slight tapping. Cracking initiated from the outer...
Abstract
A few Cr-Mo steel piston rods from different production batches were found identically cracked in the eye end near the radius after chrome plating and baking treatment. Two of them cracked in the plating stage itself instantly broke on slight tapping. Cracking initiated from the outer base surface of the forked eye end. The 40 mm diam forged piston rods were subjected to plating after heavy machining on the part without any stress-relieving treatment. Also, time lapses between plating and baking were varied from 3 to 11 h. The brittle cracking along forked eye-end radius portion was attributed to hydrogen embrittlement that occurred during chrome plating.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c0046242
EISBN: 978-1-62708-236-5
... Abstract An integral coupling and gear (Cr-Mo steel), used on a turbine-driven main boiler-feed pump, was removed from service after one year of operation because of excessive vibration. Spectrographic analysis and metallographic examination revealed the fact that gritty material in the gear...
Abstract
An integral coupling and gear (Cr-Mo steel), used on a turbine-driven main boiler-feed pump, was removed from service after one year of operation because of excessive vibration. Spectrographic analysis and metallographic examination revealed the fact that gritty material in the gear teeth (found at visual inspection) was composed of the same material as the metal in the coupling. Beach marks and evidence of cold work, typical of fatigue failure, were found on the fracture surface. Chips remaining in the analysis cut were difficult to remove, indicating a strong magnetic field in the part. Evidence found supports the conclusions that failure of the coupling was by fatigue and that incomplete demagnetization of the coupling following magnetic-particle inspection caused retention of metal chips in the roots of the teeth. Improper lubrication caused gear teeth to overheat and spall, producing chips that eventually overstressed the gear, causing failure. Because the oil circulation system was not operating properly, metal chips were not removed from the coupling. Recommendations included checking the replacement coupling for residual magnetism and changing or filtering the pump oil to remove any debris.
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