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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0046469
EISBN: 978-1-62708-229-7
... Abstract After about 17 years in service, copper alloy C27000 (yellow brass, 65% Cu) innercooler tubes in an air compressor began leaking cooling water, causing failure and requiring replacement. The tubes were 19 mm in diam and had a wall thickness of 1.3 mm (0.050 in.). The cooling water...
Abstract
After about 17 years in service, copper alloy C27000 (yellow brass, 65% Cu) innercooler tubes in an air compressor began leaking cooling water, causing failure and requiring replacement. The tubes were 19 mm in diam and had a wall thickness of 1.3 mm (0.050 in.). The cooling water that flowed through the tubes was generally sanitary (chlorinated) well water; however, treated recirculating water was sometimes used. Analysis (visual inspection, 9x and 75x unetched micrographs, and spectrochemical analysis) showed a thick uniform layer of porous, brittle copper on the inner surface of the tube, extending to a depth of about 0.25 mm (0.010 in.) into the metal, plug-type dezincification extending somewhat deeper into the metal. This supported the conclusion that failure of the tubes was the result of the use of an uninhibited brass that has a high zinc content and therefore is readily susceptible to dezincification. Recommendations included replacing the material with copper alloy C68700 (arsenical aluminum brass), which contains 0.02 to 0.06% As and is highly resistant to dezincification. Copper alloy C44300 (inhibited admiralty metal) could be an alternative selection for this application; however, this alloy is not as resistant to impingement attack as copper alloy C68700.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001470
EISBN: 978-1-62708-220-4
... Abstract One 49-in. impeller of a two-stage centrifugal air compressor disrupted without warning, causing extensive damage to the casings, the second impeller, and the driving gear box. Prior to the mishap, the machine had run normally, with no indications of abnormal vibration, temperature...
Abstract
One 49-in. impeller of a two-stage centrifugal air compressor disrupted without warning, causing extensive damage to the casings, the second impeller, and the driving gear box. Prior to the mishap, the machine had run normally, with no indications of abnormal vibration, temperature, or pressure. Initial failure had taken place in the floating dished inlet plate (eye plate) of the first-stage impeller. Failure occurred predominantly by tearing along the lines of rivet holes for the longer blades, these extended for practically the full radial width of the dished plate. Examination of the fractured surfaces showed that failure had been preceded by fatigue cracking. The material from which the dish plate was forged was a Ni-Cr-Mo steel in the oil hardened and tempered condition. Fractographic examination of the surface of the cracks showed striation markings indicative of the progress of fatigue cracks. Failure of the one impeller and the cracking of the others were attributed to “low-cycle high-strain fatigue” due to fluctuating circumferential (hoop) stresses.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001408
EISBN: 978-1-62708-220-4
... Abstract Initially, two vertical double-acting two-stage compressors delivering chlorine gas at a pressure of 100 psi appeared to be running satisfactorily. About six months later the LP piston-rod of the No. 2 compressor failed due to burning, the compressor being worked double-acting...
Abstract
Initially, two vertical double-acting two-stage compressors delivering chlorine gas at a pressure of 100 psi appeared to be running satisfactorily. About six months later the LP piston-rod of the No. 2 compressor failed due to burning, the compressor being worked double-acting at the time. About five months later, the HP piston rod of the No. 1 compressor failed in a similar manner. Specimens for microscopic examination were cut from the rod in the region of the failure and from the extreme end that had been situated above the piston and hence not subjected to an appreciable rise in temperature. The material was a steel in the normalized condition with a 0.35% C content. It appears probable that deficient lubrication of the gland resulted in overheating of the rod due to friction. The presence of a sprayed-metal coating was probably an additional factor in promoting failure, as it would present to the gas a surface area considerably greater than that of a homogeneous material.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001476
EISBN: 978-1-62708-229-7
... and washers at each end. This assembly became loose, thereby allowing air under pressure to enter the waterside of the cooler and expel the water, leading to overheating and ultimately to the damage described. Air compressors Combustion Heat exchanger tubes Overheating Brass Intergranular fracture...
Abstract
An aftercooler was of conventional design and fitted with brass tubes through which cooling-water circulated. Air at 100 psi pressure was passed over the outsides of the tubes, entering the vessel near to the upper tubeplate on one side and leaving it by a branch adjacent to the lower tubeplate on the opposite side. After a mishap, the paint had been burned off the upper half of the shell. Internally, most of the tubes were found to be twisted or bent. The casing of the pump used to circulate the cooling water was also found to be cracked after the mishap. All the evidence pointed to the probability that a fire had occurred within the vessel. Some months before the failure, one of the tubes situated towards the center of the nest developed a leak. Owing to the difficulty of inserting a replacement tube, the defective one was scaled by means of a length of screwed rod fitted with nuts and washers at each end. This assembly became loose, thereby allowing air under pressure to enter the waterside of the cooler and expel the water, leading to overheating and ultimately to the damage described.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001757
EISBN: 978-1-62708-241-9
... Abstract Rotor blades in the compressor section of a J79 engine had failed. Optical, stereoscopic, microhardness testing, and SEM examinations were conducted to determine the cause. The blades were made of STS403 and were used uncoated. They were damaged over an extensive area, from the 15th...
Abstract
Rotor blades in the compressor section of a J79 engine had failed. Optical, stereoscopic, microhardness testing, and SEM examinations were conducted to determine the cause. The blades were made of STS403 and were used uncoated. They were damaged over an extensive area, from the 15th through the 17th compressor stages, as were stator vanes and casing sections. The fractured surface of the 17th blade showed multiple origins along with secondary cracking and extensive propagation that preceded separation. The metallographic analysis of the microstructure suggested work hardening. Based on the results, the cause of the fractured blade was high-amplitude fatigue due to severe stall. After normal engine usage of five months, the blade fractured sending fragments throughout the combustion and turbine sections.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001399
EISBN: 978-1-62708-220-4
... Abstract An air compressor was installed at a chemical plant in which nitric acid was produced by burning ammonia with air. It was a 5000 hp, 5-stage centrifugal machine running at 6000 rpm, compressing air to 5 atm. Failure of the first stage impeller occurred due to a segment from the back...
Abstract
An air compressor was installed at a chemical plant in which nitric acid was produced by burning ammonia with air. It was a 5000 hp, 5-stage centrifugal machine running at 6000 rpm, compressing air to 5 atm. Failure of the first stage impeller occurred due to a segment from the back plate becoming detached. On the remaining portion, cracks were visible running between the holes for rivets by which the vanes were attached. Metallographic examination of selected sections from the backplate revealed the material to be in the hardened and tempered condition, and the cracking to have initiated on the internal surface of the plate at the crevice between the plate and the vane. It was evident that the impeller failed by stress-corrosion cracking, which initiated in the crevice between the vanes and back plate and propagated through the plate along the line of the rivets where working stresses would be greatest. The compressor intake was situated in the vicinity of nitric acid pumps which had a history of leakage troubles, and which had evidently given rise to the nitrates found on the impeller.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c0091897
EISBN: 978-1-62708-236-5
... Abstract The shaft-and-bearing assembly in a freon compressor was subjected to severe pounding and vibration after six years of service. After about one year of service, the compressor had been shut down to replace a bearing seal. One month before the shaft failed, a second seal failure...
Abstract
The shaft-and-bearing assembly in a freon compressor was subjected to severe pounding and vibration after six years of service. After about one year of service, the compressor had been shut down to replace a bearing seal. One month before the shaft failed, a second seal failure occurred, requiring the collar, spacer sleeve, seal, roller bearing, and lock washer to be replaced. The shaft was made of 4140 steel, heat treated to a hardness of 20 to 26 HRC. The seal, bearing, and lock washer were commercial components. Investigation (visual inspection, 4.5x images, x-ray diffraction, hardness testing, and microscopic exam) supported the conclusion that shaft failure was initiated by fretting between the bearing race and the bearing surface on the shaft because of improper bearing installation. Once clearance was established between the bearing and the shaft, the shaft began pounding on the inner bearing race, causing final failure of the shaft surface. Recommendations included proper fitting of the shaft and bearing race to preventing movement of the bearing on the shaft. Also, the lock washer and locknut must be installed properly.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001359
EISBN: 978-1-62708-215-0
... Abstract The cause of low fatigue life measurements obtained during routine fatigue testing of IMI 550 titanium alloy compressor blades used in the first stage of the high-pressure compressor of an aeroengine was investigated. The origin of the fatigue cracks was associated with a spherical...
Abstract
The cause of low fatigue life measurements obtained during routine fatigue testing of IMI 550 titanium alloy compressor blades used in the first stage of the high-pressure compressor of an aeroengine was investigated. The origin of the fatigue cracks was associated with a spherical bead of metal sticking to the blade surface in each case. Scanning electron microscope revealed that the cracks initiated at the point of contact of the bead with the blade surface. Energy-dispersive X-ray analysis indicated that the bead composition was the same as that of the blade. Detailed investigation revealed that fused material from the blade had been thrown onto the cold blade surface during a grinding operation to remove the targeting bosses from the forgings, thereby causing local embrittlement. It was recommended that extreme care be taken during grinding operations to prevent the hot, fused particles from striking the blade surface.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001081
EISBN: 978-1-62708-214-3
... Abstract Several compressor disks in military fighter and trainer aircraft gas turbine engines cracked prematurely in the bolt hole regions. The disks were made of precipitation-hardened AM355 martensitic stainless steel. Experimental and analytical work was performed on specimens from...
Abstract
Several compressor disks in military fighter and trainer aircraft gas turbine engines cracked prematurely in the bolt hole regions. The disks were made of precipitation-hardened AM355 martensitic stainless steel. Experimental and analytical work was performed on specimens from the fifth-stage compressor disk (judged to be the most crack-prone disk in the compressor) to determine the cause of the failures. Failure was attributed to high-strain low-cycle fatigue during service. It was also determined that the cyclic engine usage assumed in the original life calculations had been under estimated, which led to low-cycle fatigue cracking earlier than expected. Fracture mechanics analysis of the disks was carried out to assess their damage tolerance and to predict safe inspection intervals.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001427
EISBN: 978-1-62708-236-5
... Abstract The crankshaft of a compressor fractured through the web remote from the driving end after about three years of service. The fracture ran diagonally across the web into the crankpin. It passed through the centers of two screwed plugs inserted into the web from opposite faces...
Abstract
The crankshaft of a compressor fractured through the web remote from the driving end after about three years of service. The fracture ran diagonally across the web into the crankpin. It passed through the centers of two screwed plugs inserted into the web from opposite faces approximately in line with the crankpin center line. The fracture was of the fatigue type, slowly developing cracks having started from opposite sides of each tapped hole and crept across the section. Microstructure of the crankshaft indicated the material was a plain carbon steel, the carbon content being of the order of 0.3%. The failure resulted principally from the stress-raising effects of the screw holes combined with the cracks in the welds. If the screw holes had been left unfilled or if some form of mechanical locking had been used if plugged, failure would have been postponed if not averted.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001364
EISBN: 978-1-62708-215-0
... Abstract An investigation of the impeller and deposit samples from a centrifugal compressor revealed that an aluminum IR-12 refrigerant reaction had occurred, causing extensive damage to the second-stage impeller and contaminating the internal compressor components. The spherical surface...
Abstract
An investigation of the impeller and deposit samples from a centrifugal compressor revealed that an aluminum IR-12 refrigerant reaction had occurred, causing extensive damage to the second-stage impeller and contaminating the internal compressor components. The spherical surface morphology of the impeller fragments suggested that the aluminum had melted and resolidified. The deposits were similar in composition and were identified by XRD as consisting primarily of aluminum trifluoride. In addition, EDS analysis detected major amounts of chlorine and iron. Results of a combustion test indicated that the compressor deposit was comprised of a 9. 8 wt% carbon and that the condenser deposit contained 8.7 wt% carbon. It was concluded that the primary cause of failure was the rubbing of the impeller against the casting and that a self-sustaining Freon fire had occurred in the failed compressor
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001367
EISBN: 978-1-62708-215-0
... Abstract Cracking was discovered in an in-service, second-stage turbine impeller during a downtime inspection. The fabricated 4300 series low-alloy steel impeller was used in a compressor in an industrial petrochemical plant. It was also reported that a process upset had allowed a 10% NaOH...
Abstract
Cracking was discovered in an in-service, second-stage turbine impeller during a downtime inspection. The fabricated 4300 series low-alloy steel impeller was used in a compressor in an industrial petrochemical plant. It was also reported that a process upset had allowed a 10% NaOH solution to be ingested by the unit. Routine magnetic particle inspection revealed numerous cracks in the hub area and vane tips of the second-stage impeller Additionally, the outside surface of the backing plate showed a cyclic pattern of cracks. An overview of a conventional, systematic metallurgical approach to failure analysis to confirm that the cracking was caused by a caustic stress-corrosion cracking mechanism is presented.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001099
EISBN: 978-1-62708-214-3
... Abstract Uncoated high-strength alloy steel cap screws retaining a cast aluminum (356.0) diffuser assembly in a centrifugal refrigerant compressor failed in a brittle manner a short time after the system was placed in operation. Evidence obtained during the failure analysis indicated...
Abstract
Uncoated high-strength alloy steel cap screws retaining a cast aluminum (356.0) diffuser assembly in a centrifugal refrigerant compressor failed in a brittle manner a short time after the system was placed in operation. Evidence obtained during the failure analysis indicated that the failures were the result of hydrogen embrittlement produced by galvanic corrosion and attendant evolution of hydrogen at the dissimilar junction, which was also the site of the highest tensile stress. Suggested measures for minimizing recurrences included use of lower-strength, galvanically-compatible fasteners and appropriately-applied and treated compatible coatings.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001596
EISBN: 978-1-62708-225-9
... Abstract During testing of compressors under start/stop conditions, several helical suspension springs failed. The ensuing failure investigation showed that the springs failed due to fatigue. The analysis showed that during start/stop testing the springs would undergo both a lateral and axial...
Abstract
During testing of compressors under start/stop conditions, several helical suspension springs failed. The ensuing failure investigation showed that the springs failed due to fatigue. The analysis showed that during start/stop testing the springs would undergo both a lateral and axial deflection, greatly increasing the torsional stresses on the spring. To understand the fatigue limits under these test conditions, a bench test was used to establish the fatigue strength of the springs. The bench tests showed that the failed springs had an unacceptable surface texture that reduced the fatigue life. Based on an understanding of the compressor motion, a Monte Carlo model was developed based on a linear damage theory to predict the fatigue life of the springs during start/stop conditions. The results of this model were compared to actual test data. The model showed that the design was marginal even for springs with acceptable surface texture. The model was then used to predict the fatigue life requirements on the bench test such that the reliability goals for the start/stop testing would be met, thus reducing the risk in qualifying the compressor.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c0047823
EISBN: 978-1-62708-236-5
... Abstract High-horsepower electric motors were utilized to drive large compressors (made of 4340 steel shafts and gear-type couplings) required in a manufacturing process. The load was transmitted by two keys 180 deg apart. Six of the eight compressor shafts were found cracked in a keyway...
Abstract
High-horsepower electric motors were utilized to drive large compressors (made of 4340 steel shafts and gear-type couplings) required in a manufacturing process. The load was transmitted by two keys 180 deg apart. Six of the eight compressor shafts were found cracked in a keyway and one of them fractured after a few months of operation. Visual examination of fractured shaft revealed that the cracks originated from one of the keyways and propagated circumferentially around the shaft. The shaft and coupling slippage was indicated by the upset keys and this type of fracture. The shaft surface both near and in the keyways indicated fretting which greatly reduced the fatigue limit of the shaft metal and initiated fatigue cracks. Fatigue marks were observed on the fractured key. Repetitive impact loading was responsible for propagation of the cracks. The high cyclic bending stresses were caused by misalignment between the electric motor and compressor and were transmitted to the shaft through the geared coupling. Flexible-disk couplings capable of transmitting the required horsepower were installed on the shafts as a corrective measure.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001815
EISBN: 978-1-62708-241-9
... Abstract Copper electrical feedthrough pins used in a bolting application in a refrigeration compressor had functioned without failure for years of production and thousands of units. When some of the pins began to fail, an investigation was conducted to determine the cause. Visual examination...
Abstract
Copper electrical feedthrough pins used in a bolting application in a refrigeration compressor had functioned without failure for years of production and thousands of units. When some of the pins began to fail, an investigation was conducted to determine the cause. Visual examination revealed that the observed fractures were mixed brittle intergranular with ductile microvoid dimples. An extensive analysis of failed samples combined with a process of elimination indicated that the fractures were due to stress-corrosion cracking caused by an unidentified chemical species within the sealed compressor chamber. A unique combination of applied stress, residual stress, stress riser, and grain size helped isolate the failure mechanism to a single production lot of material.
Image
Published: 01 January 2002
Fig. 16 4340 steel compressor shaft that fractured because of peeling-type fatigue cracking. (a) Configuration and dimensions (given in inches). (b) and (c) Photographs showing crack path, failure origin, and beach marks on fracture surfaces of shaft and key
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Image
Published: 01 January 2002
Fig. 46 Tube sheet from an air compressor aftercooler that failed by SCC. (a) Configuration of tube sheet. (b) Micrograph of a specimen etched in 10% ammonium persulfate solution showing intergranular crack propagation. 250×. (c) Macrograph of an unetched specimen showing multiple branching
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Image
Published: 01 January 2002
Fig. 40 Freon-compressor shaft of 4140 steel that failed by fretting corrosion in the bearing area (Example 2). (a) Shaft and bearing assembly. (b) Failed region of shaft, at 2×, showing disturbed metal and partly closed keyway. (c) Shaft side of bearing inner ring, at 3×, showing pitting
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Image
Published: 01 January 2002
Fig. 28 Failed compressor rotor. Arrows indicate fractured portions of blades. 36×
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