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Coating removal

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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001572
EISBN: 978-1-62708-236-5
... with discoloration and coating removal. The substrate material was E52100 which was through-hardened to HRC 55-60. The slippers that were in contact with the coated wobbler surface were made of AISI 06 material. A synthetic oil was used as the hydraulic fluid in the application. The failure in the wobblers...
Image
Published: 30 August 2021
Fig. 20 (a) Photograph of first-stage vane ring following removal from the turbine. (b) Photograph of a vane following removal from the vane ring. (c) Optical micrograph of remnant thermal barrier coating from a hot (white) region. (d) Detail of coating interface from (c). Note the fragment More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006402
EISBN: 978-1-62708-217-4
..., and chromium in excess. No chlorides were detected. Auger spectroscopy revealed the presence of large amounts of carbon and nitrogen. The MIL-C-27725 coating was removed from a portion of the rib side by using a paint stripper. No corrosion or discoloration of the aluminum was observed. Conclusions...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c0048674
EISBN: 978-1-62708-222-8
... to clamp onto the framework prior to springback. The heat treatment cycle of the fasteners consisted of austenitizing, quenching, tempering to obtain a tempered martensite microstructure, acid cleaning, zinc electroplating, coating with a clear dichromate and thereafter baking to remove the nascent...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0045926
EISBN: 978-1-62708-235-8
... that the sodium was present before the chromate conversion treatment was performed. A review of the manufacturing procedures showed that sodium hydroxide was used as a cleaning agent before the chromate conversion coating. Failure cause was that apparently the sodium hydroxide had not been properly removed during...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0091678
EISBN: 978-1-62708-217-4
... by application of a coat of paint primer. During routine maintenance checks, a careful examination was suggested to look for damage to the protective coating, and any necessary repairs should be made by cleaning, priming, and painting. Severely corroded parts should be removed from service. Aircraft...
Image
Published: 15 May 2022
Fig. 22 Mechanisms against biofouling. (a) Antifouling coatings create an inhospitable environment for marine creatures to attach to the surface. (b) Fouling-release coatings facilitate removal of marine creatures from the surface. More
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003549
EISBN: 978-1-62708-180-1
... in the environment; change in the alloy or heat treatment; change in design; use of galvanic protection; use of inhibitors; use of nonmetallic coatings and liners; application of metallic coatings; use of surface treatments, thermal spray, or other surface modifications; corrosion monitoring; and preventive...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091384
EISBN: 978-1-62708-219-8
... Abstract A 25.4 cm (10 in.) diam gray cast iron water main pipe was buried in the soil beneath a concrete slab. The installation was believed to have been completed in the early 20th century. A leak from the pipe resulted in flooding of a warehouse. Once removed, the pipe revealed through-wall...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001656
EISBN: 978-1-62708-219-8
... of nickel-coated bars occurred even when the bar was removed from the concrete shortly after the conclusion of testing. This phenomenon is in contrast to the behaviour of zinc-dipped bars, which exhibited only a mild development of zinc salts on the whole bar surface, while no corrosion of the steel...
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001066
EISBN: 978-1-62708-214-3
... Abstract A flanged 100 mm (4 in.) diam low-carbon steel spool piece lined with Teflon was removed from a sulfuric acid denitrification system after cracks were observed in the painted coating. Visual and microstructural examination along with SEM fractography revealed scaled iron oxides on all...
Series: ASM Handbook
Volume: 11B
Publisher: ASM International
Published: 15 May 2022
DOI: 10.31399/asm.hb.v11B.a0006850
EISBN: 978-1-62708-395-9
... are used. Failure Examples Example 1—Wear Resistance of Polyurethane Elastomeric Coatings Material removal caused by the impact and sliding of a stream of particles is a typical wear mode in the oil and gas industry. Polyurethane elastomeric coatings are being used to increase the service life...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001823
EISBN: 978-1-62708-241-9
... removed from the pipe section by pipeline personnel. The coating adjacent to the feature was adhered and intact. A Plidco sleeve was located over the feature and removed by pipeline personnel before arrival. The feature was through-wall, located at the 1 o’clock orientation. There was no evidence...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046378
EISBN: 978-1-62708-234-1
... of silica, could not be filtered out of the inlet water effectively. A severely worn sleeve that was removed from a pump after only 3387 h of service is shown at left in Fig. 1 . Maximum depth of wear on this sleeve was about 1.6 mm ( 1 16 in.). Fig. 1 Hard-faced austenitic stainless steel...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0048634
EISBN: 978-1-62708-225-9
... to 0.43 mils). The coating was applied from a plating bath to which brighteners were added. Bright, impervious coatings increase the possibility of hydrogen embrittlement in steels by forming a barrier to outward hydrogen diffusion from plated parts. An accepted practice for removing hydrogen picked...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001516
EISBN: 978-1-62708-234-1
... loss. Introduction of external contamination or a wear particle at head/disk interface can lead to both types of errors. In soft errors the coating usually suffers only an extremely light damage which can not be seen with an unaided eye. When the magnetic material is removed or damaged by head media...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001586
EISBN: 978-1-62708-228-0
... to approximately 2.5 in. (6.4 cm), exposing the outer surface of the pipeline. In areas away from the cracks, the coating appeared to be well bonded and was difficult to remove from the pipeline surface. Longitudinally oriented wrinkles in the coating were observed on the sides and lower surfaces along the entire...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006424
EISBN: 978-1-62708-217-4
... valve assembly also submitted to the laboratory. In addition, the coating of the failed valve was flaking off. Although it did not cause the initial malfunction of the pressure/vent valve assembly, subsequent application of the lubricant without the complete removal of previous coats was a potential...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001517
EISBN: 978-1-62708-217-4
... revealed varying levels of signal loss. In Area A, the ultrasonic signal exhibited significant signal attenuation whereas in Area B, there was minimal signal attenuation. Sections from both the defective and non-defective areas were removed, mounted and polished for further examination. The cross-sections...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001455
EISBN: 978-1-62708-234-1
... in providing protection against exfoliation corrosion. The painted specimens all showed exfoliated areas after 4 – 6 years' exposure, but at the regions where the coating had been removed by scratching or machining, corrosion developed within a year. The sprayed coatings afforded protection for the six years...