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Coating defects

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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001589
EISBN: 978-1-62708-235-8
... Abstract The paper discusses the analysis of a coating defect on a high phosphorus electroless nickel (Ni-11 wt. % P) deposit plated on an aluminum alloy substrate. Preliminary investigations had indicated that the elongated defects were possibly caused by the entrapment of long fibers...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001625
EISBN: 978-1-62708-218-1
... with a ferrous material, such as a steel chip. Chemical analysis Coating defects Discoloration Motorcycle components Polymer (Other, miscellaneous, or unspecified) failure Two acrylic-coated polymeric motorcycle components exhibited fisheye blemishes after painting. Only one imperfection...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001215
EISBN: 978-1-62708-235-8
... alloy formation. Even in the case of steel parts with lower silicon contents the reaction between iron and zinc can continue until the pure zinc layer has been consumed entirely if the work piece is not cooled sufficiently after withdrawal. Coating defects Galvanized steels Hot dip galvanizing...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001657
EISBN: 978-1-62708-227-3
...) is even better for failure assessment purposes. Metallographic samples are first examined in the unetched condition to study the distribution of primary carbides, sulphocarbides, inclusions and various forms of casting defects. Coated components are also best suited for an unetched microstructural...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047169
EISBN: 978-1-62708-217-4
... and was thus available for examination. Failure occurred after 37 landings (about 298 roll km, or 185 roll miles). Examination of the fracture surfaces revealed that a forging defect was present in the wall of the wheel half. The anodized coating showed distinct twin-parallel and end-grain patterns between...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001765
EISBN: 978-1-62708-241-9
... bottom along the periphery inside the ring wall and failure of water side epoxy coating. Various measures to prevent such failures in the future are recommended. water storage tank corrosion coating defects carbon steel pitting and holes EDX analysis coating thickness ASTM A283 grade C UNS...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001517
EISBN: 978-1-62708-217-4
... Abstract The purpose of this investigation was to determine the cause of the ultrasonic signal attenuation noted during an inspection of a composite aircraft component. Although ultrasonics was able to identify the location of the defective areas, destructive analysis had to be utilized...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0090994
EISBN: 978-1-62708-225-9
... failed during installation due to the presence of preexisting defects. Crack surfaces were found to be corroded and phosphate coated, indicating that the cracks occurred during manufacture. Installation, which presumably entailed some axial extension, resulted in ductile overload failure at the crack...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001706
EISBN: 978-1-62708-217-4
... surface as shown in Figures 4 , 5 , 6 . Radiographic inspection and ultrasonic NDT tests were conducted according to ASTM standards to reveal defect indications, surface discontinuities and cracks in the failed truck beam. Apart from the visible signs of rust and corrosion, no internal defect...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001504
EISBN: 978-1-62708-217-4
.... Very few overload failures were noted. A number of causes were identified: design deficiencies and manufacturing defects leading mainly to fatigue failures, and poor materials selection and improper maintenance as the principal causes of corrosion-related failures. The survey showed that a proper...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001907
EISBN: 978-1-62708-217-4
... Abstract Aircraft missile launcher attachment bolts fabricated from cadmium-coated Hy-tuf steel were found broken. Subsequent analysis of the broken bolts indicated three causes of failure. First, the bolts had been carburized, which was not in conformance with the heat treating requirements...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003563
EISBN: 978-1-62708-180-1
... in coating thickness causes competitive growth during film deposition. (Although it was assumed that the best available deposition conditions were used to deposit the PVD coatings listed in Table 2 , it is worth appreciating that these are not entirely defect-free coatings, and further improvements in RCF...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0001820
EISBN: 978-1-62708-180-1
..., at the time it is put into service, contains no defects that might induce failure at its operating stress level. The ability to preservice test a pipeline to a high stress level is a unique characteristic of a pipeline. The lines are designed such that they can withstand this type of test without undergoing...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0089617
EISBN: 978-1-62708-232-7
... sticking to the bore surface. Recommendations included reducing the pouring temperatures of the molten metal and spraying a thicker insulating coating onto the mold surface. Centrifugal casting Foundry practice Molds Overheating 4130 UNS G41300 Casting-related failures The forged 4130...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c9001392
EISBN: 978-1-62708-231-0
... Abstract Following leakage which developed within the furnace of a horizontal multi-tubular type boiler, examination revealed a series of cracks adjacent to the stiffening rings in the first plain furnace ring. The fire-side surface of the sample was coated with a layer of oxide scale...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001822
EISBN: 978-1-62708-241-9
... in., and the wall thickness is 0.467 in. The pipes were manufactured by a qualified pipe mill in Saudi Arabia. The steel coils used for manufacturing of pipes were procured from a local steel mill. The total transportation distance from the pipe mill to the coating yard and then to the site was about 110 km...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001381
EISBN: 978-1-62708-215-0
... Abstract A helicopter main rotor bolt failed in the black-coated region between the threads and the taper section of the shank during assembly. The torque applied was approximately 100 N·m (900 in.·lbf) when the bolt sheared. No other bolts were reported to have failed. The failed bolt material...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0047312
EISBN: 978-1-62708-224-2
... the presence of graphite nodules, indicating the probability that the component was manufactured from a ductile cast iron. The fractured surface also exhibited the presence of a dark region toward the center, suggesting the possibility of a shrinkage defect. The estimated area of this defect was approximately...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001803
EISBN: 978-1-62708-241-9
... with the presence of superficial manufacturing routes. As a result of the analysis of various implant materials, the main reasons for failure are corrosive attack, manufacturing defects, and nonstandard-caused failures. Biocompatible inorganic materials, such as hydroxyapatite coating with some binders, would...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0048620
EISBN: 978-1-62708-225-9
... Abstract Two nuts were used to secure the water-supply pipes to the threaded connections on hot-water and cold-water taps. The nut used on the cold-water tap fractured about one week after installation. Examination of the fracture surfaces of the coldwater nut did not reveal any obvious defects...