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Book Chapter
Failure of Carburized Steel Impeller Drive Gears Due to Pitting and a Wear Pattern
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048253
EISBN: 978-1-62708-234-1
... Abstract Two intermediate impeller drive gears (made of AMS 6263 steel, gas carburized, hardened, and tempered) exhibited evidence of pitting and abnormal wear after production tests in test-stand engines. The gears were examined for hardness, case depth, and microstructure of case and core...
Abstract
Two intermediate impeller drive gears (made of AMS 6263 steel, gas carburized, hardened, and tempered) exhibited evidence of pitting and abnormal wear after production tests in test-stand engines. The gears were examined for hardness, case depth, and microstructure of case and core. It was found that gear 1 had a lower hardness than specified while the case hardness of gear 2 was found to be within limits. Both the pitting and the wear pattern were revealed to be more severe on gear 1 than on gear 2. Surface-contact fatigue (pitting) of gear 1 (cause of lower carbon content of the carburized case and hence lower hardness) was found to be the reason for failure. It was recommended that the depth of the carburized case on impeller drive gears be increased from 0.4 to 0.6 mm to 0.6 to 0.9 mm to improve load-carrying potential and wear resistance. A minimum case-hardness requirement was set at 81 HRA.
Book Chapter
Fatigue Failure of a Carburized Steel Bevel Pinion Because of Misalignment
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0048273
EISBN: 978-1-62708-225-9
... Abstract Several teeth of a bevel pinion which was part of a drive unit in an edging mill failed after three months in service. Specifications required that the pinion be made from a 2317 steel forging and that the teeth be carburized and hardened to a case hardness of 56 HRC and a core...
Abstract
Several teeth of a bevel pinion which was part of a drive unit in an edging mill failed after three months in service. Specifications required that the pinion be made from a 2317 steel forging and that the teeth be carburized and hardened to a case hardness of 56 HRC and a core hardness of 250 HRB. Two teeth were revealed by visual examination to have broken at the root and fatigue marks extending across almost the entire tooth were exhibited by the surface of the fracture. Cracking in all the tooth was showed by magnetic-particle inspection. The pinion was concluded to have failed by tooth-bending fatigue. Spalling was also noted on the pressure (drive) side of each tooth at the toe end which indicated some mechanical misalignment of the pinion with the mating gear that caused the cyclic shock load to be applied to the toe ends of the teeth.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0048257
EISBN: 978-1-62708-217-4
... of AMS 6263 steel and was gas carburized to produce a case 0.4 to 0.6 mm (0.015 to 0.025 in.) deep. Investigation Sections of the gear were removed and examined for hardness, case depth, and microstructure of case and core. The results of the examination and the specified requirements were...
Abstract
Evidence of destructive pitting on the gear teeth (AMS 6263 steel) in the area of the pitchline was exhibited by an idler gear for the generator drive of an aircraft engine following test-stand engine testing. The case hardness was investigated to be lower than specified and it was suggested that it had resulted from surface defects. A decarburized surface layer and subsurface oxidation in the vicinity of pitting were revealed by metallographic examination of the 2% nital etched gear tooth sample. It was concluded that pitting had resulted as a combination of both the defects. The causes for the defects were reported based on previous investigation of heat treatment facilities. Oxide layer was caused by inadequate purging of air before carburization while decarburization was attributed to defects in the copper plating applied to the gear for its protection during austenitizing in an exothermic atmosphere. It was recommended that steps be taken during heat treatment to ensure neither of the two occurred.
Book Chapter
Fatigue Failure of a Carburized Steel Gear From a Helicopter Transmission
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001077
EISBN: 978-1-62708-214-3
... Abstract The failure of a spiral bevel gear from the transmission of a helicopter was discovered when the transmission was removed after an in-flight incident. Two adjacent teeth from the carburized AISI 9310 steel gear were found to have undergone fatigue failure. Internal initiation occurred...
Abstract
The failure of a spiral bevel gear from the transmission of a helicopter was discovered when the transmission was removed after an in-flight incident. Two adjacent teeth from the carburized AISI 9310 steel gear were found to have undergone fatigue failure. Internal initiation occurred in a region depleted of chromium and nickel. This condition coincides with a microstructural inhomogeneity consisting of large, soft ferrite grains. Its origin was probably contamination of the solidifying ingot during the consumable vacuum arc remelting operation.
Image
Micrograph of AISI 4118 carburized steel as quenched and tempered. The micr...
Available to PurchasePublished: 01 January 2002
Fig. 45 Micrograph of AISI 4118 carburized steel as quenched and tempered. The microstructure is tempered martensite (unetched) with a quench crack propagating from a machining burr. 200×. Source: Ref 27
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Image
Micrograph of 4% Ni-C-Cr carburized steel showing massive carbides produced...
Available to PurchasePublished: 01 January 2002
Fig. 76 Micrograph of 4% Ni-C-Cr carburized steel showing massive carbides produced during carburizing with surface carbon above Ac cm carbon. Source: Ref 30
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0048261
EISBN: 978-1-62708-225-9
... holes ( Fig. 1 ) used to mount the gear to a hub. The intersection of the hole and root fillet created an acute-angle condition (Section A-A, Fig. 1 ). Fig. 1 Carburized 4817 steel spiral bevel gear. The gear broke from fatigue at acute-angle intersections of mounting holes and tooth-root...
Abstract
The gear of a spiral bevel gear set broke into three pieces after about two years of service. The gear (made of 4817 steel) broke along the root of a tooth intersected by three of the six 22-mm diam holes used to mount the gear to a hub. Fatigue progression for about 6.4 mm at the acute-angle intersections of three mounting holes with the root fillets of three teeth was revealed by examination of gear. Cracks at the intersections of the remaining three mounting holes and the adjacent tooth-root fillets were revealed by magnetic-particle inspection. Through hardening at the acute-angle intersections of the mounting holes and tooth-root fillets was revealed by metallographic examination. Design of the gear and placement of the mounting holes, which resulted in through hardening, were concluded to be the contributing factors to the fatigue failure of the gear.
Image
Light micrographs of the surface of a carburized 8620 alloy steel specimen ...
Available to PurchasePublished: 01 January 2002
Fig. 10 Light micrographs of the surface of a carburized 8620 alloy steel specimen mounted in phenolic resin. Note the shrinkage gap (see arrows in a) that has reduced the edge flatness. In (b), taken at 1000×, decarburization at the surface has caused ferrite and pearlite to form
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Image
Steel shaft (AISI 4817) carburized and hardened to HRC 60. Component loaded...
Available to PurchasePublished: 01 January 2002
Fig. 49 Steel shaft (AISI 4817) carburized and hardened to HRC 60. Component loaded in rotating bending. Fracture initiation in six fillet areas around the periphery. Six initiation sites are visible as evidenced by multiple sets of beach marks (curved black lines). Source: Ref 29
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Image
Fracture surface of a carburized and hardened steel roller. As a result of ...
Available to PurchasePublished: 01 January 2002
Fig. 6 Fracture surface of a carburized and hardened steel roller. As a result of banded alloy segregation, circumferential fatigue fracture initiated at a subsurface origin near the case-core interface (arrow).
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Image
Internal oxidation of a nickel-chromium steel carburized in a laboratory fu...
Available to PurchasePublished: 01 January 2002
Fig. 69 Internal oxidation of a nickel-chromium steel carburized in a laboratory furnace, showing both grain-boundary oxides and oxide precipitates within grains. 402×. Source: Ref 30
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Image
Globular carbides at the surface of a carburized 1% Cr-Mo steel (reheat que...
Available to PurchasePublished: 01 January 2002
Fig. 79 Globular carbides at the surface of a carburized 1% Cr-Mo steel (reheat quenched). 836×. Source: Ref 30
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Image
Cross sections through the carburized 1117 steel cylinders from two spool-t...
Available to PurchasePublished: 01 January 2002
Fig. 11 Cross sections through the carburized 1117 steel cylinders from two spool-type hydraulic valves. The cylinder of the valve that operated satisfactorily (a) had little retained austenite in the case, whereas the cylinder of the seized valve (b) had much retained austenite
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Image
Carburized AMS 6260 steel gear damaged by adhesive wear. (a) Overall view o...
Available to PurchasePublished: 01 January 2002
Fig. 39 Carburized AMS 6260 steel gear damaged by adhesive wear. (a) Overall view of damaged teeth. (b) Etched end face of the gear showing excessive stock removal from drive faces of teeth
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Image
Pitting and wear pattern on a carburized AMS 6263 steel impeller drive gear...
Available to PurchasePublished: 01 January 2002
Fig. 46 Pitting and wear pattern on a carburized AMS 6263 steel impeller drive gear. Approximately 2.3×
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Image
Carburized 4817 steel spiral bevel gear. The gear broke from fatigue at acu...
Available to PurchasePublished: 01 January 2002
Fig. 48 Carburized 4817 steel spiral bevel gear. The gear broke from fatigue at acute-angle intersections of mounting holes and tooth-root fillets as a result of through hardening. Dimensions given in inches
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Image
Fatigue fracture in gas-carburized and modified 4320 steel showing overview...
Available to PurchasePublished: 01 January 2002
Fig. 8 Fatigue fracture in gas-carburized and modified 4320 steel showing overview of initiation, stable crack propagation, and unstable crack propagation, with extent of stable crack indicated by dashed line
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Image
Fracture surface of a carburized-and-hardened steel roller. As a result of ...
Available to PurchasePublished: 01 January 2002
Fig. 38 Fracture surface of a carburized-and-hardened steel roller. As a result of banded alloy segregation, circumferential fatigue fracture initiated at a subsurface origin near the case/core interface (arrow).
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Image
Cross sections through the carburized 1117 steel cylinders from two spool-t...
Available to PurchasePublished: 15 January 2021
Fig. 11 Cross sections through the carburized 1117 steel cylinders from two spool-type hydraulic valves. The cylinder of the valve that operated satisfactorily (a) had little retained austenite in the case, whereas the cylinder of the seized valve (b) had much retained austenite
More
Image
Light micrographs of the surface of a carburized 8620 alloy steel specimen ...
Available to PurchasePublished: 15 January 2021
Fig. 2 Light micrographs of the surface of a carburized 8620 alloy steel specimen mounted in phenolic resin. Note the shrinkage gap (see arrows in a) that has reduced the edge flatness. In (b), taken at 1000×, decarburization at the surface has caused ferrite and pearlite to form
More
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