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Bombs (weapons)
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001905
EISBN: 978-1-62708-217-4
... confirmed that the component was in the annealed condition and not in the required work-hardened 1/4-hard condition. Bombs (weapons) Retaining bands Equiaxed structure Dimensional measurements 302 UNS S30200 Heat treating related failures Introduction Component: MK#15/Mod 6 Snakeye bomb...
Abstract
A bomb retaining ring fabricated from type 302 stainless steel unwrapped during a practice flight, causing the bomb fins to deploy. The retaining ring was able to unwrap itself because it was thinner and softer than required. Hardness testing, metallography, and tensile testing confirmed that the component was in the annealed condition and not in the required work-hardened 1/4-hard condition.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001909
EISBN: 978-1-62708-235-8
... parameters resulted in acceptable welds. Bombs (weapons) Bomb fins Welded joints Weld defects Low-carbon steel Joining-related failures Introduction Component: MK#83 and MK#84 general purpose bomb fins Manufacturing defects: Nonpenetrating plug welds Background A First Article...
Abstract
Welded low-carbon steel bomb fins were rejected because of poor weld practice. Visual and metallographic examination revealed that the resistance plug welds that attach the outer skin to the inner spar displayed inadequate weld penetration. Recommended changes to the resistance welding parameters resulted in acceptable welds.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001908
EISBN: 978-1-62708-235-8
..., and shrinkage defects in the castings. Most of the components failed to meet required mechanical properties because of these casting defects. Bombs (weapons) Tailcones Die castings Heat checking Inclusions Shrinkage Porosity A356 UNS A13560 Casting related failures Introduction Component...
Abstract
Cluster bomb tailcone assemblies each containing two aluminum die-cast components were rejected because of the poor surface condition of the die castings. Numerous heat checks were found on the surfaces of the tailcones and radiographic inspection revealed inclusions, gas holes, and shrinkage defects in the castings. Most of the components failed to meet required mechanical properties because of these casting defects.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001906
EISBN: 978-1-62708-217-4
... testing, scanning electron microscopy, and energy-dispersive x-ray spectroscopy. It was determined that the failures were due to forging defects. Both forging laps and seams acted as stress concentrators when the lugs were loaded during proof testing. Bombs (weapons) Suspension lugs Forging...
Abstract
Suspension lugs fabricated from AISI 4340 steel used to facilitate loading of bombs onto the underside of military aircraft could not sustain required loads during routine proof load testing. Three failed lugs underwent visual examination, chemical analysis, metallography, hardness testing, scanning electron microscopy, and energy-dispersive x-ray spectroscopy. It was determined that the failures were due to forging defects. Both forging laps and seams acted as stress concentrators when the lugs were loaded during proof testing.
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006817
EISBN: 978-1-62708-329-4
Abstract
Reliability-centered maintenance (RCM) is a systematic methodology for preventing failures. This article begins by discussing the history of RCM and uses Society of Automotive Engineers (SAE) all-industry standard JA1011 as its model to describe the key characteristics of an RCM process. It then expands on questions involved in RCM process, offering definitions when necessary. Next, the article describes the approach of RCM to failure modes and effects analysis (FMEA), the failure management policies available under RCM, and the criteria of RCM for deciding when a specific failure management policy is technically feasible. Then, after discussing the ways that RCM classifies failure effects in terms of consequences, it describes how RCM uses failure consequences to identify the best failure management policy for each failure mode. Next, the building blocks of RCM are put together to create a failure management program. The article ends with a discussion on some practical issues pertaining to RCM that lie outside the scope of SAE JA1011.