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Cassio Barbosa, Simone Kessler de Barros, Ibrahim de Cerqueira Abud, Joneo Lopes do Nascimento, Sheyla Santana de Carvalho
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Boiler tubes
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001480
EISBN: 978-1-62708-229-7
... Abstract One tube in a watertube boiler developed leakage from a perforation. The external surface was covered with a dark deposit indicative of local fusion. Perforation resulted from the development of a crack from the internal surface. Microscopic examination revealed extensive intergranular...
Abstract
One tube in a watertube boiler developed leakage from a perforation. The external surface was covered with a dark deposit indicative of local fusion. Perforation resulted from the development of a crack from the internal surface. Microscopic examination revealed extensive intergranular penetration by molten copper. Particles of copper were seen in scale deposits on the bore of the tube. The tube in general showed a ferritic structure with partially spheroidized carbide. The fact that fusion of the copper had occurred indicated temperatures of 1100 deg C (2012 deg F) had been experienced locally, and the structural condition suggested that the tube in general had been heated at a lower temperature of the order of 600 deg C (1112 deg F) for some appreciable time. In this instance, overheating of the tube in the absence of the copper deposits may not have led to failure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001176
EISBN: 978-1-62708-229-7
... Abstract A backwell tube situated in the combustion chamber of a 100 atm boiler, which had been in service for many years, failed. The temperature of the saturated steam was about 300 deg C. Two pipe sections with attacked areas in the circumferential welding joint were examined for cause...
Abstract
A backwell tube situated in the combustion chamber of a 100 atm boiler, which had been in service for many years, failed. The temperature of the saturated steam was about 300 deg C. Two pipe sections with attacked areas in the circumferential welding joint were examined for cause of failure. First section showed strong pit or trench-like attack in the welding seam on the inner surface. A bluish-black corrosion product adhered to the pits. The second section showed small blisters at the welding seam. The metallographic examination of the first section showed welding seam was strongly reduced in bulk from the inside and covered with a thick crumbling layer of magnetic iron oxide (Fe3-O4). This was a corrosion product resulting from the operation of the boiler. In addition, it was decarburized from the inside, and interspersed with grain boundary cracks. This form of attack is typical for the decarburization of steel by high-pressure hydrogen. Hence, the defects in the pipe sections were the result of scaling during the operation of the steam boiler. It was recommended to avoid unnecessary overheating during the welding of materials for high-pressure steam boiler operations.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001482
EISBN: 978-1-62708-229-7
... Abstract Penetration by molten copper occurred in the economizer of a large water-tube boiler. A cross section through a weld and the crack in the tube revealed a crack was an intergranular fissure. Small fissures of the same type also extended from its flanks. The main fissure was filled...
Abstract
Penetration by molten copper occurred in the economizer of a large water-tube boiler. A cross section through a weld and the crack in the tube revealed a crack was an intergranular fissure. Small fissures of the same type also extended from its flanks. The main fissure was filled with an oxide scale in which were embedded particles having the appearance of metallic copper. It was concluded that the cracking that occurred at the time of re-welding was due to intergranular penetration by copper present in the deposit within the tubes, which had not been completely removed prior to welding. Subsequently, it was ascertained that trouble had been experienced with the centrifugal feed pumps, resulting in scuffing of some bronze rings. The presumption is that bronze particles had been carried in mechanical suspension in the feed water and deposited in the economizer tubes.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0048350
EISBN: 978-1-62708-227-3
... Abstract Tubes in a marine boiler on a new ship failed after brief service lives. Circumferential brittle cracking was found to occur in the carbon-molybdenum steel tubes near the points where the tubes were attached to the steam drum. Fatigue striations were revealed by examination of fracture...
Abstract
Tubes in a marine boiler on a new ship failed after brief service lives. Circumferential brittle cracking was found to occur in the carbon-molybdenum steel tubes near the points where the tubes were attached to the steam drum. Fatigue striations were revealed by examination of fracture surfaces by electron microscopy at high magnification. Fatigue failures were concluded to be caused by vibrations resulting from normal steam flow at high steam demand. Too rigid support near the steam drum resulted in concentration of vibratory strain in the regions of failure. The method of supporting the tubes was changed to reduce the amount of restraint and the strain concentration.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048289
EISBN: 978-1-62708-234-1
... Abstract The center portions of two adjacent low-carbon steel boiler tubes (made to ASME SA-192 specifications) ruptured during a start-up period after seven months in service. It was indicated by reports that there had been sufficient water in the boiler two hours before start-up...
Abstract
The center portions of two adjacent low-carbon steel boiler tubes (made to ASME SA-192 specifications) ruptured during a start-up period after seven months in service. It was indicated by reports that there had been sufficient water in the boiler two hours before start-up. The microstructure near the rupture edge was revealed by metallographic examination to consist of ferrite and acicular martensite or bainite. The microstructure and the observed lack of cold work indicated a temperature above the transformation temperature of 727 deg C had been reached. Swelling of the tubes was disclosed by the wall thickness and OD of the tubing. The tubes were concluded to have failed due to rapid overheating.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001340
EISBN: 978-1-62708-215-0
... Abstract Two identical “D” tube package boilers, installed at separate plants, experienced a number of tube ruptures after relatively short operating times. The tubes, which are joined by membranes, experienced localized bulging and circumferential cracking along the fireside crown as a result...
Abstract
Two identical “D” tube package boilers, installed at separate plants, experienced a number of tube ruptures after relatively short operating times. The tubes, which are joined by membranes, experienced localized bulging and circumferential cracking along the fireside crown as a result of overheating and thermal fatigue. It was recommended that recent alterations to the steam-drum baffling be remodified to improve circulation in the boiler and prevent further overheating. Several thermocouples were attached to tubes in problem areas of the boiler to monitor the effects of the steam-drum modifications on tube wall temperatures.
Image
Published: 01 January 2002
Fig. 9 Microstructures of specimens from carbon steel boiler tubes subjected to prolonged overheating below Ac 1 . (a) Voids (black) in grain boundaries and spheroidization (light, globular), both of which are characteristic of tertiary creep. 250×. (b) Intergranular separation adjacent
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Image
Published: 01 January 2002
Fig. 10 Typical microstructures of 0.18% C steel boiler tubes that ruptured as a result of rapid overheating. (a) Elongated grains near tensile rupture resulting from rapid overheating below the recrystallization temperature. (b) Mixed structure near rupture resulting from rapid overheating
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Image
Published: 01 January 2002
Fig. 12 Plots of scale thickness versus temperature for two sizes of boiler tubes and two values of heat flux. (a) and (b) The effect of scale thickness on the temperature gradient across the scale. (c) and (d) The effect of scale thickness on the temperature of the metal at the outer surface
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Image
Published: 15 January 2021
Fig. 19 Oxygen pitting along the outside-diameter surface of boiler tubes from a fire-tube boiler. (a) Through-wall pitting due to oxygen pitting. (b) Oxygen pitting had penetrated approximately 80% of the boiler tube wall thickness on this sample.
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Image
Published: 15 January 2021
Fig. 9 (a) Short-term and (b) long-term overheating of boiler tubes. Long-term overheating usually is caused by creep as the microstructure of the material degrades at temperature over time. Grains do not deform, but voids develop at grain-boundary junctions and grow and coalesce over time
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0091291
EISBN: 978-1-62708-234-1
... Abstract Carbon steel tubes from a boiler feedwater heater feeding a deaerator were treated to control scale formation, but the treatment instead produced more iron oxide. The additional iron oxide reduced the tubing to a totally corroded condition. Investigation showed that the chelate...
Abstract
Carbon steel tubes from a boiler feedwater heater feeding a deaerator were treated to control scale formation, but the treatment instead produced more iron oxide. The additional iron oxide reduced the tubing to a totally corroded condition. Investigation showed that the chelate injected to control the scaling was added ahead of the preheater, where the boiler water still contained oxygen. As the chelate removed iron oxide, the O2 in the water continued to form more. Recommendations included moving the chelate addition to a point after the deaerator to stop the corrosion.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001709
EISBN: 978-1-62708-229-7
... Abstract Several waterwall tubes in a power station boiler failed after ten years of service. The boiler is a suspension type equipped with 30 IK boxes where retractable soot blowers are inserted to clean the inside of the boiler using high-pressure steam. The tubes, which operate at 693 deg F...
Abstract
Several waterwall tubes in a power station boiler failed after ten years of service. The boiler is a suspension type equipped with 30 IK boxes where retractable soot blowers are inserted to clean the inside of the boiler using high-pressure steam. The tubes, which operate at 693 deg F (367 deg C) and 2935 psi (20.5 MPa), failed near the IK boxes as a result of thermal fatigue. Thermal fatigue damage was accelerated by repetitive exposure to water droplets from the soot blower and the associated rapid cooling.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001479
EISBN: 978-1-62708-229-7
... Abstract Several ruptures took place in the front wall tubes of a water tube boiler. Some rupture samples showed ductile failure while others showed brittle failure. Specimens taken from the rupture where a thick edge had been produced, i.e., with little evidence of prior plastic deformation...
Abstract
Several ruptures took place in the front wall tubes of a water tube boiler. Some rupture samples showed ductile failure while others showed brittle failure. Specimens taken from the rupture where a thick edge had been produced, i.e., with little evidence of prior plastic deformation, showed a coarse microstructure indicative of gross overheating. The examination indicated that failure in the main resulted from gross overheating arising from water starvation as could have been due to a number of causes. The ruptures in some tubes were of the type commonly found in overheated tubes, the material being drawn out to a feather edge at the time of rupture. Other ruptures in the same and other tubes were of a more brittle type, this being associated with penetration of material by molten copper derived from scale.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001834
EISBN: 978-1-62708-241-9
... to high temperature corrosive flux accelerated the corrosion on the outer wall. Microstructure degradation and the corrosion characteristics observed indicate that the tubes failed primarily because of overheating, which is confirmed by calculations. boiler tubes stress rupture wall thinning low...
Abstract
The failure of T12 reheater tubes that had been in service for only 3000 h was investigated. The thickness of the tubes was visibly reduced by heavy oxidation corrosion on the inner and outer walls. The original pearlite substrate completely decomposed. Uniform oxide scale observed on the inner wall showed obvious vapor oxidation corrosion characteristics. Corrosion originated in the grain boundary, and selective oxidation occurred due to ion diffusion in the substrate. The layered oxide scale on the inner wall is related to the different diffusion rates for different cations. Exposure to high temperature corrosive flux accelerated the corrosion on the outer wall. Microstructure degradation and the corrosion characteristics observed indicate that the tubes failed primarily because of overheating, which is confirmed by calculations.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001194
EISBN: 978-1-62708-235-8
... Abstract A seamless hot-drawn boiler tube NW 300 of 318 mm OD and 9 mm wall thickness made of steel 15Mo3 was bent with sand filling after preheating allegedly to 1000 deg C. In the process it had cracked repeatedly in the drawn fiber. The composition corresponded to specifications...
Abstract
A seamless hot-drawn boiler tube NW 300 of 318 mm OD and 9 mm wall thickness made of steel 15Mo3 was bent with sand filling after preheating allegedly to 1000 deg C. In the process it had cracked repeatedly in the drawn fiber. The composition corresponded to specifications, but exceptionally high copper content was noticeable. Microstructural examination showed the damage was due to overheating and burning during preheating and bending. Furthermore, crack formation was promoted by precipitation of metallic copper that had penetrated into the austenitic grain boundaries under the influence of tensile stresses that arose during bending. This phenomenon is known as “solder brittleness.”
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001569
EISBN: 978-1-62708-229-7
... of other units. Boilers Economizers Superheaters Tubing Steel tube Corrosion fatigue Transgranular fracture Fatigue fracture Introduction Understanding the characteristic causes of fatigue failures should help to identify areas of the boiler that may be more likely to fail by fatigue...
Abstract
This paper reviews several fatigue failures from the waterwall, superheater, and economizer portions of the boiler, their causes and how they were mitigated and monitored. Some cases required simple field modifications by cutting or welding, repair of existing controls, and/or changes in maintenance. Nondestructive inspections by visual, magnetic particle, ultrasonic, and radiographic methods for detecting and monitoring damage are discussed. These failures are presented to provide hindsight that will help others in increasing the success rate for anticipating and analyzing the remaining life of other units.
Book Chapter
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001791
EISBN: 978-1-62708-241-9
... temperatures. The combined effect of pitting, incrustations, and phase transformations caused the pipe to rupture. boiler tube fracture corrosion pits salt incrustation carbon steel thermal fatigue striations dimples microstructural analysis plastic strain A192 (carbon steel) UNS K01201...
Abstract
A pipe in the lateral wall of a boiler powering an aircraft carrier flat-top boat failed during a test at sea. The pipe was made from ASTM 192 steel, an adequate material for the application. Microstructural analysis along with equipment operating records provided valuable insight into what caused the pipe to rupture. Although the pipe had been replaced just 50 h before the accident, the analysis revealed incrustations and corrosion pits on the inner walls and oxidation on the outer walls. Microstructural changes were also observed, indicating that the steel was exposed to high temperatures. The combined effect of pitting, incrustations, and phase transformations caused the pipe to rupture.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001739
EISBN: 978-1-62708-215-0
... Abstract The rear wall tube section of a boiler that had been in service for approximately 38 years was removed and examined. Visual examination of the tube revealed a small bulge with a through-wall crack. Metallography showed that the microstructure of the bulged area consisted of a few...
Abstract
The rear wall tube section of a boiler that had been in service for approximately 38 years was removed and examined. Visual examination of the tube revealed a small bulge with a through-wall crack. Metallography showed that the microstructure of the bulged area consisted of a few partially decarburized pearlite colonies in a ferrite matrix. The microstructure remote from the bulged area consisted of pearlite in a ferrite matrix. EDS analysis of internal deposits on the tube detected a major amount of iron, plus trace amounts of other elements. The evidence indicated that the bulge and crack in the tube resulted from hydrogen damage. Examination of the remaining water circuit boiler tubing using nondestructive techniques and elimination of any heavy deposit buildup was recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001433
EISBN: 978-1-62708-235-8
... Abstract On attempting to manipulate or bend a boiler tube some 22 ft. long, sudden failure occurred at what appeared to be a butt weld in the tube. Externally, the weld reinforcement had been ground flush and the entire tube surface painted. Internally, the appearance and width of the heated...
Abstract
On attempting to manipulate or bend a boiler tube some 22 ft. long, sudden failure occurred at what appeared to be a butt weld in the tube. Externally, the weld reinforcement had been ground flush and the entire tube surface painted. Internally, the appearance and width of the heated band suggested that the weld had been made by the oxy-gas process. A lack of root fusion over most of its length was evident. Examination of the fracture faces, which were of crystalline appearance indicative of brittle behavior, indicated incomplete fusion of the weld root. Microscopic examination showed the deposit to possess a large grain size with a low carbon content disposed as carbides along the grain boundaries, a feature which would provide an explanation of the brittle behavior. Subsequent inspection showed that this tube was one of several of the batch ordered for retubing of a boiler and which had a 2 ft. length welded to one end to make up the length.
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