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Adrian Pierorazio, Nicholas E. Cherolis, Michael Lowak, Daniel J. Benac, Matthew T. Edel
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Blistering
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001454
EISBN: 978-1-62708-220-4
...Abstract Abstract The interior of a cylindrical tank used for the road transport of concentrated sulfuric acid revealed severe blistering of the plates, mainly over the crown and more particularly on the first ring. The tank, made in 1958, was of welded construction, the material being mild...
Abstract
The interior of a cylindrical tank used for the road transport of concentrated sulfuric acid revealed severe blistering of the plates, mainly over the crown and more particularly on the first ring. The tank, made in 1958, was of welded construction, the material being mild steel plate. Some of the blisters were pierced by drilling a hole in the center and at the same time applying a small flame. In several cases combustion of the escaping gas caused minor explosions, a result characteristic of hydrogen. Etching showed the material to be a low-carbon steel in the partly spheroidized condition. There was no evidence of cracking of the material in the region of the blisters and bend tests demonstrated it possessed satisfactory ductility. The primary cause of the blistering was ascribed to the presence of discontinuities within the plate. This provided cavities in which the hydrogen was able to accumulate and build up pressure. Had the material been free from discontinuities of appreciable size, the blistering would not have occurred.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001235
EISBN: 978-1-62708-228-0
... by cracks or blisters almost over its entire perimeter in agreement with the ultrasonic test results. Only the weld seam and a strip on each side of it were crack-free. Based on this investigation, the pipeline was taken out of service and reconstructed. To avoid such failures in the future, two...
Abstract
A welded natural gas line of 400 mm OD and 9 mm wall thickness made of unalloyed steel with 0.22C had to be removed from service after four months because of a pipe burst. Metallographic examination showed the pipe section located next to the gas entrance was permeated by cracks or blisters almost over its entire perimeter in agreement with the ultrasonic test results. Only the weld seam and a strip on each side of it were crack-free. Based on this investigation, the pipeline was taken out of service and reconstructed. To avoid such failures in the future, two preventative measures may be considered. One is to desulfurize the gas. Based on tests, however, the desulfurization would have to be carried very far to be successful. The second possibility is to dry the gas to such an extent as to prevent condensate, and this corrosion, from forming no matter how low winter temperatures may drop. This measure was ultimately recommended, deemed more effective and cheaper.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001546
EISBN: 978-1-62708-217-4
... material, and those that exhibited a dual failure. The last category failed in the adhesive bond and also showed a type of pitting on one face of the base material. In a third case, a 2024-T4 extrusion section was found to exhibit blistering after chemical milling. The presence of interconnecting...
Abstract
A longeron assembly constructed of Alclad 2024, some parts being in the T3 condition, others in the T42 condition, failed at a rivet hole. Plastic deformation at the crack site was found, but no plastic deformation was found in similar failed components. It was concluded that the numerous hairline cracks in the Alclad layer adjacent to the main fracture were fatigue cracks. In another case, bonded samples of 2024-T3 sheet were fatigue tested at various stress levels. Failures could be separated into three groups: those that failed in the adhesive bond, those that failed in the base material, and those that exhibited a dual failure. The last category failed in the adhesive bond and also showed a type of pitting on one face of the base material. In a third case, a 2024-T4 extrusion section was found to exhibit blistering after chemical milling. The presence of interconnecting microcracks between adjacent discontinuities supported a hydrogen blistering diagnosis.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001765
EISBN: 978-1-62708-241-9
...Abstract Abstract This paper describes the investigation of a corrosion failure of bottom plates on an aboveground tank used for the storage of potable water. The tank was internally inspected for the first time after six years of service. Paint blisters and rust spots were observed...
Abstract
This paper describes the investigation of a corrosion failure of bottom plates on an aboveground tank used for the storage of potable water. The tank was internally inspected for the first time after six years of service. Paint blisters and rust spots were observed on the bottom plates and first to third course shell plates. Sand blasting and repainting of the bottom plates and first course shell plates was to be used as a remedial measure. However, during the sand blasting, holes and deep pitting were observed on the bottom plates. On-site visual inspection, magnetic flux leakage (MFL) inspection, ultrasonic testing (UT), and evaluation of the external cathodic protection (CP) system were used in the failure analysis. The corrosion products were analyzed using energy-dispersive X-ray analysis (EDAX). The failure is attributed to the ingress of water and its impoundment under the tank bottom along the periphery inside the ring wall and failure of water side epoxy coating. Various measures to prevent such failures in the future are recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001176
EISBN: 978-1-62708-229-7
... for cause of failure. First section showed strong pit or trench-like attack in the welding seam on the inner surface. A bluish-black corrosion product adhered to the pits. The second section showed small blisters at the welding seam. The metallographic examination of the first section showed welding seam...
Abstract
A backwell tube situated in the combustion chamber of a 100 atm boiler, which had been in service for many years, failed. The temperature of the saturated steam was about 300 deg C. Two pipe sections with attacked areas in the circumferential welding joint were examined for cause of failure. First section showed strong pit or trench-like attack in the welding seam on the inner surface. A bluish-black corrosion product adhered to the pits. The second section showed small blisters at the welding seam. The metallographic examination of the first section showed welding seam was strongly reduced in bulk from the inside and covered with a thick crumbling layer of magnetic iron oxide (Fe3-O4). This was a corrosion product resulting from the operation of the boiler. In addition, it was decarburized from the inside, and interspersed with grain boundary cracks. This form of attack is typical for the decarburization of steel by high-pressure hydrogen. Hence, the defects in the pipe sections were the result of scaling during the operation of the steam boiler. It was recommended to avoid unnecessary overheating during the welding of materials for high-pressure steam boiler operations.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001613
EISBN: 978-1-62708-235-8
... and microvoid coalescence in the center. The improper baking after electroplating of the screw led to H2-induced blistering/cracking. The high strength of the threaded region of the adjusting screw increased the failure propensity. Electroplating 16MnCr5 DIN 17210 Hydrogen damage and embrittlement...
Abstract
The electroplated tappet adjusting screws used in diesel engines failed during initial bend testing. The analysis of the failure showed that the fracture was nucleated from the subsurface of the screw. The fracture surface was intergranular at the ID and OD region and microvoid coalescence in the center. The improper baking after electroplating of the screw led to H2-induced blistering/cracking. The high strength of the threaded region of the adjusting screw increased the failure propensity.
Book Chapter
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003507
EISBN: 978-1-62708-180-1
.... The article discusses the types of imperfections that can be traced to the original ingot product. These include chemical segregation; ingot pipe, porosity, and centerline shrinkage; high hydrogen content; nonmetallic inclusions; unmelted electrodes and shelf; and cracks, laminations, seams, pits, blisters...
Abstract
This article describes the general root causes of failure associated with wrought metals and metalworking. This includes a brief review of the discontinuities or imperfections that may be the common sources of failure-inducing defects in bulk working of wrought products. The article discusses the types of imperfections that can be traced to the original ingot product. These include chemical segregation; ingot pipe, porosity, and centerline shrinkage; high hydrogen content; nonmetallic inclusions; unmelted electrodes and shelf; and cracks, laminations, seams, pits, blisters, and scabs. The article provides a discussion on the imperfections found in steel forgings. The problems encountered in sheet metal forming are also discussed. The article concludes with information on the causes of failure in cold formed parts.
Book Chapter
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003552
EISBN: 978-1-62708-180-1
...Abstract Abstract This article provides an overview of the classification of hydrogen damage. Some specific types of the damage are hydrogen embrittlement, hydrogen-induced blistering, cracking from precipitation of internal hydrogen, hydrogen attack, and cracking from hydride formation...
Abstract
This article provides an overview of the classification of hydrogen damage. Some specific types of the damage are hydrogen embrittlement, hydrogen-induced blistering, cracking from precipitation of internal hydrogen, hydrogen attack, and cracking from hydride formation. The article focuses on the types of hydrogen embrittlement that occur in all the major commercial metal and alloy systems, including stainless steels, nickel-base alloys, aluminum and aluminum alloys, titanium and titanium alloys, copper and copper alloys, and transition and refractory metals. The specific types of hydrogen embrittlement discussed include internal reversible hydrogen embrittlement, hydrogen environment embrittlement, and hydrogen reaction embrittlement. The article describes preservice and early-service fractures of commodity-grade steel components suspected of hydrogen embrittlement. Some prevention strategies for design and manufacturing problem-induced hydrogen embrittlement are also reviewed.
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006784
EISBN: 978-1-62708-295-2
.... Not relevant for impact-induced cracking Hydrogen-induced blistering Low-strength steels at ambient temperatures Hydrogen forms gas-filled blisters Cracking from precipitation of internal gaseous hydrogen Heavy steel sections Induced by high-temperature exposure followed by rapid cooling Hydrogen...
Abstract
Hydrogen damage is a term used to designate a number of processes in metals by which the load-carrying capacity of the metal is reduced due to the presence of hydrogen. This article introduces the general forms of hydrogen damage and provides an overview of the different types of hydrogen damage in all the major commercial alloy systems. It covers the broader topic of hydrogen damage, which can be quite complex and technical in nature. The article focuses on failure analysis where hydrogen embrittlement of a steel component is suspected. It provides practical advice for the failure analysis practitioner or for someone who is contemplating procurement of a cost-effective failure analysis of commodity-grade components suspected of hydrogen embrittlement. Some prevention strategies for design and manufacturing problem-induced hydrogen embrittlement are also provided.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0091631
EISBN: 978-1-62708-229-7
... of corrosion; however, on one of the sections there was a transverse crack along the edge of a 6.4 mm ( 1 4 in.) diameter pitted area. Two adjacent areas were raised, resembling blisters, and also had transverse cracks along their edges. The cracks were irregular and had penetrated completely through...
Abstract
A steam-condensate line (type 316 stainless steel tubing) began leaking after five to six years in service. The line carried steam condensate at 120 deg C (250 deg F) with a two hour heat-up/cool-down cycle. No chemical treatment had been given to either the condensate or the boiler water. To check for chlorides, the inside of the tubing was rinsed with distilled water, and the rinse water was collected in a clean beaker. A few drops of silver nitrate solution were added to the rinse water, which clouded slightly because of the formation of insoluble silver chloride. This and additional investigation (visual inspection, and 250x micrograph etched with aqua regia) supported the conclusion that the tubing failed by chloride SCC. Chlorides in the steam condensate also caused corrosion of the inner surface of the tubing. Stress was produced when the tubing was bent during installation. Recommendations included providing water treatment to remove chlorides from the system. Continuous flow should be maintained throughout the entire tubing system to prevent concentration of chlorides. No chloride-containing water should be permitted to remain in the system during shutdown periods, and bending of tubing during installation should be avoided to reduce residual stress.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001534
EISBN: 978-1-62708-220-4
... and metallographic evidence clearly indicated that the failure started at the area of lack of penetration in the weld and propagated in a brittle manner. In the crack initiation zone, cracking was intergranular. This region also exhibited blisters around inclusions. Microcracks emanating from inclusion sites...
Abstract
A detailed failure analysis was conducted on an ammonia refrigerant condenser tube component that failed catastrophically during its initial hours of operation. Evidence collected clearly demonstrated that the weld between a pipe and a dished end contained a sharp unfused region at its root (lack of penetration). Component failure had started from this weld defect. The hydrogen absorbed during welding facilitated crack initiation from this weld defect during storage of the component after welding. Poor weld toughness at the low operating temperature facilitated crack growth during startup, culminating in catastrophic failure as soon as the crack exceeded critical length.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001556
EISBN: 978-1-62708-218-1
... between plating and baking were noted to vary from 3 to 11 hours. Fig. 1 Cracking of the eye end portion near the radius, at × 0.75. Macroexamination revealed numerous tiny blisters all over the bright chrome plated piston rod surface. On examination under stereoscopic microscope, fracture...
Abstract
A few Cr-Mo steel piston rods from different production batches were found identically cracked in the eye end near the radius after chrome plating and baking treatment. Two of them cracked in the plating stage itself instantly broke on slight tapping. Cracking initiated from the outer base surface of the forked eye end. The 40 mm diam forged piston rods were subjected to plating after heavy machining on the part without any stress-relieving treatment. Also, time lapses between plating and baking were varied from 3 to 11 h. The brittle cracking along forked eye-end radius portion was attributed to hydrogen embrittlement that occurred during chrome plating.
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006835
EISBN: 978-1-62708-329-4
..., pits, blisters, and scabs Chemical Segregation Ingot Pipe, Porosity, and Centerline Shrinkage High Hydrogen Content Nonmetallic Inclusions Other Ingot-Related Imperfections Primary Reduction Flaws Various terms are used to describe surface and subsurface imperfections in wrought...
Abstract
The primary purpose of this article is to describe general root causes of failure that are associated with wrought metals and metalworking. This includes a brief review of the discontinuities or imperfections that may be common sources of failure-inducing defects in the bulk working of wrought products. The article addresses the types of flaws or defects that can be introduced during the steel forging process itself, including defects originating in the ingot-casting process. Defects found in nonferrous forgings—titanium, aluminum, and copper and copper alloys—also are covered.
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006760
EISBN: 978-1-62708-295-2
... with tungsten inclusion. Kroll’s etch. (b) Energy-dispersive x-ray spectroscopy graph of tungsten inclusion Entrapped hydrogen can expand during subsequent heat treatment, leaving voids (blisters) and distorting the metal ( Fig. 34 ). Fig. 34 (a) Protrusions on machined surface of 2024 aluminum...
Abstract
Visual examination, using the unaided eye or a low-power optical magnifier, is typically one of the first steps in a failure investigation. This article presents the guidelines for selecting samples for scanning electron microscope examination and optical metallography and for cleaning fracture surfaces. It discusses damage characterization of metals, covering various factors that influence the damage, namely stress, aggressive environment, temperature, and discontinuities.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c0048830
EISBN: 978-1-62708-228-0
... small blisters were observed on the inner surface near the weld after attempts had been made to repair the crack. Fig. 1 Vessel made of ASTM A204, grade C, steel that failed as the result of hydrogen embrittlement. (a) Portion of tank; Detail A shows locations of cracks, at welds joining shell...
Abstract
A vessel made of ASTM A204, grade C, molybdenum alloy steel and used as a hydrogen reformer was found to have cracked in the weld between the shell and the lower head. Six samples from different sections were investigated. The crack was found to be initiated at the edge of the weld in the coarsegrain portion of the HAZ. The microstructure was found to be severely embrittled and severely gassed in an area around the crack. The microstructure of the metal in the head was revealed to be banded and contained spheroidal carbides. The lower head was established by hardness values and microscopic examination to have been overheated for a sufficiently long time to reduce the tensile strength below the minimum required for the steel. It was interpreted that the wide difference in tensile strength between head and weld metal (including HAZ) formed a metallurgical notch that enhanced the diffusion of hydrogen into the metal in the cracked region. The resultant embrittlement and associated fissuring was established to have caused the failure. The hydrogen was diffused out by wrapping the vessel in asbestos and heating followed by cooling as prescribed by ASME code.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001548
EISBN: 978-1-62708-219-8
.... Deterioration was in the form of blistering of the surface paint, bubbling and delamination of the aluminum from the plywood, and cracks in the aluminum. All towers exhibited the same phenomena, on both the interior and exterior. The Navy demanded the client take action to repair the damage. At this point...
Abstract
In 1975, a manufacturer was awarded a contract to produce modular air-traffic control towers for the U.S. Navy. The specifications called for painted steel siding, but the manufacturer convinced the Navy to substitute aluminum-bonded-to-plywood panels that were provided by a supplier. In less than one year, the panels began to delaminate and the aluminum began to crack. It was found that the failure was the result of chloride-induced intergranular corrosion caused by chemicals in the adhesive and excessive moisture in the wood introduced during manufacturing.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003540
EISBN: 978-1-62708-180-1
... or blistering. Blistering is most often associated with the melting or heat treatment of aluminum, where reaction with water vapor produces hydrogen. Blistering due to hydrogen is frequently associated with grain-boundary precipitates or the formation of small voids. Blister formation in aluminum is different...
Abstract
This article briefly reviews the various metallurgical or environmental factors that cause a weakening of the grain boundaries and, in turn, influence the occurrence of intergranular (IG) fractures. It discusses the mechanisms of IG fractures, including the dimpled IG fracture, the IG brittle fracture, and the IG fatigue fracture. The article describes some typical embrittlement mechanisms that cause the IG fracture of steels.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001695
EISBN: 978-1-62708-229-7
... is an unpredictable length. There is generally absence of any significant swelling, but occasional bubbles of hydrogen may be evolved, and the pinhole in the aluminum may be discolored by small particles of UO 2 . The propagation stage is characterized by the growth of a blister at the pinhole. Once swelling starts...
Abstract
Large quantities of aluminum-clad spent nuclear materials have been in interim storage in the fuel storage basins at The Savannah River Site while awaiting processing since 1989. This extended storage as a result of a moratorium on processing resulted in corrosion of the aluminum clad. Examinations of this fuel and other data from a corrosion surveillance program in the water basins have provided basic insight into the corrosion process and have resulted in improvements in the storage facilities and basin operations. Since these improvements were implemented, there has been no new initiation of pitting observed since 1993. This paper describes the corrosion of spent fuel and the metallographic examination of Mark 31A target slugs removed from the K-basin storage pool after 5 years of storage. It discusses the SRS Corrosion Surveillance Program and the improvements made to the storage facilities which have mitigated new corrosion in the basins.
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006777
EISBN: 978-1-62708-295-2
... the susceptibility of aluminum to hydrogen damage. Hydrogen damage in aluminum alloys may take the form of IG or transgranular cracking or blistering. Blistering is most often associated with the melting or heat treatment of aluminum, in which reaction with water vapor produces hydrogen. Blistering due to hydrogen...
Abstract
This article briefly reviews the factors that influence the occurrence of intergranular (IG) fractures. Because the appearance of IG fractures is often very similar, the principal focus is placed on the various metallurgical or environmental factors that cause grain boundaries to become the preferred path of crack growth. The article describes in more detail some typical mechanisms that cause IG fracture. It discusses the causes and effects of IG brittle cracking, dimpled IG fracture, IG fatigue, hydrogen embrittlement, and IG stress-corrosion cracking. The article presents a case history on IG fracture of steam generator tubes, where a lowering of the operating temperature was proposed to reduce failures.
Book Chapter
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006804
EISBN: 978-1-62708-329-4
... that is designed and constructed to recognized codes and standards. This standard includes numerous sections on assessment procedures for calculating the impact of damage mechanisms such as general metal loss and local metal loss, blisters and laminations, weld misalignment and shell distortion, cracklike flaws...
Abstract
This article addresses the effects of damage to equipment and structures due to explosions (blast), fire, and heat as well as the methodologies that are used by investigating teams to assess the damage and remaining life of the equipment. It discusses the steps involved in preliminary data collection and preparation. Before discussing the identification, evaluation, and use of explosion damage indicators, the article describes some of the more common events that are considered in incident investigations. The range of scenarios that can occur during explosions and the characteristics of each are also covered. In addition, the article primarily discusses level 1 and level 2 of fire and heat damage assessment and provides information on level 3 assessment.