Skip Nav Destination
Close Modal
By
Christopher A. Walton, Benjamin E. Nesbit, Henrique M. Candia, Zachary A. Myers, Wilburn R. Whittington ...
Search Results for
Aluminum alloy
Update search
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
NARROW
Format
Topics
Book Series
Date
Availability
1-20 of 90 Search Results for
Aluminum alloy
Follow your search
Access your saved searches in your account
Would you like to receive an alert when new items match your search?
Sort by
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001022
EISBN: 978-1-62708-214-3
... Abstract Two complete aircraft undercarriage-leg 2014 aluminum alloy forgings and a number of sectional ends that exhibited cracks during nondestructive testing were examined to determine the extent of damage and the type of cracking. Cracks were primarily confined to the diaphragm and...
Abstract
Two complete aircraft undercarriage-leg 2014 aluminum alloy forgings and a number of sectional ends that exhibited cracks during nondestructive testing were examined to determine the extent of damage and the type of cracking. Cracks were primarily confined to the diaphragm and adjoining wall between the steel sleeve and the steel diaphragm washer. Metallographic analysis and accelerated corrosion tests showed that the cracks had originated as stress-corrosion failures.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001283
EISBN: 978-1-62708-215-0
... (max) Tin 0.0023 0.05 (max) Chromium 0.08 0.2 (max) Aluminum bal bal Fig. 7 X-ray map obtained with an SEM microprobe, showing copper-rich particles in the crack path. The basic cause of random cracking and bursting of the preforged and finish forged parts was the...
Abstract
During the preproduction stages of forging, an initial batch of 50 mm (2 in.) diam Al-4Cu alloy (L77) extruded bar stock material was found to be cracking randomly. Failure analysis was conducted to determine the metallurgical factors underlying the phenomenon. Microexamination of sections across the defects revealed intergranular cracks tracing a path of round, segregated particles and oxide film discontinuities. The segregated particles were rich in copper It was concluded that the cracking was the result of segregations occurring in poor-quality raw material. The source of segregation was suspected to be the use of improperly made master alloys. Use of improved melting techniques and proper master alloys was recommended.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001339
EISBN: 978-1-62708-215-0
... Abstract The failure mode of through-wall cracking of a butt weld in a 5083-O aluminum alloy piping system in an ethylene plant was identified as mercury liquid metal embrittlement. As a result of this finding, 226 of the more than 400 butt welds in the system were ultrasonically inspected for...
Abstract
The failure mode of through-wall cracking of a butt weld in a 5083-O aluminum alloy piping system in an ethylene plant was identified as mercury liquid metal embrittlement. As a result of this finding, 226 of the more than 400 butt welds in the system were ultrasonically inspected for cracking. One additional weld was found that had been degraded by mercury. A welding team experienced in repairing mercury contaminated piping was recruited to make the repairs. Corrective action included the installation of a sulfur-impregnated charcoal mercury-removal bed and replacement of the aluminum equipment that was in operation prior to the installation of the mercury-removal bed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0048095
EISBN: 978-1-62708-224-2
... Abstract The T-section cross member of the lifting sling failed in service while lifting a 966 kg (2130 lb) load. The L-section sling body and the cross member were made of aluminum alloy 5083 or 5086 and were joined by welding using aluminum alloy 4043 filler metal. The fracture was found by...
Abstract
The T-section cross member of the lifting sling failed in service while lifting a 966 kg (2130 lb) load. The L-section sling body and the cross member were made of aluminum alloy 5083 or 5086 and were joined by welding using aluminum alloy 4043 filler metal. The fracture was found by visual examination to have occurred at the weld joining the sling body and the cross member. Inadequate joint penetration and porosity was revealed by macrographic examination of the weld. Lower silicon content and a higher magnesium and manganese content than the normal for alloy 4043 filler metal were found during chemical analysis. It was revealed by examination of the ends of the failed cross member that a rotational force that had been applied on the cross member caused it to fracture near the sling body. It was concluded that brittle fracture at the weld was caused by overloading which was attributed to the misalignment of the sling during loading. Aluminum alloy 5183 or 5356 filler metal was recommended to be used to avoid brittle welds.
Book Chapter
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001781
EISBN: 978-1-62708-241-9
... Abstract A commercial hybrid-iron golf club fractured during normal use. The club fractured through its cast aluminum alloy hosel. Optical analysis revealed casting pores through 20% of the hosel thickness. Mechanical properties were determined from characterization results, then used to...
Abstract
A commercial hybrid-iron golf club fractured during normal use. The club fractured through its cast aluminum alloy hosel. Optical analysis revealed casting pores through 20% of the hosel thickness. Mechanical properties were determined from characterization results, then used to construct a finite element model to analyze material performance under failure conditions. In addition, a full scale structural test was conducted to determine failure strength. It was concluded that the club failed not from ground impact but from a force reversal at the bottom of the downswing. Large moments generated during the downswing aggravated by manufacturing defects and stress concentration combined to create an overload condition.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001124
EISBN: 978-1-62708-214-3
... Abstract Several wires in aluminum conductor cables fractured within 5 to 8 years of, service in Alaskan tundra. The cables were comprised of 19-wire strands; the wires were aluminum alloy 6201-T81. Visual and metallographic examinations of the cold-upset pressure weld joints in the wires...
Abstract
Several wires in aluminum conductor cables fractured within 5 to 8 years of, service in Alaskan tundra. The cables were comprised of 19-wire strands; the wires were aluminum alloy 6201-T81. Visual and metallographic examinations of the cold-upset pressure weld joints in the wires established that the fractures were caused by fatigue loading attributable to wind/thermal factors at the joints. The grain flow at the joints was transverse to the wire axis, rendering the notches of the joints sensitive to fatigue loading. An additional contributory factor was intergranular corrosion, which assisted fatigue crack initiation/propagation. The failure was attributed to the departure of conductor quality from the requirements of ASTM B 398 and B 399, which specify that “no joints shall be made during final drawing or in the finished wire” and that the joints should not be closer than 15 m (50 ft). The failed cable did not meet either criterion. It was recommended that the replacement cable be inspected for strict compliance to ASTM requirements.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001125
EISBN: 978-1-62708-214-3
... Abstract An 1100 aluminum alloy connector of a high-tension aluminum conductor steel-reinforced (ACSR) transmission cable failed after more than 20 years in service, in a region of consider able industrial pollution. The steel core was spliced with a galvanized 1020 carbon steel sheath. Visual...
Abstract
An 1100 aluminum alloy connector of a high-tension aluminum conductor steel-reinforced (ACSR) transmission cable failed after more than 20 years in service, in a region of consider able industrial pollution. The steel core was spliced with a galvanized 1020 carbon steel sheath. Visual examination showed that the connector had undergone considerable plastic deformation and necking before fracture. The steel sheath was severely corroded, and the steel splice was pressed off-center in the axial direction inside the connector. Examination of the fracture surface and micro-structural analysis indicated that the failure was caused by mechanical overload, which occurred because of weakening of the steel support cable by corrosion inside the fitting. The corrosion was ascribed to defective assembly of the connector which allowed moisture penetration.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001029
EISBN: 978-1-62708-214-3
... Abstract Two investment-cast A356 aluminum alloy actuators used for handles on passenger doors of commercial aircraft fractured during torquing at less than the design load. Visual examination showed that cracking had occurred through a machined side hole. Fractography revealed that the cracks...
Abstract
Two investment-cast A356 aluminum alloy actuators used for handles on passenger doors of commercial aircraft fractured during torquing at less than the design load. Visual examination showed that cracking had occurred through a machined side hole. Fractography revealed that the cracks originated in hot tear locations in the castings. Microprobe analysis of fracture surfaces in the hot tear region indicated a much higher silicon-to-aluminum ratio compared with the overload fracture area. No microstructural anomalies related to the failure were found during metallographic examination. It was concluded that the strength of the castings had been compromised by the presence of the casting defects. Modification of the gating system for casting was recommended to eliminate the hot tear zone. It was also suggested that the balance of the castings from the same manufacturing lot be radiographically inspected.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001366
EISBN: 978-1-62708-215-0
... Abstract An AMS 4126 (7075-T6) aluminum alloy impeller from a radial inflow turbine fractured during commissioning. Initial examination showed that two adjacent vanes had fractured through airfoils in the vicinity of the vane leading edges, and one vane fractured through an airfoil near the hub...
Abstract
An AMS 4126 (7075-T6) aluminum alloy impeller from a radial inflow turbine fractured during commissioning. Initial examination showed that two adjacent vanes had fractured through airfoils in the vicinity of the vane leading edges, and one vane fractured through an airfoil near the hub in the vicinity of the vane trailing edge. Some remaining vanes exhibited radial and transverse cracks in similar locations. Binocular and scanning electron microscope examinations showed that the cracks had been caused by high-cycle fatigue and had progressed from multiple origins on the vane surface. Structural analysis indicated that the fatigue loading probably had been caused by forced excitation, resulting in the impeller vibrating at its resonant frequency. It was recommended that the impeller design, control systems, and material of construction be changed.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001123
EISBN: 978-1-62708-214-3
... environment in a coastal area. It was recommended that proper chemical analysis of the zinc-aluminum alloy be carried out as a quality control procedure. Die castings Marine environments Zamak 3 Intergranular corrosion Intergranular fracture Extensive cracking was found in a batch of...
Abstract
Extensive cracking was found in a batch of die-cast ZAMAK 3 solenoid valve seats during commissioning of the system in which they were installed. Scanning electron microscopic and chemical analyses conducted on one of the failed valve seats showed that the composition of the alloy was different from that specified. The presence of excess aluminum and lead impurities that had segregated to the grain boundaries, coupled with an inadequate amount of magnesium, resulted in intergranular corrosion and subsequent intergranular failure. Corrosion was accelerated by storage in a humid environment in a coastal area. It was recommended that proper chemical analysis of the zinc-aluminum alloy be carried out as a quality control procedure.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001024
EISBN: 978-1-62708-214-3
... 6061-T651 aluminum alloy extrusion and 26 fiberglass “pockets” that provided the trailing-edge airfoil shape. Visual examination of the fracture surface of the aluminum extrusion indicated fatigue crack growth followed by ductile overload separation. Examination of the fatigue fracture region revealed...
Abstract
A Marine Corps helicopter crash was investigated. Efforts were directed to the failure of one of the main rotor blades that had apparently separated in the air. The apparent failure of a blade integrity monitor (BIM) system was also considered. The rotor blade comprised a long, hollow 6061-T651 aluminum alloy extrusion and 26 fiberglass “pockets” that provided the trailing-edge airfoil shape. Visual examination of the fracture surface of the aluminum extrusion indicated fatigue crack growth followed by ductile overload separation. Examination of the fatigue fracture region revealed several pits that appeared to have acted as fracture origin sites. Time to failure was determined using fracture mechanics. It was concluded that failure was caused by a fatigue crack that grew to critical length without detection. The crack originated at pits that resulted from the use of an improperly designed heating element used to cure fiberglass repairs.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001297
EISBN: 978-1-62708-215-0
... Abstract A helicopter tail rotor blade spar failed in fatigue, allowing the blade to separate during flight. The 2014-T652 aluminum alloy blade had a hollow spar shank filled with lead wool ballast and a thermoset polymeric seal. A corrosion pit was present at the origin of the fatigue zone and...
Abstract
A helicopter tail rotor blade spar failed in fatigue, allowing the blade to separate during flight. The 2014-T652 aluminum alloy blade had a hollow spar shank filled with lead wool ballast and a thermoset polymeric seal. A corrosion pit was present at the origin of the fatigue zone and numerous trails of corrosion pits were located on the spar cavity's inner surfaces. The corrosion pitting resulted from the failure of the thermoset seal in the spar shank cavity. The seal failure allowed moisture to enter into the cavity. The moisture then served as an electrolyte for galvanic corrosion between the lead wool ballast and the aluminum spar inner surface. The pitting initiated fatigue cracking which led to the spar failure.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001812
EISBN: 978-1-62708-241-9
... Abstract Several cases of embrittlement failure are analyzed, including liquid-metal embrittlement (LME) of an aluminum alloy pipe in a natural gas plant, solid metal-induced embrittlement (SMIE) of a brass valve in an aircraft engine oil cooler, LME of a cadmium-plated steel screw from a...
Abstract
Several cases of embrittlement failure are analyzed, including liquid-metal embrittlement (LME) of an aluminum alloy pipe in a natural gas plant, solid metal-induced embrittlement (SMIE) of a brass valve in an aircraft engine oil cooler, LME of a cadmium-plated steel screw from a crashed helicopter, and LME of a steel gear by a copper alloy from an overheated bearing. The case histories illustrate how LME and SMIE failures can be diagnosed and distinguished from other failure modes, and shed light on the underlying causes of failure and how they might be prevented. The application of LME as a failure analysis tool is also discussed.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001303
EISBN: 978-1-62708-215-0
... Abstract A sand-cast LM6M aluminum alloy sprocket drive wheel in an all-terrain vehicle failed. Extensive cracking had occurred around each of the six bolt holes in the wheel. Evidence of considerable deformation in this area was also noted. Examination indicated that the part failed because of...
Abstract
A sand-cast LM6M aluminum alloy sprocket drive wheel in an all-terrain vehicle failed. Extensive cracking had occurred around each of the six bolt holes in the wheel. Evidence of considerable deformation in this area was also noted. Examination indicated that the part failed because of gross overload. Use of an alloy with a much higher yield strength and improvement in design were recommended.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001021
EISBN: 978-1-62708-214-3
... Abstract Following the crash of a Mirage III-0 aircraft (apparently caused by engine failure), a small crack was detected in a bolt hole in the wing main spar (AU4SG aluminum alloy). Because this area was considered to be critical to aircraft safety and similar cracking was found in other spars...
Abstract
Following the crash of a Mirage III-0 aircraft (apparently caused by engine failure), a small crack was detected in a bolt hole in the wing main spar (AU4SG aluminum alloy). Because this area was considered to be critical to aircraft safety and similar cracking was found in other spars in service, the Royal Australian Air Force requested that the crack growth rate during service be determined. The loading history of the aircraft was made available in the form of flight by-flight records of the counts from the vertical accelerometer sensors fitted to the airframe and a series of “overstress” events recorded during the life of the aircraft. The bolt hole was examined by eddy current testing, visual examination, high-powered light microscope, and scanning electron microscope. Simulation tests were also conducted. The use of simulation specimens permitted actual crack growth rate data to be determined for the configuration of interest.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001025
EISBN: 978-1-62708-214-3
... Abstract A piece of wheel flange separated from the main landing gear wheel of a C130 aircraft as it taxied on a runway. The wheel was a 2014-T61 aluminum alloy forging and had been in service nearly 20 years. Fractographic evidence indicated that the initial crack growth was caused by high...
Abstract
A piece of wheel flange separated from the main landing gear wheel of a C130 aircraft as it taxied on a runway. The wheel was a 2014-T61 aluminum alloy forging and had been in service nearly 20 years. Fractographic evidence indicated that the initial crack growth was caused by high-cycle fatigue. The crack grew to approximately 8 in. in length before final catastrophic fracture. Fatigue analyses accurately predicted the cyclic life demonstrated by the failed wheel since its last inspection, assuming an initial crack length of 13 to 25 mm (0.5 to 1.0 in.). It was recommended that the inspection interval be reduced to one-third of its original duration for the current level of inspection reliability, or that inspection procedures be improved in order that cracks substantially smaller than 13 mm (0.5 in.) can be reliably detected.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001290
EISBN: 978-1-62708-215-0
... aircraft. Fractographic and surface examination of metal fragments (stainless steel and aluminum alloy) from damaged areas indicated that the accident was caused by an explosion in the front toilet. A reconstruction exercise confirmed this conclusion. Damage to the undercarriage and underside resulted from...
Abstract
Damage to a passenger aircraft that resulted from a midair explosion and subsequent emergency landing was investigated to determine the cause and location of the explosion. Extensive damage had occurred in the front toilet and cockpit areas and to the undercarriage and underside of the aircraft. Fractographic and surface examination of metal fragments (stainless steel and aluminum alloy) from damaged areas indicated that the accident was caused by an explosion in the front toilet. A reconstruction exercise confirmed this conclusion. Damage to the undercarriage and underside resulted from the emergency landing.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001292
EISBN: 978-1-62708-215-0
... Abstract A crack was detected in one arm of the right-hand horizontal brace of the nose landing gear shock strut from a large military aircraft. The shock strut was manufactured from a 7049 aluminum alloy forging in the shape of a delta. A laboratory investigation was conducted to determine the...
Abstract
A crack was detected in one arm of the right-hand horizontal brace of the nose landing gear shock strut from a large military aircraft. The shock strut was manufactured from a 7049 aluminum alloy forging in the shape of a delta. A laboratory investigation was conducted to determine the cause of failure. It was concluded that the arm failed because of the presence of an initial defect that led to the initiation of fatigue cracking. The fatigue cracking grew in service until the part failed by overload. The initial defect was probably caused during manufacture. Fleet-wide inspection of the struts was recommended.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001298
EISBN: 978-1-62708-215-0
... Abstract A helicopter tail rotor blade spar failed in fatigue, allowing the outer section of the blade to separate in flight. The 7075-T7351 aluminum alloy blade had fiberglass pockets. The blade spar was a hollow “D” shape, and corrosion pits were present on the inner surface of the hollow...
Abstract
A helicopter tail rotor blade spar failed in fatigue, allowing the outer section of the blade to separate in flight. The 7075-T7351 aluminum alloy blade had fiberglass pockets. The blade spar was a hollow “D” shape, and corrosion pits were present on the inner surface of the hollow spar A single corrosion pit, 0.38 mm (0.015 in.) deep, led to a fatigue failure of the spar The failure initiated on the pylon side of the blade. Dimensional analysis of the spar near the failure revealed measurements within engineering drawing tolerances. Though corrosion pitting was present, there was an absence of significant amounts of corrosion product and all of the pits were filled with corrosion-preventative primer. This indicated that the pitting occurred during spar manufacture, prior to the application of the primer The pitting resulted from multiple nickel plating and defective plating removal by acid etching. Post-plating baking operations subsequently reduced the fatigue strength of the spar.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001695
EISBN: 978-1-62708-229-7
... storage for up to 8 years. 1 The spent nuclear fuel is primarily irradiated uranium-aluminum alloy or depleted uranium metal fuel clad with a 30-mil type 1100 or 8001 aluminum alloy. After about two years of storage, visible corrosion product was evident on the depleted uranium metal Mk-31A target...
Abstract
Large quantities of aluminum-clad spent nuclear materials have been in interim storage in the fuel storage basins at The Savannah River Site while awaiting processing since 1989. This extended storage as a result of a moratorium on processing resulted in corrosion of the aluminum clad. Examinations of this fuel and other data from a corrosion surveillance program in the water basins have provided basic insight into the corrosion process and have resulted in improvements in the storage facilities and basin operations. Since these improvements were implemented, there has been no new initiation of pitting observed since 1993. This paper describes the corrosion of spent fuel and the metallographic examination of Mark 31A target slugs removed from the K-basin storage pool after 5 years of storage. It discusses the SRS Corrosion Surveillance Program and the improvements made to the storage facilities which have mitigated new corrosion in the basins.