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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001019
EISBN: 978-1-62708-217-4
... Abstract A broken aircraft crankshaft and a severely damaged main brass bearing were examined to determine whether engine failure was initiated in the bearing or in the crankshaft. The steel crankshaft failure was a classical fatigue fracture. The bearing had been subjected to extremely high...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001743
EISBN: 978-1-62708-217-4
... Abstract Cylinder fatigue can result from abnormal heating in service. Fatigue can be experienced also by piston heads, exhaust valves, and turbosupercharger housings (castings). Pistons from different engines series can sometimes fit, but because of slight design modifications, they may...
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001081
EISBN: 978-1-62708-214-3
... Abstract Several compressor disks in military fighter and trainer aircraft gas turbine engines cracked prematurely in the bolt hole regions. The disks were made of precipitation-hardened AM355 martensitic stainless steel. Experimental and analytical work was performed on specimens from...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001752
EISBN: 978-1-62708-241-9
... crankshafts failed within 15 h to 1,254 h of service after being installed in six-cylinder reciprocating engines of airplanes. After the aircraft engine manufacturer analyzed this problem, the Federal Aviation Agency (FAA) approved the manufacturer’s issue of Mandatory Service Bulletin 00-5 (MSB 00-5) [ 1...
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Published: 01 June 2019
Fig. 1 Cast stainless steel fuel-control lever that failed when the aircraft engine in which it was mounted experienced excessive vibration. (a) Configuration and dimensions (given in inches). (b) View of a fracture surface; arrow indicates region of fracture origin More
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Published: 01 June 2019
Fig. 1 Fractures in aluminum alloy aircraft-engine oil-line elbows caused by poor welding practice. (a) Fracture of gas tungsten arc weld joining threaded boss to oil-line elbow showing lack of penetration through the surface of the V-notch and cracks at both sides of the apex of the notch. (b More
Image
Published: 01 June 2019
Fig. 1 Forged 4337 steel master connecting rod for a reciprocating aircraft engine that failed by fatigue cracking in the bore section between the flanges. (a) Configuration and dimensions (given in inches). (b) Fractograph showing inclusions (arrows) and fatigue beach marks More
Image
Published: 01 January 2002
Fig. 25 Forged 4337 steel master connecting rod for a reciprocating aircraft engine that failed by fatigue cracking in the bore section between the flanges. (a) Configuration and dimensions (given in inches). (b) Fractograph showing inclusions (arrows) and fatigue beach marks More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001552
EISBN: 978-1-62708-217-4
... generation which induced grinding cracks and grinding burn. Tensional stresses resulting from grinding developed in a thin surface layer. On another crankshaft, chromium plating introduced undesirable residual tensile stresses. Such plating is an unsatisfactory finish for crankshafts of aircraft engines...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001734
EISBN: 978-1-62708-234-1
... Abstract An aircraft engine in which an in-flight fire had occurred was dismantled and examined. A bracket assembly fabricated from 2024 aluminum, one of several failed components, was of prime interest because of apparent heat damage. Scanning electron microscopy was used to compare laboratory...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047598
EISBN: 978-1-62708-217-4
... Abstract Two aircraft-engine tailpipes of 19-9 DL stainless steel (AISI type 651) developed cracks along longitudinal gas tungsten arc butt welds after being in service for more than 1000 h. Binocular-microscope examination of the cracks in both tailpipes revealed granular, brittle-appearing...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001507
EISBN: 978-1-62708-217-4
... Abstract A large four-engine aircraft was on a cargo flight at night when a loud bang was heard, accompanied by a loss of power from both engines on the left side. After an emergency landing, it was discovered that the propellers from both left side engines were missing. The initial...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047072
EISBN: 978-1-62708-217-4
... Abstract Postflight inspection of a gas-turbine aircraft engine that had experienced compressor stall revealed that the engine air-intake bullet assembly had dislodged and was seated against the engine-inlet guide vanes at the 3 o'clock position. The bullet assembly consisted of an outer...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0048257
EISBN: 978-1-62708-217-4
... Abstract Evidence of destructive pitting on the gear teeth (AMS 6263 steel) in the area of the pitchline was exhibited by an idler gear for the generator drive of an aircraft engine following test-stand engine testing. The case hardness was investigated to be lower than specified...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0046142
EISBN: 978-1-62708-217-4
... Abstract To ensure no malfunctions and although there were no apparent problems, a main fuel control was returned to the factory for examination after service on a test aircraft engine that had experienced high vibrations. When the fuel control was disassembled, a lever, cast from AMS 5350...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047541
EISBN: 978-1-62708-217-4
... Abstract A throttle arm of an aircraft engine fractured and caused loss of engine control. The broken part consisted of a 6.4-mm (1/4-in.) diam medium-carbon steel rod with a thread to fit a knurled brass nut that was inserted into the throttle knob. The threaded rod had been welded...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047176
EISBN: 978-1-62708-235-8
... Abstract A ring clamp (8740 (AMS 6322), steel forged and cadmium plated) used for attaching ducts to an aircraft engine became loose after three hours of service. When the clamp was removed from the engine, the hinge tabs on one clamp half were found to be broken. Analysis (visual inspection...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047059
EISBN: 978-1-62708-217-4
... Abstract The governor on an aircraft engine failed and upon disassembly of the unit, it was discovered that the retainer for the flyweight pivot pins was broken. The channel-shaped retainer was made of 0.8 mm (0.030 in.) thick 1018 or 1020 steel. The part was plated with copper, which acted...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047636
EISBN: 978-1-62708-217-4
... Abstract Several elbow subassemblies comprising segments of oil-line assemblies that recycled aircraft-engine oil from pump to filter broke in service. The components of the subassemblies were made of aluminum alloy 6061-T6. Two subassemblies were returned to the laboratory to determine cause...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0089563
EISBN: 978-1-62708-217-4
... Abstract A lever (machined from a casting made of AISI type 410 stainless steel, then surface hardened by nitriding) that was a component of the main fuel-control linkage of an aircraft engine fractured in flight after a service life of less than 50 h. Investigation (radiographic inspection...