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4140
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0048082
EISBN: 978-1-62708-221-1
... Abstract The horizontal cross-travel shaft on a derrick failed after two years of service. The shaft was required to be made of 4140 steel quenched to a hardness of 302 to 352 HRB. The shaft was found to have fractured approximately 13 mm from the change in section between the splined end...
Abstract
The horizontal cross-travel shaft on a derrick failed after two years of service. The shaft was required to be made of 4140 steel quenched to a hardness of 302 to 352 HRB. The shaft was found to have fractured approximately 13 mm from the change in section between the splined end and the shaft proper. The cracks were found to have propagated in the longitudinal and transverse directions until failures occurred. It was showed by a transverse section through the spline that the longitudinal cracks were initiated at the sharp corners at the roots of the spline teeth. The shaft was subjected to reverse torsional loading by the operation of the derrick and the shaft fatigue fracture was caused by this. The fillets at the roots of the spline teeth were increased in size and polished to minimize stress concentrations in these areas.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047105
EISBN: 978-1-62708-225-9
... forcefully in the direction of the load, causing substantial damage to other machinery components in the vicinity. The failed component, which was 43 cm (17 in.) in diameter, was machined from 4140 plate and heat treated to 34 to 36 HRC. Analysis (visual inspection, composite micrographs, scanning electron...
Abstract
The locking collar on a machine failed suddenly when the shaft it restrained was inadvertently subjected to an axial load slightly higher than the allowable working load. The locking collar fractured abruptly, producing four large fragments. This allowed the shaft to be propelled forcefully in the direction of the load, causing substantial damage to other machinery components in the vicinity. The failed component, which was 43 cm (17 in.) in diameter, was machined from 4140 plate and heat treated to 34 to 36 HRC. Analysis (visual inspection, composite micrographs, scanning electron microscopy, and mechanical-property analysis) supported the conclusions that the alloy steel plate used in this application contained significant brittle microstructural fibering or banding. This condition produced considerable anisotropy in ductility and toughness as revealed by mechanical testing. Unfortunately, the potential effects of anisotropy were apparently neglected when this component was designed and manufactured from the plate stock, because the loading was applied in a direction that stressed the weakest planes in the material, that is, a direction normal to the fibering. No recommendations were made.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0046057
EISBN: 978-1-62708-225-9
... Abstract After less than 30 days in service, several cadmium-plated retaining rings, made of 4140 steel tubing and heat treated to 36 to 40 HRC, broke during operation that included holding components of a segmented fitting in place under a constant load. Photographic and 100x nital-etched...
Abstract
After less than 30 days in service, several cadmium-plated retaining rings, made of 4140 steel tubing and heat treated to 36 to 40 HRC, broke during operation that included holding components of a segmented fitting in place under a constant load. Photographic and 100x nital-etched micrographic examination showed a microstructure of tempered martensite with low inclusion content as well as a pit or burned spot on the outer area of the ring. The defect was approximately 0.18 mm (0.007 in.) deep and 0.5 mm (0.020 in.) in diam and had a hardness of 58 to 60 HRC. The base metal adjacent to the defect had a hardness of 36 to 40 HRC. Small cracks or fissures were also evident within the defect. Thus, the rings failed in brittle fracture as the result of an arc strike (or burn) on the surface of the ring. At the site of the arc strike, a small region of hard, brittle untempered martensite was formed as the result of an arc strike during the cadmium-plating operation. Fracture occurred readily when the ring was stressed. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0046388
EISBN: 978-1-62708-224-2
... Abstract The bolt in a bolt and thimble assembly used to connect a wire rope to a crane hanger bracket was worn excessively. Two worn bolts, one new bolt, and a new thimble were examined. Specifications required the bolts to be made of 4140 steel heat treated to a hardness of 277 to 321 HRB...
Abstract
The bolt in a bolt and thimble assembly used to connect a wire rope to a crane hanger bracket was worn excessively. Two worn bolts, one new bolt, and a new thimble were examined. Specifications required the bolts to be made of 4140 steel heat treated to a hardness of 277 to 321 HRB. Thimbles were to be made of cast 8625 steel, but no heat treatment or hardness were specified. Analysis (visual inspection, hardness testing, and metallographic examination) supported the conclusion that the wear was due to strikingly difference hardness measurements in the bolt and thimble. Recommendations included hardening and tempering the bolts to the hardness range of 375 to 430 HRB. The thimbles should be heat treated to a similar microstructure and the same hardness range as those of the bolt. Molybdenum disulfide lubricant can be liberally applied during the initial installation of the bolts. A maintenance lubrication program was not suggested, but galling could be reduced by periodic application of a solid lubricant.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047830
EISBN: 978-1-62708-235-8
... Abstract Textile-machine crankshafts forged from 4140 steel fractured transversely on one cheek during one to three years of service. The cause of failure for two forgings (one complete fractured forging and second a section that contained the shorter shaft fracture cheek) was determined...
Abstract
Textile-machine crankshafts forged from 4140 steel fractured transversely on one cheek during one to three years of service. The cause of failure for two forgings (one complete fractured forging and second a section that contained the shorter shaft fracture cheek) was determined. Indication of fatigue failure was revealed by visual examination of the fracture surfaces. Rough grooves from hot trimming of the flash were visible on the surface of the cheeks. The outer face of one cheek of the throw on the forging contained shallow surface folds. Slightly decarburized forged surface was identified around one of the folds and a fatigue crack initiated in the fold and propagated across the cheek. Properties representative of 4140 steel, quenched and tempered to a hardness of 20 to 22 HRC, were observed. Tempered bainite was revealed in the general microstructure. As a corrective measure, the forgings were normalized, hardened and tempered to 28 to 32 HRC before being machined to increase fatigue strength and extremely rough surfaces were removed by careful grinding.
Image
in Fracture of an Accumulator Ring Due to Hydrogen Embrittlement
> ASM Failure Analysis Case Histories: Processing Errors and Defects
Published: 01 June 2019
Fig. 1 Hydrogen-embrittlement fracture in a cadmium-plated 4140 steel forged accumulator ring. (a) Ring segment showing a fine crack (arrow). (b) Electron fractograph showing the predominantly intergranular fracture. 7800×
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Image
in Fatigue Fracture of a 4140 Steel Forged Crankshaft Resulting From Stress Raisers Created During Hot Trimming
> ASM Failure Analysis Case Histories: Processing Errors and Defects
Published: 01 June 2019
Fig. 1 Forged 4140 steel textile-machine crankshaft that fractured in fatigue originating at machining marks and forging defects. (a) Configuration and dimensions (given in inches). (b) Fracture surface. (c) Hot trim marks. (d) Snag grinding marks. (e) Hot folds. (f) Section through a hot fold
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Image
in Fatigue Fracture of a 4140 Steel Cross-Travel Shaft
> ASM Failure Analysis Case Histories: Construction, Mining, and Agricultural Equipment
Published: 01 June 2019
Fig. 1 4140 steel cross-travel shaft that failed in service. (a) Broken end of the shaft from a derrick showing the star-type fracture that results from reversed torsional loading. (b) Transverse section through the spline showing cracks initiated at sharp corners at the roots of the spline
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Image
in Deformation of a Gas-Nitrided Drive-Gear Assembly
> ASM Failure Analysis Case Histories: Construction, Mining, and Agricultural Equipment
Published: 01 June 2019
Fig. 1 Gas-nitrided 4140 steel (27–31 HRC) drive-gear assembly in which gear teeth deformed because of faulty design and low core hardness. Details A and B show deformed areas on drive-gear teeth and mating internal splines. Dimensions given in inches
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Image
in Fretting of Freon-Compressor Shaft because of a Loose Bearing
> ASM Failure Analysis Case Histories: Improper Maintenance, Repair, and Operating Conditions
Published: 01 June 2019
Fig. 1 Freon-compressor shaft of 4140 steel that failed by fretting corrosion in the bearing area (Example 2). (a) Shaft and bearing assembly. (b) Failed region of shaft, at 2×, showing disturbed metal and partly closed keyway. (c) Shaft side of bearing inner ring, at 3×, showing pitting
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in Bearing Failure Caused by Improper Heat Treatment of Outer-Ring Raceway
> ASM Failure Analysis Case Histories: Mechanical and Machine Components
Published: 01 June 2019
Fig. 1 Large-diameter 4140 steel radar-antenna bearing that failed because of improper heat treatment of outer-ring raceway. (a) Configuration and dimensions (given in inches). (b) Fractograph showing typical damage on outer-ring raceway. (c) Micrograph of section through metal in outer ring
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Image
in Brittle Failure of Locking Collar Produced From Rolled 4140 Grade Steel Plate
> ASM Failure Analysis Case Histories: Mechanical and Machine Components
Published: 01 June 2019
Fig. 1 Failure of a 4140 steel locking collar machined from rolled plate. (a) Collar assembly showing fracture location. (b) Illustration of the failure with respect to the plate orientation. (c) SEM micrograph showing the cleavage-failure mode. (d) Composite micrograph showing microstructural
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Image
in Brittle Fracture of a Cadmium-Plated 4140 Steel Retaining Ring at a Hard Spot Caused by an Arc Strike
> ASM Failure Analysis Case Histories: Mechanical and Machine Components
Published: 01 June 2019
Fig. 1 Retaining ring of cadmium-plated 4140 steel that failed by brittle fracture at a hard spot caused by an arc strike during plating. (a) View of retaining ring, and section showing location of arc strike. Dimensions given in inches. (b) Photograph of the retaining ring showing pit
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Image
Published: 01 June 2019
Fig. 1 4140 steel slat track from a military aircraft wing. The track bent because one end did not become fully austenitic during heat treatment, producing a low-strength structure of ferrite and tempered martensite.
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c0047181
EISBN: 978-1-62708-233-4
... Abstract Hydraulic cylinder housings were being fabricated from 4140 grade seamless steel tubing. During production, magnetic-particle inspection indicated the presence of circumferential and longitudinal cracks in a large number of cylinders. Analysis (visual inspection, dye penetrant...
Abstract
Hydraulic cylinder housings were being fabricated from 4140 grade seamless steel tubing. During production, magnetic-particle inspection indicated the presence of circumferential and longitudinal cracks in a large number of cylinders. Analysis (visual inspection, dye penetrant inspection, 50x/90x/400x SEM micrographs, and metallographic analysis) supports the conclusion that the cracking problem in these components was identified as quench cracks due to their brittle, intergranular nature and the characteristic temper oxide on the fracture surfaces. Although the steel met the compositional requirements of SAE 4140, the sulfur level was 0.022% and would account for the formation of the sulfide stringers observed. Apparently, the combination of the clustered, stringer-type inclusions and the quenching conditions were too severe for this component geometry. The result was a high incidence of quench cracks that rendered the parts useless. Recommendations included changing the specification, requiring the steel to have lower sulfur concentrations. Magnetic-particle cleanliness standards should be imposed that will exclude material with harmful clusters of sulfide stringers, for example, modified AMS 2301.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0092155
EISBN: 978-1-62708-221-1
... and the adjacent splined coupling sleeve. Specifications included that the gear and coupling be made from 4140 steel bar oil quenched and tempered to a hardness of 265 to 290 HB (equivalent to 27 to 31 HRC) and that the finish-machined parts be single-stage gas nitrided to produce a total case depth of 0.5 mm...
Abstract
Component slippage in the left-side final drive train of a tracked military vehicle was detected after the vehicle had been driven 13,700 km (8500 miles) in combined highway and rough-terrain service. The slipping was traced to the mating surfaces of the final drive gear and the adjacent splined coupling sleeve. Specifications included that the gear and coupling be made from 4140 steel bar oil quenched and tempered to a hardness of 265 to 290 HB (equivalent to 27 to 31 HRC) and that the finish-machined parts be single-stage gas nitrided to produce a total case depth of 0.5 mm (0.020 in.) and a minimum surface hardness equivalent to 58 HRC. Investigation (visual inspection, low-magnification images, 500X images of polished sections etched in 2% nital, spectrographic analysis, and hardness testing) supported the conclusion that the failure occurred by crushing, or cracking, of the case as a result of several factors. Recommendations included reducing the high local stresses at the pitch line to an acceptable level with a design modification. Also suggested was specification of a core hardness of 35 to 40 HRC to provide adequate support for the case and to permit attainment of the specified surface hardness of 58 HRC.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0048077
EISBN: 978-1-62708-221-1
... examination. The shaft was identified by chemical analysis to be 1040 steel (hardness 170 HRB) which was concluded to have insufficient fatigue strength. The step at the base of the fillet was revealed as the point of initiation of the fatigue crack. Shaft material was changed to 4140 steel oil-quenched...
Abstract
The 14-cm diam main hoist shaft of a mobile shovel was found to have multiple crack indications when ultrasonically inspected in the field. A crack around the entire circumference at the change in section was revealed by magnetic-particle inspection of the shaft. The crack was found to coincide with the junction of the fillet and the smaller diam at this change in section. A slight step in the continuity of the fillet and some machining marks were noted at this junction. A fine crack extending 2.5 mm from the surface and originating at the machining marks was revealed by microscopic examination. The shaft was identified by chemical analysis to be 1040 steel (hardness 170 HRB) which was concluded to have insufficient fatigue strength. The step at the base of the fillet was revealed as the point of initiation of the fatigue crack. Shaft material was changed to 4140 steel oil-quenched and tempered to a hardness of 302 to 352 HRB and all machining discontinuities were removed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047991
EISBN: 978-1-62708-225-9
... Abstract Deformation, surface cracking, and spalling on the raceway of the outer ring (made of 4140 steel) of a large bearing caused it to be replaced from a radar antenna. The raceway surfaces were to be flame hardened to 55 HRC minimum and 50 HRC 3.2 mm below the surface, according...
Abstract
Deformation, surface cracking, and spalling on the raceway of the outer ring (made of 4140 steel) of a large bearing caused it to be replaced from a radar antenna. The raceway surfaces were to be flame hardened to 55 HRC minimum and 50 HRC 3.2 mm below the surface, according to specifications. Samples from both the inner and outer rings were examined. A much lower hardness (25.2 to 18.9 HRC) was indicated during a vertical traverse 4.1 cm from the outer surface of the outer ring while slightly lower hardness values (46.8 to 54.8 HRC) were seen on the hardness traverse on the inner ring raceway. The lower hardness values were attributed to improper flame hardening. It was confirmed by metallographic examination of a 3% nital etched sample that the inner ring (tempered martensite and ferrite) and the outer ring (ferrite, scattered patches of pearlite, and martensite) were not properly austenitized. Displacement of metal on the outer raceway was revealed by elongation of grain structure. It was concluded that the failure of the raceway surface was due to incomplete austenitization caused by the improper heat treatment during flame hardening process.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0045992
EISBN: 978-1-62708-225-9
... instead of the specified 55 to 60 HRC. Thus, the poppet failed by brittle fracture, and cracking occurred across nonmetallic inclusions. Recommendation was to redesign the valve with the poppet material changed to 4140 steel, hardened, and tempered to 50 to 55 HRC. Hardness Nonmetallic inclusions...
Abstract
After two weeks of operation, a poppet used in a check valve to control fluid flow and with a maximum operating pressure of 24 MPa (3.5 ksi) failed during operation. Specifications required that the part be made of 1213 or 1215 rephosphorized and resulfurized steel. The poppet was specified to be case hardened to 55 to 60 HRC, with a case depth of 0.6 to 0.9 mm (0.025 to 0.035 in.); the hardness of the mating valve seat was 40 HRC. Analysis showed that the fracture occurred through two 8 mm (0.313 in.) diam holes at the narrowest section of the poppet. The valve continued to operate after it broke, which resulted in extensive loss of metal between the holes. 80x micrograph and 4x macrograph of a 5% nital etched longitudinal section, and chemical analyses showed the poppet did fit 1213 or 1215 specs. However, hardness measurements showed surface hardness was excessive-61 to 65 HRC instead of the specified 55 to 60 HRC. Thus, the poppet failed by brittle fracture, and cracking occurred across nonmetallic inclusions. Recommendation was to redesign the valve with the poppet material changed to 4140 steel, hardened, and tempered to 50 to 55 HRC.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0048073
EISBN: 978-1-62708-224-2
... confirmed failure of the shaft by fatigue fracture. As a corrective measure the shaft was replaced with one made of 4140 steel, quenched and tempered to a hardness of 286 to 319 HRB. The keyway was moved away from the change in section and was machined with a 1.6-mm radius in the bottom corners and a larger...
Abstract
A drum pinion shaft (1030 steel) which was part of the hoisting gear of a crane (capacity 18,140-kg) operating in a blooming mill failed while lifting a 9070 kg load. Chatter marks, rough-machining marks, and sharp corner radii were revealed in the keyway which extended into a shoulder at a change in diam. A circular recess below the keyway surface was revealed at each end of the keyway. A sharp corner at the end of the keyway was revealed by examination to be the origin of fracture. Beach marks were found radiating from the origin over a large portion of the fracture surface which confirmed failure of the shaft by fatigue fracture. As a corrective measure the shaft was replaced with one made of 4140 steel, quenched and tempered to a hardness of 286 to 319 HRB. The keyway was moved away from the change in section and was machined with a 1.6-mm radius in the bottom corners and a larger-radius fillet was machined at the change in section.
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