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18-8
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001237
EISBN: 978-1-62708-220-4
... Abstract A welded vessel made of acid resistant 18-8 steel used in a derusting operation started to leak after a long period due to the formation of cracks. The vessel was heated from the outside and did not come into direct contact with the flame. It was surrounded by a casing of unalloyed...
Abstract
A welded vessel made of acid resistant 18-8 steel used in a derusting operation started to leak after a long period due to the formation of cracks. The vessel was heated from the outside and did not come into direct contact with the flame. It was surrounded by a casing of unalloyed steel. Where the cracks had not eroded away, it was clear they ran transcrystalline, indicative of stress-corrosion cracking. Because the cracks propagated from the outer surface of the vessel, they were not caused by the derusting agent but by the external atmosphere in conjunction with welding stresses. The narrow gap between vessel and mild steel casing may have aggravated the situation in that it hindered ventilation and evaporation of condensation and favored the absorption and concentration of acids and salts. Contact and crevice corrosion due to deposition of rust from the mild steel casing may have contributed.
Image
Published: 01 January 2002
Fig. 33 Fatigue striations in 18-8 austenitic stainless steel tested in rotating bending. (a) Fine striations were located midway between origin and final overload fracture, while (b) coarse striations were located closer to the overload area. Overall direction of crack growth in these SEM
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Image
Published: 01 January 2002
Fig. 40 Crystallographic fatigue of 18-8 austenitic stainless steel near fracture origin in rotating beam specimen. Global crack propagation direction from lower left to upper right in this SEM view
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Image
Published: 15 January 2021
Fig. 33 Fatigue striations in 18-8 austenitic stainless steel tested in rotating bending. (a) Fine striations were located midway between origin and final overload fracture, while (b) coarse striations were located closer to the overload area. Overall direction of crack growth
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Image
Published: 15 January 2021
Fig. 40 Crystallographic fatigue of 18-8 austenitic stainless steel near fracture origin in rotating-beam specimen. Global crack propagation direction from lower left to upper right in this scanning electron microscope view
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in Metallic Inclusions in Steel
> ASM Failure Analysis Case Histories: Processing Errors and Defects
Published: 01 June 2019
Fig. 5 Foreign inclusion in a pipe 18/8 stainless steel. Longitudinal section through the weakly magnetized region. Etch: V2A pickle 10×
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in Metallic Inclusions in Steel
> ASM Failure Analysis Case Histories: Processing Errors and Defects
Published: 01 June 2019
Fig. 6 Foreign inclusion in a pipe 18/8 stainless steel. Longitudinal section through the weakly magnetized region. Etch: V2A pickle 500×
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001168
EISBN: 978-1-62708-219-8
... Abstract Steel pipes, used for years in a food factory soft water preheater, were found to leak as a result of corrosion. The pipes, made of 18/8 steel, were immersed in steam maintained at 0.5 atm and 150 deg C. They carried desalinated process water, heating it to approximately 100 deg C...
Abstract
Steel pipes, used for years in a food factory soft water preheater, were found to leak as a result of corrosion. The pipes, made of 18/8 steel, were immersed in steam maintained at 0.5 atm and 150 deg C. They carried desalinated process water, heating it to approximately 100 deg C. Inspection revealed a reddish-brown coating on the outside of the pipe with a few flat pitting holes and incipient cracks. Corrosion was also observed on the inner walls of the pipe, consisting of rust patches with pitting scars, branching out to predominantly transcrystalline cracks. In this case, leaking appears to be the result of a combination of pitting and stress corrosion, most likely due to chlorides. The factory was recommended to use molybdenum-alloyed steels (type 18/10 or 18/12) which are more resistant to local disruption of passivating films and pitting than molybdenum-free types such as 18/8.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c9001423
EISBN: 978-1-62708-233-4
... Abstract Five cylinders out of a group of nine in a drying machine developed leaks after a few months service in a textile mill. Leakage was reported from locations between the hoop and body and from the circumferential welds. The materials in the affected area were 18/8 Ti and 18/10/3/Mo...
Abstract
Five cylinders out of a group of nine in a drying machine developed leaks after a few months service in a textile mill. Leakage was reported from locations between the hoop and body and from the circumferential welds. The materials in the affected area were 18/8 Ti and 18/10/3/Mo austenitic stainless steels. Examination of the cracks at high magnification revealed them to be of the stress-corrosion type. The welds were of satisfactory quality. Cracking was also visible at these locations, this again being of the stress corrosion type. The method of cylinder construction introduced a crevice between the outer hoop and the cylinder at the inboard edge so that during washing of the rolls, water could penetrate the crevice and subsequent heating would lead to the concentration of chlorides within the crevice. Redesign of the cylinder to eliminate the crevice was recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001184
EISBN: 978-1-62708-235-8
... pearlite range (Troostite). In a pipe of 18-8 austenitic stainless steel a weakly magnetizable spot of limited size was found. This inclusion too was probably more alloy-deficient than the austenitic steel, similar to the ones described above. All three cases were casting defects. Inclusions Steel...
Abstract
Examples of metallic inclusions in steels of various types are presented. The structure of an inclusion in an annealed Fe-1C-1.5Cr steel consisted of ferrite with lamellar pearlite. The carbon content of the inclusion was therefore considerably lower than that of the chromium steel and was adapted to the latter by diffusion only at the periphery of the inclusion. In another section of a hardened piece of the same chromium steel, the steel in this case had a structure of martensite with hypereutectic carbide, while the inclusions consisted of a very fine laminated eutectoid of the lower pearlite range (Troostite). In a pipe of 18-8 austenitic stainless steel a weakly magnetizable spot of limited size was found. This inclusion too was probably more alloy-deficient than the austenitic steel, similar to the ones described above. All three cases were casting defects.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001397
EISBN: 978-1-62708-235-8
... Abstract Banding wires of the rotor of an 1800 hp motor were renewed following replacement of the banding rings. After about six months of service, a breakdown occurred due to bursting of the banding wires in several places. The 0.064 in. diam wire was nonmagnetic and of the 18/8 Cr-Ni type...
Abstract
Banding wires of the rotor of an 1800 hp motor were renewed following replacement of the banding rings. After about six months of service, a breakdown occurred due to bursting of the banding wires in several places. The 0.064 in. diam wire was nonmagnetic and of the 18/8 Cr-Ni type of austenitic stainless steel. The fractures were short and partially crystalline, with no evidence of slowly developing cracks of the fatigue type. Microscopical examination of sections taken through the fractures showed the cracking to be of the multiple branching type. Because the material was in the heavily cold-worked condition, it was not possible to determine with certainty if the cracks were of the inter- or trans-granular type. It was concluded that failure was due to stress-corrosion cracking in a chloride environment. Failure of the wires was likely due to the use of a chloride-containing flux during the soldering operation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0045911
EISBN: 978-1-62708-230-3
... Abstract Within the first few months of operation of an 8 km (5 mile) long 455 mm (18 in.) diam high-pressure steam line between a coal-fired electricity-generating plant and a paper mill, several of the Inconel 600 bellows failed. The steam line operated at 6030 kPa (875 psi) and 420 deg C...
Abstract
Within the first few months of operation of an 8 km (5 mile) long 455 mm (18 in.) diam high-pressure steam line between a coal-fired electricity-generating plant and a paper mill, several of the Inconel 600 bellows failed. The steam line operated at 6030 kPa (875 psi) and 420 deg C (790 deg F). Metallographic sections, energy-dispersive x-ray spectra, chemical analyses, tensile tests, and Auger microscope analyses showed the failed bellows met the specifications for the material. However, investigation also showed entire oxide thickness was contaminated with relatively large amounts of sodium, calcium, potassium, aluminum, and sulfur, alkali, alkali earth, and other contaminants that completely permeated even the thin oxides on the fracture surfaces. Additional investigation of the purity of the steam itself as reported by the power plant showed that corrosion and cracks were ultimately caused by the steam. While under normal operation, the steam's purity posed no problem to the material, during boiler cleaning operations, the generating plant had allowed contamination to get into the steam line.
Image
Published: 01 January 2002
Fig. 41 Centerline cooling curves showing the effect of scale on the cooling curves of two different steels quenched in fast oil without agitation. (a) 1095 steel; oil temperature, 50 °C (125 °F). (b) 18-8 stainless steel; oil temperature, 25 °C (75 °F). Test specimens were 13 mm (0.5
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001401
EISBN: 978-1-62708-220-4
... forms) Sodium chloride Stress relieving 18-8 Stress-corrosion cracking Following disruption of the basket of a hydro-extractor used for the separation of crystals of salt (sodium chloride) from glycerine, samples of the broken parts were submitted to the Company with a view to ascertaining...
Abstract
Following disruption of the austenitic stainless steel basket of a hydro-extractor used for the separation of crystals of salt (sodium chloride) from glycerin, samples of the broken parts were analyzed. Examination revealed that the fish-plates joining the reinforcing hoops had broken, the shell had split from top to bottom adjacent to the weld, the top and bottom cover plates had become loose, all the rivets having pulled out, and the shaft was also found to be bent. Fracture took place in an irregular manner and was of the shear type towards both ends; it occurred immediately adjacent to the weld or a short distance from it and on alternate sides. Microscopical examination did not reveal any intergranular carbide precipitation, such as is well known to result in the weld-decay mode of failure. It was concluded that the primary cause of failure was stress-corrosion cracking arising from the combined effect of residual stresses and the corrosive effect of the material being centrifuged. If the shell had been stress-relieved after fabrication, the failure likely would not have occurred.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001489
EISBN: 978-1-62708-217-4
... 6 11 53 10 7 16 1 2 7 18 44 17 5 2 1 13 8 18 28 30 8 3 1 12 MO-N 2 O 3 spinels 9 47 2 22 3 — 12 14 M=Fe, Mn, or Mg 10 57 — 3 — — 23 17 N=Cr or Al 11 50 19 14 — — 17 — 12 27 8 52 7 5 — 1 Calculated Results Based...
Abstract
The cause of the fatigue failure in the retaining ring of the compressor region of an aero-engine turbine was found to be the presence of a high concentration of nonmetallic inclusions. The results of chemical analysis were used to estimate the phases present. The most frequently observed inclusions were spinel solid solutions of the type MO middot; N2O3, where M = Fe, Mn, or Mg and N = Cr or Al. The detrimental inclusions were corundum, calcium aluminates, cristobalite, and silicates. The most detrimental phases were traced on the surfaces of the specimens fractured using impact loading; the comparison is being made with the polished surfaces and the tensile specimen fracture surfaces. The inclusions in the failed retaining ring were compared with the ones in a similar component obtained from a used engine. In the case of the latter, a large number of fine and elongated (Mn, Cr, Fe)S inclusions were present along with spinels. The nondeformable, rigid oxide particles are considered more undesirable than the sulfides as far as fatigue life of the component is concerned. It has been reported that the presence of sulfides may eliminate the stresses due to oxides.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001171
EISBN: 978-1-62708-219-8
... results in a typical intercrystalline corrosion. The carbide precipitation rate is related to the steel carbon content. In the 18/8 stainless steels, the carbon is stable in solid solution, on all conditions, up to a maximum content of 0,03 wt-%. With the increasing of this content, up to about 0,08...
Abstract
The defects observed along weldings of stainless steel pipelines employed in marine environments were evidenced by metallographic and electrochemical examination. A compilation of cases on the effect of defective weldings, in addition to improper choice of stainless steel for water pipelines, lead to the conclusion that intercrystalline corrosion in steels involved precipitation of a surplus phase at grain boundaries. Intercrystalline corrosion in austenitic stainless steels due to precipitation of chromium carbides during conditions generated due to welding and ways to avoid the precipitation (including reduction of carbon content, appropriate heat treatment, cold work of steel, reduction of austenitic grain size and stabilizing elements) were described. The presence of microcracks due to highly localized heat concentrations with consequent thermal expansion and considerable shrinkages during cooling was investigated. The specimens were taken from various sources including transverse and longitudinal welding seam, sensitized areas and it was concluded appropriate material selection with respect to medium could control some corrosion processes.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001301
EISBN: 978-1-62708-215-0
... of gear segment MLR The fracture surfaces on teeth 18 and 23 of gear segment F exhibited similar thumbnail patterns that appeared to emanate from a single location on each fracture surface. Figures 8 and 9 show the thumbnail pattern and the suspected fracture origin, respectively, for tooth 18...
Abstract
Gears in a strip mining dragline failed in service. The material was identified as a low-alloy (NiCrMoV) steel. SEM analysis indicated that the initial fracture and subsequent fractures resulted from impact or a suddenly applied load. Mechanical testing indicated that the gears had low impact strength. Failure was attributed to low toughness caused by the absence of, or improper, heat treatment. Casting defects identified during metallographic examination were determined to be the fracture initiation site, but were considered less significant than the low as-received impact strength of the material. It was recommended that the equipment manufacturer implement an appropriate heat treatment to meet the impact requirements of the application.
Image
Published: 01 January 2002
Ref MPa ksi 1–4 5.6 0.84 0.12 0.5 18 5–7 0.5 4.25 0.62 0.05–0.1 29 8 (a) 1.6 0.69 0.10 0.05 27 (a) N 2 atmosphere at room temperature
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0048607
EISBN: 978-1-62708-225-9
... were not subjected to cyclic loading, fatigue or corrosion fatigue was not possible. To prevent reoccurrence, bolts were required to conform to the specified chemical composition. The hardness range for the bolts was changed from 35 to 45 HRC to 18 to 24 HRC. Petroleum jelly was used as an antiseizure...
Abstract
Stainless steel bolts broke after short-term exposure in boiler feed-pump applications. Specifications required that the bolts be made of a 12% Cr high-strength steel with a composition conforming to that of AISI type 410 stainless steel. Several bolts from three different installations were examined. It was found that fracture of the bolts was by intergranular stress corrosion. A metallic copper-containing antiseizure compound on the bolts in a corrosive medium set up an electro-chemical cell that produced trenchlike fissures or pits for fracture initiation. Because the bolts were not subjected to cyclic loading, fatigue or corrosion fatigue was not possible. To prevent reoccurrence, bolts were required to conform to the specified chemical composition. The hardness range for the bolts was changed from 35 to 45 HRC to 18 to 24 HRC. Petroleum jelly was used as an antiseizure lubricant in place of the copper-containing compound. As a result of these changes, bolt life was increased to more than three years.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001146
EISBN: 978-1-62708-229-7
...) 20.0 (27.1) 3. (L) +73 room temp. (23°C) 13.0 (17.6) 4. (L) +32 (0°C) 20.0 (27.1) 5. (L) 0 (−18°C) 10.5 (14.2) 6. (L) 0 (−18°C) 13.5 Plate 2 (18.3) 7. (L) −35 (−37°C) 20.0 (27.1) 8. (L) −60 (−51°C) 18.75 Plate 2 (25.4) 9. (L) −270 Liq...
Abstract
A metallurgical failure analysis was performed on pieces of the cracked vent header pipe from the Edwin I. Hatch Unit 2 Nuclear power plant. The analysis consisted of optical microscopy, chemical analysis, mechanical Charpy impact testing, and fractography. It was found that the material of the vent header met the mechanical and chemical properties of ASTM A516 Grade 70 carbon-manganese steel material and microstructures were consistent with this material. Fracture faces of the cracked pipe were predominantly brittle in appearance with no evidence of fatigue contribution. The NDTT (Nil ductility Transition Temperature) for this material was approximately -51 deg C (-60 deg F). The fact that the material's NDTT was significantly out of the normal operating range of the pipe suggested an impingement of low temperature nitrogen (caused by a faulty torus inerting system) induced a thermal shock in the pipe which, when cooled below its NDTT, cracked in a brittle manner.
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