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1020
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0048091
EISBN: 978-1-62708-224-2
... and welding. The metal was identified to be 1020 steel. It was indicated by the coarse as-rolled structure (grain size of ASTM 00 to 4) of the base metal that the weldment (stop block and guide) had not been normalized. The brittle failure was evaluated to have been initiated at a metallurgical and mechanical...
Abstract
A section from a stop-block guide fell to the floor on a crane runway after it failed. A brittle crystalline-type break was disclosed by examination of the fracture surface. The point of initiation was in a hardened heat-affected layer that had developed during flame cutting and welding. The metal was identified to be 1020 steel. It was indicated by the coarse as-rolled structure (grain size of ASTM 00 to 4) of the base metal that the weldment (stop block and guide) had not been normalized. The brittle failure was evaluated to have been initiated at a metallurgical and mechanical notch produced by flame cutting and welding. As corrective measures, fully silicon-killed 1020 steel with a maximum grain size of ASTM 5 were used to make new stop-block weldments. The weldments were normalized at 900 deg C after flame cutting and welding to improve microstructure and impact strength. All flame-cut surfaces were ground to remove notches.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0048060
EISBN: 978-1-62708-224-2
... Abstract The crane hook (rated for 13000 kg) failed in the threaded shank while lifting a load of 9072 kg. The metal in the hook was revealed by chemical analysis to be killed 1020 steel. It was disclosed by visual examination that the fracture had at the last thread on the shank and rough...
Abstract
The crane hook (rated for 13000 kg) failed in the threaded shank while lifting a load of 9072 kg. The metal in the hook was revealed by chemical analysis to be killed 1020 steel. It was disclosed by visual examination that the fracture had at the last thread on the shank and rough machining and chatter marks were evident on the threads. Beach marks that emanated from the thread-root locations on opposite sides of the fracture surface identified these locations to be the origins of the fracture. A medium-coarse slightly acicular structure was revealed by metallographic examination which indicated that the material was in the as-forged condition (which meant lower fatigue strength). The fracture was concluded to have occurred due to stress concentration in the root of the last thread. Normalizing of the crane hook after forging was suggested as a corrective measure. A stress-relief groove with a diam slightly smaller than the root diam was placed at the end of the thread and a large-radius fillet was machined at the change in diameter of the shank.
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in Mechanisms and Appearances of Ductile and Brittle Fracture in Metals
> Failure Analysis and Prevention
Published: 01 January 2002
Fig. 37 Tensile fracture of a 1020 steel showing slanted fracture intersecting the outside surface at an angle
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in Mechanisms and Appearances of Ductile and Brittle Fracture in Metals
> Failure Analysis and Prevention
Published: 01 January 2002
Fig. 38 Fractured 1020 steel showing an angled connection between a cup portion on one half of the fractured bar and a cup portion on the other half
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Published: 01 January 2002
Fig. 5 Surface of 1020 steel eroded by SiC at 80 m/s (260 ft/s) and 30° impact angle
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Published: 01 January 2002
Fig. 6 Erosion rates of 1020 steel by 180 to 250 μm (7 to 10 mil) particles at 80 m/s (260 ft/s)
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Published: 01 January 2002
Fig. 1 Exposure to vibratory cavitation of normalized AISI 1020 steel. (a) Damage after 5 min. (b) Material removal after 10 min
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Published: 01 January 2002
Fig. 12 Typical design of a 45,360-kg (50-ton) capacity 1020 steel C-hook with a stress-relief groove at end of threads and well-proportioned radii in body. Dimensions given in inches
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Published: 01 January 2002
Fig. 13 13,600-kg (15-ton) 1020 steel crane hook that failed in fatigue. View of a fracture surface of the hook showing beach marks. Original and improved designs for the nut and the threaded end of the hook are also shown. Dimensions given in inches
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in Fatigue Fracture of a 1020 Steel Crane Hook
> ASM Failure Analysis Case Histories: Material Handling Equipment
Published: 01 June 2019
Fig. 1 13,600-kg (15-ton) 1020 steel crane hook that failed in fatigue. View of a fracture surface of the hook showing beach marks. Original and improved designs for the nut and the threaded end of the hook are also shown. Dimensions given in inches
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Published: 15 January 2021
Fig. 5 Surface of AISI 1020 carbon steel eroded by SiC at 80 m/s (260 ft/s) and 30° impact angle. Source: Ref 8
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Published: 15 January 2021
Fig. 6 Erosion rates of AISI 1020 carbon steel by 180 to 250 μm (7 to 10 mils) particles at 80 m/s (260 ft/s)
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in Mechanisms and Appearances of Ductile and Brittle Fracture in Metals
> Failure Analysis and Prevention
Published: 15 January 2021
Fig. 37 Tensile fracture of a 1020 plain carbon steel showing slanted fracture intersecting the outside surface at an angle
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in Mechanisms and Appearances of Ductile and Brittle Fracture in Metals
> Failure Analysis and Prevention
Published: 15 January 2021
Fig. 38 Fractured 1020 plain carbon steel showing an angled connection between a cup portion on one half of the fractured bar and a cup portion on the other half
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in Failures of Cranes and Lifting Equipment
> Analysis and Prevention of Component and Equipment Failures
Published: 30 August 2021
Fig. 32 Typical design of a 45,360 kg (50 ton) capacity grade 1020 steel C-hook with a stress-relief groove at end of threads and well-proportioned radii. Dimensions given in inches
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in Failures of Cranes and Lifting Equipment
> Analysis and Prevention of Component and Equipment Failures
Published: 30 August 2021
Fig. 33 13,600 kg (15 ton) grade 1020 steel crane hook that failed in fatigue. View of a fracture surface of the hook showing beach marks (right). Original and improved designs for the nut and the threaded end of the hook are also shown (left). Dimensions given in inches
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c0048087
EISBN: 978-1-62708-231-0
... Abstract Several of the welds in a hoist carriage tram-rail assembly fabricated by shielded metal arc welding the leg of a large T-section 1020 steel beam to the leg of a smaller T-section 1050 steel rail failed in one portion of the assembly. Four weld cracks and several indefinite indications...
Abstract
Several of the welds in a hoist carriage tram-rail assembly fabricated by shielded metal arc welding the leg of a large T-section 1020 steel beam to the leg of a smaller T-section 1050 steel rail failed in one portion of the assembly. Four weld cracks and several indefinite indications were found by magnetic-particle inspection. The cracks were revealed by metallographic examination to have originated in the HAZs in the rail section. Cracks in welds and in HAZs resulting from arcing the electrode adjacent to the weld and weld spatter were also revealed. The tram-rail assembly was concluded to have failed by fatigue cracking in HAZs. The fatigue cracking was initiated and propagated by vibration of the tram rail by movement of the hoist carriage on the rail. As a corrective measure, welding procedures were improved and the replacement rail assemblies were preheated and postheated.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001017
EISBN: 978-1-62708-219-8
... Abstract A 10-in. diam, spiral-welded AISI 1020 carbon steel pipe carrying water under pressure developed numerous leaks over a four mile section. The section was fabricated using submerged-arc welding from the outside surface. Each welded length of pipe had been subjected to a proof pressure...
Abstract
A 10-in. diam, spiral-welded AISI 1020 carbon steel pipe carrying water under pressure developed numerous leaks over a four mile section. The section was fabricated using submerged-arc welding from the outside surface. Each welded length of pipe had been subjected to a proof pressure approximately twice the specified design pressure and two-thirds the approximate yield point of the parent metal. No failures or leakage were observed during proof testing. Metallurgical examination corroborated visual checks, indicating a distinct lack of root penetration in the split areas. Splitting occurred as a result of inadequate root penetration. The most likely source of difficulty in the welding process was the linear speed. Probably, the failures would not have occurred in absence of the welding problem. Also, the pipe was inadequate for the specified design pressure, as well as the reported maximum system pressure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0048068
EISBN: 978-1-62708-224-2
... measure, the chain-sling hook was replaced with one made of normalized, fully killed, finegrain 1020 steel. Acicular structure Cranes Normalizing (heat treatment) 1015 UNS G10150 Metalworking-related failures Fatigue fracture A hook on a two-leg chain broke while lifting a 4990-kg (11,000...
Abstract
A hook on a two-leg chain (each 13 mm diam, included angle 60 deg) failed at the junction of the eye and shank while lifting a 4990 kg load. The diam of the hook at this junction was approximately 22 mm. Light intergranular oxidation at the surface on the side of the hook where cracking started was revealed by visual examination of the fracture region. Almost 50% of the fracture surface was found to contain beach marks (indicative of fatigue failure) while the remainder contained cleavage facets. A medium-coarse acicular as-forged structure was revealed by metallographic examination and the metal was showed by chemical analysis to be semikilled 1015 steel. The fatigue fracture was concluded to have initiated in the intergranular oxidation region and the failure of the hook was contributed by the poor fatigue and impact properties of the forged structure. As a corrective measure, the chain-sling hook was replaced with one made of normalized, fully killed, finegrain 1020 steel.
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