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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047387
EISBN: 978-1-62708-225-9
... composition Gear teeth Hardenability Sprockets Low-alloy steel (Other, miscellaneous, or unspecified) failure Induction-hardened teeth on a sprocket cast of low-alloy steel wore at an unacceptably high rate. A surface hardness of 50 to 51 HRC was determined; 55 HRC minimum had been specified...
Abstract
Induction-hardened teeth on a sprocket cast of low-alloy steel wore at an unacceptably high rate. A surface hardness of 50 to 51 HRC was determined; 55 HRC minimum had been specified. Analysis revealed that the alloy content of the steel was adequate for the desired hardenability but that the specified carbon content (0.29%) was too low. The low specified carbon content resulted in unacceptably low hardness. Because hardness largely controls wear rate, an early failure occurred. The specification for this part was changed so that a higher carbon content (0.45% C) was required.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0046953
EISBN: 978-1-62708-220-4
...), which exceeded normal operating temperatures, and carburization was not the principal cause of failure. No recommendations were made. Chemical reactors Melting Overheating Hastelloy X UNS N06002 (Other, miscellaneous, or unspecified) failure A portion of the wall of a reactor vessel used...
Abstract
A portion of the wall of a reactor vessel used in burning impurities from carbon particles failed by localized melting. The vessel was made of Hastelloy X (Ni-22Cr-9Mo-18Fe). Considering the service environment, melting could have been caused either by excessive carburization (which would have lowered the melting point of the alloy markedly) or by overheating. A small specimen containing melted and unmelted metal was removed from the vessel wall and examined metallographically. It was observed that the interface between the melted zone and the unaffected base metal was composed of large grains and enlarged grain boundaries. An area a short distance away from the melted zone was fine grained and relatively free of massive carbides. This evidence supported the conclusion that the vessel failed by melting that resulted from heating to about 1230 to 1260 deg C (2250 to 2300 deg F), which exceeded normal operating temperatures, and carburization was not the principal cause of failure. No recommendations were made.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0048035
EISBN: 978-1-62708-224-2
.... Thus, a 50% loss in tensile strength of the wires was caused by overheating which lead to failure of the rope. It was recommended that prolonged exposure of wire ropes to extreme conditions should be avoided. Cranes Slags Tensile strength Steel wire rope (Other, miscellaneous, or unspecified...
Abstract
A 3.8-cm diam 6 x 37 rope of improved plow steel wire failed in service during dumping of a ladle of hot slag. A heavy blue oxide extending 0.6 to 0.9 m back from each side of the break was revealed on examination of the rope. Tensile fractures were shown by the broken ends of the rope. Recrystallization of the steel was revealed during microscopic examination of the wires adjacent to the break which indicated that the wires had been heated in excess of 700 deg C (1292 deg F). The tensile strength of the wires in the rope that broke was 896 MPa whereas the specification required it to be 1724 MPa. Thus, a 50% loss in tensile strength of the wires was caused by overheating which lead to failure of the rope. It was recommended that prolonged exposure of wire ropes to extreme conditions should be avoided.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001900
EISBN: 978-1-62708-225-9
... the residue of partial melting was seen. Ball bearings Electric arcs Electric motors Grounding (electrical) Martensite Melting Scanning electron microscopy 52100 UNS G52986 (Other, miscellaneous, or unspecified) failure Incorrect grounding of an electric motor resulted in electric current...
Abstract
Incorrect grounding of an electric motor resulted in electric current passing through a 52100 steel ball bearing and caused multiple arcing between the rolling elements. The multiple arcing developed a pattern on the outer race known as ‘fluting’. A section of ball race outer showed the distinct banding (fluting) resulting from spark discharges while the bearing was rotating. The severe distress of the surface resulted in unacceptable levels of vibration. An SEM photograph of the banded regions showed smoothing of the asperities from continued operation is evident. In the craters the residue of partial melting was seen.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047939
EISBN: 978-1-62708-225-9
... 4620 UNS G46200 (Other, miscellaneous, or unspecified) failure The roller bearing shown in Fig. 1 was one of two that were mounted in an electric motor/gearbox assembly. Rough operation of the bearing was observed, and the unit was shut down. The bearing was removed and submitted...
Abstract
Rough operation of the roller bearing mounted in an electric motor/gearbox assembly was observed. The bearing components made of low-alloy steel (4620 or 8620) and the cup, cone and rollers were carburized, hardened and tempered. The contact surfaces of these components (cup, cone and roller) were revealed to be uniformly electrolytically etched by visual examination. The action similar to anodic etching was believed to have occurred as a result of stray currents in the electric motor (not properly grounded) and the presence of an electrolyte (moisture) between the cup and roller surfaces of the bearing. As a remedial action, the bearing was insulated for protection from stray currents by grounding of the motor and the moisture was kept out by sealing both bearings in the assembly.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047935
EISBN: 978-1-62708-225-9
..., miscellaneous, or unspecified) wear (Other, miscellaneous, or unspecified) failure The electric motor in an office machine was producing intermittent noise. Ball bearings were suspected as the source of the noise and were removed from the motor and sent to the laboratory for examination. The bearings...
Abstract
Ball bearings made of type 440C stainless steel hardened to 60 HRC and suspected as the source of intermittent noise in an office machine were examined. A number of spots on the inner-ring raceway were revealed by scanning electron microscopy. The metal in the area around the spot was evidenced to have been melted and welded to the inner-ring raceway. It was revealed by randomly spaced welded areas on the raceways that the welding was the result of short electrical discharges between the bearing raceways and the balls. The use of an electrically nonconductive lubricant in the bearings was suspected to have caused the electric discharge by accumulation and discharge of static charge. The electrical resistance between the rotor and the motor frame lubricated with electrically conductive grease and the grease used in the current case was measured and compared to confirm the fact the currently used grease was nonconductive. It was concluded that the pits were formed by momentary welding between the ball and ring surfaces. The lubricant was replaced by electrically conductive grease as a corrective measure.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0046956
EISBN: 978-1-62708-232-7
... boundaries Intermetallic phases Muffle furnaces Overheating Nickel-base high-temperature alloy (Other, miscellaneous, or unspecified) failure A brazing-furnace muffle 34 cm (13 1 4 in.) wide, 26 cm (10 3 8 in.) high, and 198 cm (78 in.) long, was fabricated from nickel-base high...
Abstract
A brazing-furnace muffle 34 cm (13 in.) wide, 26 cm (10 in.) high, and 198 cm (78 in.) long, was fabricated from nickel-base high-temperature alloy sheet and installed in a gas-fired furnace used for copper brazing of various assemblies. The operating temperature of the muffle was reported to have been closely controlled at the normal temperature of 1175 deg C (2150 deg F); a hydrogen atmosphere was used during brazing. After about five months of continuous operation, four or five holes developed on the floor of the muffle, and the muffle was removed from service. Analysis (visual inspection, x-ray spectrometry, and metallographic examination) supported the conclusion that the muffle failed by localized overheating in some areas to temperatures exceeding 1260 deg C (2300 deg F). The copper found near the holes had dripped to the floor from assemblies during brazing. The copper diffused into the nickel-base alloy and formed a grain-boundary phase that was molten at the operating temperature. The presence of this phase caused localized liquefaction and weakened the alloy sufficiently to allow formation of the holes. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047118
EISBN: 978-1-62708-235-8
... Nonmetallic inclusions 1035 UNS G10350 (Other, miscellaneous, or unspecified) failure An automobile manufacturer rejected several 1035 steel stub axles because of what appeared to be short longitudinal cracks in the surfaces of the pins. ( Fig. 1a ). The cracks were found when six axles were examined...
Abstract
An automobile manufacturer rejected several 1035 steel stub axles because of what appeared to be short longitudinal cracks in the surfaces of the pins. The cracks were found when six axles were examined for defects by magnetic-particle inspection. However, metallographic examination showed that these lines were not cracks but slag inclusions at and immediately below the surface. Analysis (visual inspection, metallographic examination, and 100x/500x magnetic-particle inspection) supported the conclusions that the inclusions consisted of pieces of fireclay from channel brick that were flushed into the ingot mold. Although no true cracks were present, rejection of the stub axles was nevertheless justified. Slag streaks could reduce the strength of the stub axles and lead to the formation of fatigue fractures during operation. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001080
EISBN: 978-1-62708-214-3
...) Turbine disks Turbine steel (Other, miscellaneous, or unspecified) failure Handbook of Case Histories in Failure Analysis, Volume 1 Copyright © 1992 ASM International® K.A. Esaklul, editor All rights reserved DOI: 10.31399/asm.fach.v01.c9001080 www.asminternational.org ...
Abstract
A steam turbine developed excessive noise and vibration during routine operation. It was found that the nut that locked the turbine disk In place had worked its way out from the threads and the disk had come of the shaft. Examination of the locking mechanism indicated that its design was responsible for the loosening of the nut. It was recommended that the locking mechanism be redesigned and changed in all existing turbines.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001623
EISBN: 978-1-62708-232-7
... wool (Other, miscellaneous, or unspecified) failure Several glass wool insulation sections from a heat-treat furnace showed visible discoloration. The insulation was originally white but exhibited a gray discoloration in some areas, as shown in Fig. 1 . As in the coin example, this discoloration...
Abstract
Several glass wool insulation sections from a heat-treat furnace showed visible, but only cosmetic discoloration. EDS showed the presence of silicon, aluminum, and oxygen in the nondiscolored region, and these elements are consistent with glass wool. Relatively high levels of chromium and nickel were detected in the discolored area, along with lower amounts of iron, manganese, sodium, calcium, cobalt, and sulfur, in addition to the surrounding glass wool elements. Results of this limited evaluation showed the discoloration was caused by the presence of elevated levels of chromium, nickel, and aluminum. The visual appearance, along with the EDS findings, suggested these elements were present in the form of oxides. These oxides were likely deposited from adjacent structural components of the furnace, which had oxidized during operation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001015
EISBN: 978-1-62708-217-4
... Carburetors Clamps Helicopters Turbochargers Metal (Other, miscellaneous, or unspecified) failure Careful investigation of the flight log and accident reports indicated that a helicopter rapidly lost altitude and struck a tree, causing a fire and severe damage. In cases of this kind, it is common...
Abstract
A helicopter rapidly lost altitude and struck a tree, causing a fire and severe damage. The hose clamp which was the subject of this investigation was one of two used on a short length of hose between the turbocharger and the carburetion system. The purpose of this examination was to determine whether the hose failed during or before the accident. Fracture in the failed clamp was accompanied by obvious permanent deformation and evidence of local shearing at the ends of the perforation where fracture occurred, and in the adjacent perforation. The first test involved tightening the clamps to failure with a torque wrench. In no case did the band material fracture. In a second attempt to duplicate the failure, a tensile testing machine was used to pull the two fittings apart while the hose was clamped in place. When the testing machine was operated at maximum head travel (approximately 20 in. per min.), one of the hose clamps broke in the same manner as the clamp in question. The manner of failure during the tension test indicated this clamp failed at the time of the crash because of a sudden separation between the turbocharger and the remainder of the aircraft.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001626
EISBN: 978-1-62708-235-8
... into place and another type of tank material be considered. Chemical analysis Discoloration Pickling Tubes 17-4 PH UNS S17400 (Other, miscellaneous, or unspecified) failure A type 17-4PH stainless steel tube exhibited brown discoloration after a pickling operation. Although the discoloration...
Abstract
A type 17-4PH stainless steel tube exhibited brown discoloration after a pickling operation. EDS analysis of the extracted substance revealed relatively high levels of iron and chromium, along with lower amounts of aluminum, silicon, sulfur, chlorine, calcium, manganese, and nickel. The iron, chromium, and nickel are likely in the form of dissolution products from the pickling solution. FTIR analysis revealed the presence of polypropylene and poly(ethylene:propylene). The EDS results showed that the discoloration of the tube was associated with oxidation products of the tube material, as well as adherent organic residue. Analysis by FTIR of the residue revealed detectable levels of two polymeric substances, which were later determined to be construction materials of the pickling tank. It was recommended that more frequent cleaning and/or replacement of the pickling solution be put into place and another type of tank material be considered.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001624
EISBN: 978-1-62708-218-1
..., which led to melting of the wire. Chemical analysis Corrosion products Discoloration Electric Sensors Wire Copper (Other, miscellaneous, or unspecified) failure An electronic sensor coil failed continuity testing, indicating that a break was present in the polymercoated wire...
Abstract
An electronic sensor coil failed continuity testing, indicating that a break was present in the polymer-coated wire. An area of the wire showed a green discoloration and the break in the wire was located in this same region. The discoloration was suspected to be an indicator of what caused the failure. SEM/EDS and FTIR results showed the break in the coil wire was associated with corrosion. The corrosion debris contained relatively high levels of sodium and chlorine, which were likely in the form of salt. Some salt deposits were noted also in other areas along the wire surface. The findings suggested salt or salt water had leaked into the sensor and caused localized corrosion to the wire, possibly at an area where preexisting damage was present in the coating. Separation occurred in the wire when the current density at the reduced cross section caused excessive localized heating, which led to melting of the wire.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001572
EISBN: 978-1-62708-236-5
... in this case for the production acceptance tests. Coating removal Gouging Hydraulic assemblies Wobblers 52100E Titanium nitride coating UNS G52986 (Other, miscellaneous, or unspecified) failure Background Extensive slipper/wobbler failures had occurred in the integrated drive generators...
Abstract
Extensive slipper/wobbler failures occurred in the integrated drive generators that incorporated TiN coated wobblers, during the production acceptance test. Similar coated wobblers had passed the application tests. The nature of the failure was extensive gouging of the wobbler surface with discoloration and coating removal. The substrate material was E52100 which was through-hardened to HRC 55-60. The slippers that were in contact with the coated wobbler surface were made of AISI 06 material. A synthetic oil was used as the hydraulic fluid in the application. The failure in the wobblers was caused by lack of temperature control during application which resulted in localized surface rehardening. It was established that there was a significant difference in the grade of the hydraulic fluid that was used in the two test programs. Use of superior grade of hydraulic fluid was recommended in this case for the production acceptance tests.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001441
EISBN: 978-1-62708-220-4
... failures (Other, miscellaneous, or unspecified) failure Soft-soldered joints in pipes that are subjected intermittently to temperatures below the freezing-point of water occasionally fail in a rather unusual manner, the two examples to be described having occurred in refrigerating plants. The samples...
Abstract
Soft-soldered copper pipe joints used in refrigerating plants failed. The solder had not adhered uniformly to the pipe surface. In addition, there were some longitudinal grooves on the pipe surfaces, parts of which were not filled with solder. The unsoldered areas formed cavities within the joints, some of which had been in direct communication with the outsides via the grooves or interconnected cavities. On cooling, moisture condensed on the external surfaces. Some of this was drawn by capillary action into the cavities in open communication with the external surface. On continued cooling to below freezing-point, water that entered the cavities solidified. This was accompanied by a slight increase in volume, which collapsed the pipe walls. In the examples, the pipe ends had not been properly tinned. The solder used was found to be of the tin-antimony type, containing about 5% antimony, which is more difficult to use than the usual tin-lead alloys. The use of this particular type of solder was a contributory factor in the production of unsound joints in the samples examined.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0045909
EISBN: 978-1-62708-232-7
... inclusion at the failure site in the melting pot may have reacted violently with the molten magnesium, causing the leak. Fires Foundries Liquid metals Magnesium Nonmetallic inclusions Xray analysis Hot-rolled steel (Other, miscellaneous, or unspecified) failure A steel pot used to melt...
Abstract
A hot rolled, low-carbon steel pot used to melt magnesium alloys leaked, releasing about 35 kg (80 lb) of molten magnesium onto the foundry floor and causing an extensive fire. Due to the fire, the original leakage hole could not be investigated. Samples of the failed pot were polished and etched and were found to be composed of ferrite and pearlite mixtures, as would be expected. However, the sample taken from a location about 75 mm (3 in.) from the hole contained a cluster of unusually large inclusions. By removing the beryllium window from in front of the detector, EPMA spectra were obtained from the inclusions and from the steel matrix. The inclusion spectrum contained primarily iron and oxygen, whereas the matrix spectrum contained primarily iron. X-ray maps were made to show the distribution of iron and oxygen. These results indicated that the inclusions were iron oxide. A similar inclusion at the failure site in the melting pot may have reacted violently with the molten magnesium, causing the leak.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047986
EISBN: 978-1-62708-217-4
... Stresses Vibration 52100 UNS G52986 (Other, miscellaneous, or unspecified) failure An engine on a jet aircraft produced excessive vibration in flight and was immediately shut down. Dismantling the engine revealed complete failure (fracture) of the cage in one of the two main-shaft ball...
Abstract
The engine on a jet aircraft was shut down immediately as it produced excessive vibration. Complete failure of the cage in one of the two main-shaft ball bearings (placed side by side in the engine) was revealed in the dismantled engine. The ball bearings (made of vacuum-melted 52100 steel) were both of the single-row deep-groove type with split inner rings and were designed to operate at a maximum temperature of 175 deg C. Overtempering of the rings was indicated by the reduced hardness in comparison to unfailed rings. Severe damage to approximately 20% of the load-bearing surface, with more damage on one of the shoulders of the groove, was revealed during examination of the outer raceway of the bearing which indicated misalignment of the bearing. No damage other than spalling cavities in the inner-ring raceway, caused by the elongated subsurface inclusion revealed by metallographic examination of circumferential section of the largest cavity, was exhibited by the second bearing. It was concluded that the fracture of the cage was caused by overheating and misalignment caused excessive stressing of the bearing on the main shaft.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0048257
EISBN: 978-1-62708-217-4
... in an exothermic atmosphere. It was recommended that steps be taken during heat treatment to ensure neither of the two occurred. Aerospace engines Case hardening Controlled atmosphere Exothermic reactions Surface hardness AMS 6263 UNS K44414 (Other, miscellaneous, or unspecified) failure Heat...
Abstract
Evidence of destructive pitting on the gear teeth (AMS 6263 steel) in the area of the pitchline was exhibited by an idler gear for the generator drive of an aircraft engine following test-stand engine testing. The case hardness was investigated to be lower than specified and it was suggested that it had resulted from surface defects. A decarburized surface layer and subsurface oxidation in the vicinity of pitting were revealed by metallographic examination of the 2% nital etched gear tooth sample. It was concluded that pitting had resulted as a combination of both the defects. The causes for the defects were reported based on previous investigation of heat treatment facilities. Oxide layer was caused by inadequate purging of air before carburization while decarburization was attributed to defects in the copper plating applied to the gear for its protection during austenitizing in an exothermic atmosphere. It was recommended that steps be taken during heat treatment to ensure neither of the two occurred.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c9001627
EISBN: 978-1-62708-222-8
.... Based on these findings, one of the recommendations was to use thicker pads between the sinks to allow any such liquids to dry before causing corrosion damage. Chemical analysis Chlorides Discoloration Kitchen sinks 304 UNS S30400 (Other, miscellaneous, or unspecified) failure A section...
Abstract
A section from a stainless steel kitchen sink showed a round red stain on its surface after a short time in storage. Several of these sinks were stacked together and separated by felt pads while in storage, and the mating sink showed a nearly identical stain in the same area, while no stains were noted on any of the other sinks in the stack. The stain was located near one of the pads; however, no discoloration was noted at the pad location. EDS analysis showed the base metal to be austenitic stainless steel, such as type 304. FTIR analysis of the stain revealed carboxylic salts and salts of organic acids, in addition to hydroxyl functionality. The discoloration was caused by localized rusting of the sink from prolonged exposure to a chloride containing substance. The appearance suggests that the substance may actually have been a drop of perspiration (sweat) from a factory worker. Based on these findings, one of the recommendations was to use thicker pads between the sinks to allow any such liquids to dry before causing corrosion damage.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001285
EISBN: 978-1-62708-215-0
... marked “T” indicate tensile failures, arrows “S” indicate shear failures, and arrows marked “C” indicate crushing damage. Compression damage Steel wire rope (Other, miscellaneous, or unspecified) failure Handbook of Case Histories in Failure Analysis, Volume 2 Copyright © 1993 ASM International...
Abstract
A 6 x 19 fiber core steel wire rope failed as it was being used to lower a steel television tower. Fracture of the rope occurred at a point under one of two clips used to fashion a spliced loop that was directly connected to the top of the tower. Microscopic examination of the fracture surfaces and the condition of the individual wires revealed that 59% of the wires failed by shear, 39% failed in tension, and 2% had been cut. In addition, 87% of the wires showed some degree of crushing damage, ranging from mild to severe. The failure was attributed to improper installation of the clips.
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