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Molybdenum
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0048299
EISBN: 978-1-62708-229-7
Abstract
Pendant-style reheater, constructed of ASME SA-213, grade T-11, steel ruptured. A set of four tubes, specified to be 64 mm OD x 3.4 mm minimum wall thickness was examined. A small quantity of loose debris was removed from the inside of one of the tubes. The major constituent was revealed by EDS analysis of the debris to be iron with traces of phosphorus, manganese, sodium, calcium, copper, zinc, potassium, silicon, chromium, and molybdenum. Thus the debris was interpreted to be the scale from ID of the tube with boiler feedwater chemicals from the attemperation spray. The likely cause of failure was concluded to be exfoliation of the scale from the ID surface of the tube. Creep failures were interpreted to be caused by localized temperatures higher than the maximum service temperature. Replacement of the affected tubes was recommended. Inspection of the tubes by radiography to find the circuits with the greatest accumulation of debris and replacing them as necessary was recommended on an annual basis.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001062
EISBN: 978-1-62708-214-3
Abstract
The causes of internal cracking that occurred in 9% Ni steel castings during manufacture were investigated using a series of eight laboratory castings containing varying amounts of molybdenum. The effect of mold thickness was also investigated. The laboratory castings were subjected to three-point bend testing, and fracture surfaces were examined using SEM fractography, metallography, and depth analysis (SIMS) of the fracture surface. The cracks were found to originate at austenitic grain boundaries that coincided with primary dendrite interfaces. The cracking was attributed to a decrease in grain-boundary cohesion resulting from sulfur segregation. Addition of molybdenum proved effective in preventing cracking. The molybdenum promoted MnS precipitation in the grain and preferentially segregated to the interfaces.