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Book Chapter
Microstructural Analysis of the Brass Seat of a Valve from the 1907 Steam Tug ‘Hercules’
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001684
EISBN: 978-1-62708-225-9
Abstract
The steam tug Hercules was an ocean-going and bay tug for 55 years before being retired. It is now being restored by the National Park Service. A broken steam valve was obtained for microstructural examination. The body was gray cast iron, and the stem and seat were brass. The examination centered on corrosion of the brass components. The seat and shaft were alpha brass, with a hardness of 64 and 79 DPH, respectively. A nut held the shaft onto the seat, and was alpha-beta brass with a hardness of 197 DPH. Welded on the end of the shaft was a ring of hard (DPH 294) alpha-beta brass, which seated against the nut. The brass seat and stem show little corrosion. However, the alpha-beta brass nut and welded tip showed extensive dezincification. This process of removal of Zn and the retention of Cu began in the high Zn beta phase, but eventually both phases were attacked. The depth of penetration was consistent with dezincification rates reported in the literature for such brasses in salt water if the valve had been in service about 55 years.
Book Chapter
Connecting Rod That Fractured Because of a Forging Fold
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0047151
EISBN: 978-1-62708-227-3
Abstract
A motorboat engine connecting rod forged from carbon steel fractured in two places and cracked at the small end during service. The analysis (visual inspection, 50x micrographs of sections etched with 2% nital, magnetic-particle inspection, and metallographic examination) supported the conclusion that the connecting rods were rendered susceptible to fatigue-crack initiation and propagation by the notch effect of coarse folds formed during the forging operation. One fracture was caused by fatigue resulting from operating stresses, and the other was a secondary tensile fracture. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001195
EISBN: 978-1-62708-227-3
Abstract
A connecting rod from a motor boat was broken in two places at the small end. At position I there was a fatigue fracture brought about by operational stress, whereas the fibrous fracture surface II was a secondary tensile fracture. Furthermore the transition on the other side of the rod was cracked symmetrically to the fatigue fracture (position III). Magnetic inspection showed indications of cracking at the transition between the rod and small end in six other connecting rods from the same batch. Metallographic investigation showed the connecting rods were rendered susceptible to fatigue by the notch effect of coarse scale-filled folds formed during forging.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001003
EISBN: 978-1-62708-227-3
Abstract
Gross wastage and embrittlement were observed in plain carbon steel desuperheaters in five new Naval power plants. The gross wastage could be duplicated in laboratory bomb tests using sodium hydroxide solutions and was concluded to be caused by free caustic concentrated by high heat flux. The embrittlement was shown to be caused by the flow of corrosion generated hydrogen which converted the cementite to methane which nucleated voids in the steel. A thermodynamic estimate indicated that a small amount of chromium would stabilize the carbides against decomposition by hydrogen in this temperature range, and laboratory tests with 2-14% Cr steel verified this.
Book Chapter
Corrosion-Fatigue Failure of a Bearing in a Marine Environment
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0047917
EISBN: 978-1-62708-227-3
Abstract
The support bearing of a hydrofoil vessel failed after only 220 h of operation. The bearing consisted of an outer ring made of chromium-plated AISI type 416 stainless steel and an inner ring with a spherical outer surface made of AISI type 440C stainless steel, with a plastic material, bonded to the outer ring, between the two. The inner ring was found to have failed in four places. The two metallic rings were allowed to come in contact with each other by the disappearance of the plastic material. It was revealed by examination of the fracture surfaces of the inner ring that the failure was caused by fatigue initiated in corrosion pits (caused by seawater). The fracture was found to be transgranular. It was recommended that the inner and outer rings should both be made from the more corrosion resistant 17-4 PH (AISI type 630) stainless steel.
Book Chapter
Stress-Corrosion Cracking of Aluminum Alloy Fittings in a Marine Atmosphere
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0091669
EISBN: 978-1-62708-227-3
Abstract
During a routine inspection, cracks were discovered in several aluminum alloy (similar to either 2014 or 2017) coupling nuts on the fuel lines of a missile. The fuel lines had been exposed to a marine atmosphere for six months while the missile stood on an outdoor test stand near the seacoast. A complete check was then made, both visually and with the aid of a low-power magnifying glass, of all coupling nuts of this type on the missile. Investigation (visual inspection, spectrographic and chemical analysis, and metallographic examination) supported the conclusion that the cracking of the aluminum alloy coupling nuts was caused by stress corrosion. Contributing factors included use of a material that is susceptible to this type of failure, sustained tensile stressing in the presence of a marine (chloride-bearing) atmosphere, and an elongated grain structure transverse to the direction of stress. The elongated grain structure transverse to the direction of stress was a consequence of following the generally used procedure of machining this type of nut from bar stock. Recommendations included changing the materials specification for new coupling nuts for this application to permit use of only aluminum alloys 6061-T6 and T651 and 2024-T6, T62, and T851.
Book Chapter
Fracture of the Low Carbon Steel Tail Shaft on a Tanker Ship
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001511
EISBN: 978-1-62708-227-3
Abstract
An LNG tanker experienced a fracture of the solid tail shaft, which is a section of the main drive shaft. The tail shaft was made of a forged low-carbon steel. In spite of two ultrasonic inspections, a large defect the size of a football in the center of the shaft was missed. During heat treating following forging, it was surmised that the defect led to the propagation of an internal brittle crack, or clink. A fatigue crack propagated from this origin to the outer surface of the shaft after about a year of service. Finally a last ligament of a few square inches held the shaft together and broke, leading to the separation of the shaft. The cause of failure was fatigue crack initiation and crack growth under reverse bending cyclic stresses. There was no indication that misalignment existed because there was no indication of fretting at the bolt holes in the flange at the end of the shaft. In the case of this shaft, a solution would have been to machine the core of the shaft to remove the brittle material or to use a tubular shaft.
Book Chapter
Use of XRD to Evaluate Cracks in Steel Cargo Tiedown Sockets
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0090639
EISBN: 978-1-62708-227-3
Abstract
Cracks initiating from the tip of the cloverleaf pattern in steel cargo tiedown sockets were observed by the builder following installation aboard several cargo vessels in various stages of construction. Testing of finite element models and measurements performed in the field on cargo ships with the cracking problem supported the conclusion that the failure was caused by overload. Additional testing showed that the overload failure and the transition from ductile to brittle fracture were facilitated by a combination of high brittleness due to flame cutting, increased hardness due to the cold-working coining process, and high residual stresses created by welding. Recommendations included the removal of the brittle, carbon-rich transformed martensite layer introduced by flame cutting and the application of a localized stress-relief heat treatment process. X-ray diffraction residual-stress measurements were then performed on heat treated tiedown sockets to verify the effectiveness of the localized heat treatment process applied.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001523
EISBN: 978-1-62708-227-3
Abstract
In TAKR 300 (Bob Hope) Class transport ships, the builder observed cracking of steel cloverleaf vehicle tie-down deck sockets following installation. Sockets were made from AH36 steel plate by flame cutting and cold coining, then submerged-arc welded to the shop deck. Cracks initiated from the tip of the cloverleaf pattern in >300 cases aboard several cargo vessels in various stages of construction. Consultants who analyzed the situation concluded that the problem may have been corrosion and hydrogen embrittlement. Three possible mechanisms of failure were considered: overload failure; fatigue fracture; and, environmentally-assisted cracking. Testing indicated overload failure was the cause. Remedial actions were taken to improve the fracture properties of the deck socket. A modified manufacturing process was developed involving milling and cutting instead of coining to round the comers of the flame-cut cloverleaf lobe. This new manufacturing process solved the problem.
Book Chapter
RMS Titanic: A Metallurgical Problem
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001591
EISBN: 978-1-62708-227-3
Abstract
On 14 April 1912, at 11:40 p.m., Greenland Time, the Royal Mail Ship Titanic on its maiden voyage was proceeding westward at 21.5 knots (40 km/h) when the lookouts on the foremast sighted a massive iceberg estimated to have weighed between 150,000 to 300,000 tons at a distance of 500 m ahead. Immediately, the ship’s engines were reversed and the ship was turned to port (left) in an attempt to avoid the iceberg. In about 40 sec, the ship struck the iceberg below the waterline on its starboard (right) side near the bow. The iceberg raked the hull of the ship for 100 m, destroying the integrity of the six forward watertight compartments. Within 2 h 40 min the RMS Titanic sank. Metallurgical examination and chemical analysis of the steel taken from the Titanic revealed important clues that allow an understanding of the severity of the damage inflicted on the hull. Although the steel was probably as good as was available at the time the ship was constructed, it was very inferior when compared with modern steel. The notch toughness showed a very low value (4 J) for the steel at the water temperature (-2 deg C) in the North Atlantic at the time of the accident.
Book Chapter
Investigation of a Failed Stainless Steel Spindle Assembly
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001703
EISBN: 978-1-62708-227-3
Abstract
This paper describes the metallurgical investigation of a broken spindle used to attach an antenna to the mast of a naval vessel. Visual inspections of both failed and intact fastener assemblies were carried out both on-board ship and in the laboratory followed by metallographic and fractographic examinations. Simulations were also performed on stressed material in a suitable environment to assess the relative importance of postulated failure mechanisms. Factors contributing to this failure including assembly procedures and applied preloads, service loading and environment, and material selection and specification. The discussion considers whether this failure was an isolated incident or is likely to be a fleet-wide problem, and suggests ways to prevent reoccurrence.
Book Chapter
Metallographic Studies of the U.S.S. Arizona
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001720
EISBN: 978-1-62708-227-3
Abstract
Metallographic studies found that steel used to fabricate the U.S.S. Arizona battleship during original construction, 1913-1915 and reconstruction, 1929-1931 were consistent with the best materials available during each time period. Due to the force of the forward magazine detonation, the best steel available today would not have had any impact on the outcome. Heavy banding in steels from both periods could adversely affect the corrosion resistance under anaerobic conditions that prevail during a corrosion cycle that has developed under hard biofouling layers for over 58 years. Banding would have no effect on corrosion rate under aerobic conditions that may occur in local areas on the hull. In the part of the ship from which samples for this report were obtained, high temperatures above 1340 deg F did not occur. Hull plate samples from the submerged wreckage are not yet available. These samples will be important to confirm findings to this time and determine the remaining thickness of the hull plate and, indirectly, the integrity of the fuel oil tanks.