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Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001779
EISBN: 978-1-62708-241-9
Abstract
Material samples collected from failed booster pumps were analyzed to determine the cause of failure and assess the adequacy of the materials used in the design. The pumps had been in service at a power plant, transporting feedwater from a deaerator to a main turbine boiler. Samples from critical areas of the pump were examined using optical and scanning electron microscopy, electrochemical analysis, and tensile testing. Based on microstructure and morphology, estimated corrosion rates, and particle concentrations in the feedwater, it was concluded that cavitation and erosion were the dominant failure mechanisms and that the materials and processes used to make the pumps were largely unsuited for the application.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001809
EISBN: 978-1-62708-241-9
Abstract
A brackish water pump impeller was replaced after four years of service, while its predecessor lasted over 40 years. The subsequent failure investigation determined that the nickel-aluminum bronze impeller was not properly heat treated, which made the impeller susceptible to aluminum dealloying. The dealloying corrosion was exacerbated by erosion because the pump was slightly oversized. The investigation recommended better heat treating procedures and closer evaluation to ensure that new pumps are properly sized.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001249
EISBN: 978-1-62708-236-5
Abstract
The flanged bearing bush carrying the drive shaft of a feed pump suddenly fractured after about two years of service. The chemical composition was normal for high chromium ledeburitic cast steel, which was corrosion and wear resistant as well as refractory. For unknown reasons the rotating shaft came into direct contact with the flange. Mechanical friction caused a rise in temperature on both contact surfaces. This mutual contact lasted long enough for the temperature in the contact zone to exceed 1200 deg C, at which the flange material became softened or molten. As a result, considerable structural changes took place on the inner wall of the flange. Thermal stresses and excessive mechanical loads due to smearing of the flange material then led to fracture of the flange.