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Dragline excavators
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001488
EISBN: 978-1-62708-236-5
Abstract
While an attempt was being made to start the diesel engine of a dragline type excavator, a severe explosion took place, the operator unfortunately being killed. The engine was normally started by compressed air from an air bottle or receiver charged to a pressure of 350 psi by a small auxiliary engine driven compressor fitted on the excavators. On an occasion when this had broken down, the air bottle was replenished by the engineer-in-charge from a cylinder of compressed air. The compressor engine remained unserviced and when the starting bottle again became depleted, the excavator operator re-charged it himself from another cylinder without the knowledge of the engineer. The engine was started satisfactorily, and the bottle charged again to 350 psi in readiness for the start on the following day. It was while an attempt was being made to start the engine on this occasion that the explosion took place. The cylinder used by the operator for re-charging the receiver contained not air but oxygen.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047428
EISBN: 978-1-62708-235-8
Abstract
A cast dragline bucket tooth failed by fracturing after a short time in service. The tooth was made of medium-carbon low-alloy steel heat treated to a hardness of 555 HRB. The fracture surface was covered with chevron marks. These converged at several sites on the surface of the tooth. A hardfacing deposit was located at each of these sites. Visual inspection of the hardfacing deposits revealed numerous transverse cracks, characteristic of many types of hardfacing. This failure was caused by cracks present in hardfacing deposits that had been applied to the ultrahigh-strength steel tooth. Given the small critical crack sizes characteristic of ultrahigh-strength materials, it is generally unwise to weld them. It is particularly inadvisable to hardface ultrahigh-strength steel parts with hard, brittle, crack-prone materials when high service stresses will be encountered. The operators of the dragline bucket were warned against further hardfacing of these teeth.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0047474
EISBN: 978-1-62708-221-1
Abstract
A 10-cm (4-in.) chain link used in operating a large dragline bucket failed after several weeks in service. The link was made of cast low-alloy steel (similar to ASTM A487, class 10Q) that had been normalized, hardened, and tempered to give a yield strength of approximately 1034 MPa (150 ksi). A hydrogen flake approximately 5 cm (2 in.) in diam was observed at the center of the fracture surface. Beach marks indicative of fatigue encircled the hydrogen flake and covered nearly all of the remaining fracture surface. The failure of this linkways caused by an excessive hydrogen content. Two steps were taken to combat this type of failure. First, when service conditions did not require high hardness to combat wear, the links were produced of a steel having a yield strength of about 690 MPa (100 ksi) rather than 1034 M
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001472
EISBN: 978-1-62708-221-1
Abstract
Severe damage to the jib of a dragline excavator resulted from failure of the shaft which carried the derricking sheaves at the apex of the "A" frame. Failure occurred within the hub of the center sheave of the group of three at the right-hand end of the shaft. The shaft was manufactured from a 0.5% carbon, 1% chromium steel heat treated to give a hardness value of 300 VDP. The material was in the hardened and tempered condition and showed no abnormalities which would predispose to early failure. The content of non-metallic matter was only of nominal amount. Failure of the shaft resulted from fatigue due to the cumulative action of the repeated stresses which it had been subjected to during service. The shaft had been subjected to repeated stress applications sufficient to result in the initiation and development of a fatigue crack at the radial hole. To prevent a repetition of the failure it was recommended that the stress-raising effect of the holes be reduced by chamfering or preferably rounding-off the edges. Furthermore, rotation of the shaft should be prevented so that the radial holes were positioned on the opposite side of the shaft.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001524
EISBN: 978-1-62708-221-1
Abstract
A 140 ft. (42.7 m) long boom on a dragline crane used in coal strip-mining operations failed. One of the principal load-bearing longitudinal beams or chords of the trussed boom had fractured adjacent to a bolt hole at a location about halfway along the length of the boom. Over the lifetime of the crane, several repairs had been made to the boom. At least a year before the failure, a reinforcing gusset plate had been bolted and welded to this chord at this location. Stereomicroscopy revealed microcracks in the weld metal. A fatigue crack 45 mm (1.8 in.) long was observed to emanate from this microcrack. Scanning electron microscopy showed an overload crack extended across the remaining cross section of the chord. It was concluded that the presence of the bolt hole used to attach the gusset plate to the chord created a stress riser adjacent to the hole. Repeated high tensile stresses on the chord during the lifting of enormous loads initiated a fatigue crack in the weld region adjacent to the bolt hole.