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Pipe joints
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Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001774
EISBN: 978-1-62708-241-9
Abstract
A ring-type joint in a reactor pipeline for a hydrocracker unit had failed. Cracks were observed on the flange and the associated ring gasket during an inspection following a periodic shutdown of the unit. The components were manufactured from stabilized grades of austenitic stainless steel; the flange from type 321, and the ring gasket from 347. Examination revealed that the failure occurred by transgranular stress-corrosion cracking, initiated by the presence of polythionic acid. Detailed metallurgical investigation was subsequently conducted to identify what may have caused the formation of polythionic acid in the process gas.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001586
EISBN: 978-1-62708-228-0
Abstract
On 9 March 2000, a gasoline pipeline failed near Greenville, TX releasing approximately 12,000 barrels of fuel. After the on-scene portion of the investigation was completed, an 8.5 ft. (2.6 m) section of the 28 in. (71 cm) diam pipe was sent to the materials laboratory for examination. Examination included optical and scanning electron microscopy of the fracture surfaces and metallographic examination of cross sections through the fracture surface. From the outer to inner edge of the fracture surface, three different areas were observed. Fracture features in area 1 were obliterated by corrosion. The fracture features in region 2 were relatively smooth, and striations were observed, typical of fatigue. In region 3, dimple features were observed, typical of ductile overstress. Also, corrosion pits were observed on the outer surface of the pipe section in locations where the protective black tar-like coating was cracked.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0046252
EISBN: 978-1-62708-229-7
Abstract
A type 321 stainless steel bellows expansion joint on a 17-cm (6 in.) OD inlet line (347 stainless) in a gas-turbine test facility cracked during operation. The line carried high-purity nitrogen gas at 1034 kPa (150 psi) with a flow rate of 5.4 to 8.2 kg/s (12 to 18 lb/s). Cracking occurred in welded joints and in unwelded portions of the bellows. The bellows were made by forming the convolution halves from stainless steel sheet, then welding the convolutions together. Evidence from visual examination, liquid penetrant inspection chemical analysis, hardness tests, and metallographic examination of sections etched with Vilella's reagent supports the conclusions that failure of the bellows occurred by intergranular fatigue cracking. Secondary degrading effects on the piping existed as well. Recommendations included the acceptability of Type 321 stainless steel (provided open-cycle testing does not result in surface oxidation and crevices) Although type 347 stainless steel would be better, and Inconel 600 would be an even better choice. Welds would also need modified processing for reheating and annealing. Prevention of oil leakage into the system would minimize carburization of the piping and bellows.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001682
EISBN: 978-1-62708-229-7
Abstract
The secondary cooling water system pressure boundary of Savannah River Site reactors includes expansion joints utilizing a thin-wall bellows. While successfully used for over thirty years, an occasional replacement has been required because of the development of small, circumferential fatigue cracks in a bellows convolute. One such crack was recently shown to have initiated from a weld heat-affected zone liquation microcrack. The crack, initially open to the outer surface of the rolled and seam welded cylindrical bellows section, was closed when cold forming of the convolutes placed the outer surface in residual compression. However, the bellows was placed in tension when installed, and the tensile stresses reopened the microcrack. This five to eight grain diameter microcrack was extended by ductile fatigue processes. Initial extension was by relatively rapid propagation through the large-grained weld metal, followed by slower extension through the fine-grained base metal. A significant through-wall crack was not developed until the crack extended into the base metal on both sides of the weld. Leakage of cooling water was subsequently detected and the bellows removed and a replacement installed.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0048747
EISBN: 978-1-62708-229-7
Abstract
A 455 mm diam x 8 mm thick wall carbon steel (ASTM A 53) discharge line for a circulating-water system at a cooling tower fractured in service; a manifold section cracked where a Y-shaped connection had been welded. Investigation (visual inspection and photographs) supported the conclusion that the pipe failed by fatigue. Cracks originated at crevices and pits in the weld area that acted as stress raisers, producing high localized stresses because of the sharp-radius corner design. Abnormally high structural stresses and alternating stresses resulting from the pump vibrations contributed to the failure. Recommendations included changing the joint design to incorporate a large-radius corner and improving fitting of the components to permit full weld penetration. Backing strips were suggested to increase weld quality, and the pipe wall thickness was increased from 8 to 9.5 mm.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001652
EISBN: 978-1-62708-220-4
Abstract
Three separate corrosion mechanisms were involved in the failure of an AISI type 304 stainless steel pipe elbow. The major cracks, including the one that penetrated the wall, tend to be wide-mouthed, tapering to a blunt tip, with corrosion products filling much of the crack space. This was characteristic of corrosion fatigue. The second type of cracking originated at some of the major cracks. These cracks were branched and transgranular, which is characteristic of stress-corrosion caused by chlorides. The third crack mode, an intergranular network, was most probably the result of hydrogen sulphide attack. The 13-year service life of the elbow made it difficult, if not impossible, to determine the order of the corrosion mechanisms or the length of time it took to reach the present state of degradation after the initiation of corrosion. Based on the long service life the present material has given, it was recommended that it be used again.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001441
EISBN: 978-1-62708-220-4
Abstract
Soft-soldered copper pipe joints used in refrigerating plants failed. The solder had not adhered uniformly to the pipe surface. In addition, there were some longitudinal grooves on the pipe surfaces, parts of which were not filled with solder. The unsoldered areas formed cavities within the joints, some of which had been in direct communication with the outsides via the grooves or interconnected cavities. On cooling, moisture condensed on the external surfaces. Some of this was drawn by capillary action into the cavities in open communication with the external surface. On continued cooling to below freezing-point, water that entered the cavities solidified. This was accompanied by a slight increase in volume, which collapsed the pipe walls. In the examples, the pipe ends had not been properly tinned. The solder used was found to be of the tin-antimony type, containing about 5% antimony, which is more difficult to use than the usual tin-lead alloys. The use of this particular type of solder was a contributory factor in the production of unsound joints in the samples examined.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001324
EISBN: 978-1-62708-215-0
Abstract
A type 430Ti stainless steel flue gas expansion joint cracked because of caustic-induced stress-corrosion cracking. Energy-dispersive X-ray spectroscope analysis of the fracture surface deposits revealed the presence of sodium and potassium—caustics in hydroxide form. Primary fracture surfaces were all similar in appearance, and a primary crack origin could not be identified. A secondary crack brought to fracture in the laboratory showed brittle, cleavage features rather than classic, tensile overload features. This suggested that the material was embrittled.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001342
EISBN: 978-1-62708-215-0
Abstract
A type 321 stainless steel downcomer expansion joint that handled process gases was found to be leaking approximately 2 to 3 weeks after installation. The expansion joint was the second such coupling placed in the plant after failure of the original bellows. The failed joint was disassembled and examined to determine the cause of failure. Energy-dispersive x-ray analysis revealed significant peaks for chlorine and phosphorus, indicating failure by chloride stress-corrosion cracking (SCC). Cracks in the liner and bellows exhibited a branched pattern also typical of SCC. Cracks through the inner liner initiated on the outer surface of the liner and propagated inward, whereas cracks in the bellows originated on the inner surface and propagated outward. Stress-corrosion cracking of the assembly was caused by chloride contaminants trapped inside the bellows following hydrostatic testing. Checking the test fluid for chloride and removing all fluids after hydrostatic testing were recommended to prevent further failure.