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Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001775
EISBN: 978-1-62708-241-9
Abstract
A bent Ni-Cu Monel 400 alloy tube, which operated as part of a pipeline in a petrochemical distillery, failed by through-thickness cracking. The pipeline was used to carry a stream of gaseous hydrocarbons containing hydrochloric acid (HCl) into a reaction tower. The tower provided a caustic solution (NaOH) to remove HCl from the stream, before the latter was directed to a burner. Metallographic examination showed that the cracks were intergranular and were frequently branched. Although nominal chemical composition of the component was found within the specified range, energy dispersive x-ray analysis (EDXA) indicated significant segregation of sulfur and chlorine along the grain boundaries. Failure was attributed to hypochlorous-acid (HClO)-induced stress-corrosion cracking (SCC). The HClO was formed by the reaction of HCl with atmospheric O 2 that entered the tube during shutdowns and startups. Residual stresses, originating from in situ bend forming of the tube during assembly of the line, provided a driving force for crack growth, and the segregation of sulfur on grain boundaries made the material more susceptible to cracking.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001407
EISBN: 978-1-62708-220-4
Abstract
The onset of leakage adjacent to two butt welds in a 2 in. bore pipe was traced to the development of fine cracks. The pipe carried 40% sodium hydroxide solution. The actual temperature was not known, but the pipeline was steam traced at a pressure of 30 psi, equivalent to a temperature of 130 deg C (266 deg F). Magnetic crack detection revealed circumferential crack-like indications situated a short distance from the butt weld. Cracking originated on the bore surfaces of the tube and was of an intergranular nature reminiscent of caustic cracking in steam boilers. The strength of the solution of caustic soda and possibly the temperature also were in the range known to produce stress-corrosion cracking of mild steels in the presence of stresses of sufficient magnitude. In this instance the location of the cracking suggested that residual stresses from welding, which approach yield point magnitude, were responsible. As all other welds were suspect, the remedy was to remove the joints and to reweld followed by local stress relief.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001711
EISBN: 978-1-62708-229-7
Abstract
Failures of 10Cr-Mo9-10 and X 20Cr-Mo-V12-1 superheated pipes during service in steam power generation plants are described. Through micrographic and fractographic analysis, creep and overheating were identified as the cause of failure. The Larson-Miller parameter is computed, as a function of oxidation thickness, temperature and time, confirming the creep failure diagnostic.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c9001565
EISBN: 978-1-62708-230-3
Abstract
A stainless steel pipe transferring hot white liquor solution of sodium hydroxide and sodium sulfite, developed leaks adjacent to the welds within four years of service. The stainless steel pipe was AISI type 304 and welded with E308 weld electrodes. The service temperature was 190 deg C (375 deg F) and the solution contained approximately 700 ppm chlorides. Liquid penetrant inspection of the pipeline showed the leaks were numerous and confined adjacent to the welds. A metallographic specimen from the circumferential weld showed the cracks initiated at the inside surface. In addition to the base metal, SCC also had initiated at a notch at the weld root due to improper welding procedures. Failure was attributed to chloride-induced SCC with secondary contributory factors, including improper welding procedures. It was recommended that the pipeline be replaced with a material more resistant to SCC. The candidate materials are commercial grade unalloyed titanium or Inconel 600, which have superior resistance to SCC compared to austenitic stainless steels.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c9001564
EISBN: 978-1-62708-230-3
Abstract
An 8 in. diam stainless steel black liquor feed pipe to a carbon steel digester had failed within one year of service. The material was type 316 molybdenum-containing austenitic stainless steel. The service environment was alkaline black liquor at 175 deg C (350 deg F). The pipe had developed cracks on the inside surface coincident with an external support gusset. The cracks initiated at wide corrosion grooves. The early stages were corrosion-assisted fatigue cracks. The cracks initiated at the corrosion grooves and propagated as transgranular SCC with characteristic branching. Evaluation indicated the cracks were localized in an area of high cyclic stresses as a consequence of geometrical constraints on the piping and unsupported cantilever loads. No cracks were found elsewhere in the pipe. In the absence of highly localized service stresses (exceeding yield strength of the material), the corrosion grooving and subsequent SCC would not have occurred in this service environment. The pipe support system was modified with additional gussets to reduce the magnitude of cyclic stresses at the critical areas. The modification was apparently successful.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001233
EISBN: 978-1-62708-232-7
Abstract
High-chromium steel pipes 42.25 x 3.25 mm from a blast furnace gas fired recuperator for the preheating of air were heavily oxidized and perforated in places. It was found that the blast furnace gas had a high sulfur content. Both the carburization and the formation of sulfide proved that in addition, from time to time at least, combustion was incomplete and the operation was carried out in a reducing atmosphere, with the result that oxygen deficiency prevented the formation or maintenance of a protective surface layer on the external surface of the pipes. The sulfur would probably not have damaged the nickel-free steel used here at the given temperatures if it had been present as sulfur dioxide in an oxidizing atmosphere. The damage was therefore caused primarily by an incorrectly conducted combustion process.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0089617
EISBN: 978-1-62708-232-7
Abstract
A forged 4130 steel cylindrical permanent mold, used for centrifugal casting of gray- and ductile-iron pipe, was examined after pulling of the pipe became increasingly difficult. In operation, the mold rotated at a predetermined speed in a centrifugal casting machine while the molten metal, flowing through a trough, was poured into the mold beginning at the bell end and ending with the spigot end being poured last. After the pipe had cooled, it was pulled out from the bell end of the mold, and the procedure was repeated. Investigation supported the conclusion that failure of the mold surface was the result of localized overheating caused by splashing of molten metal on the bore surface near the spigot end. In addition, the mold-wash compound (a bentonite mixture) near the spigot end was too thin to provide the proper degree of insulation and to prevent molten metal from sticking to the bore surface. Recommendations included reducing the pouring temperatures of the molten metal and spraying a thicker insulating coating onto the mold surface.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001714
EISBN: 978-1-62708-232-7
Abstract
In a HyL III heat exchanger's radiant pipes, metal dusting reduced the pipe thickness from 8.5 to 3 mm in just nine months, leaving craters on the inner surface. The pipes are fabricated from HK 40 alloy. The heated gas (400 to 800 deg C) consisted of CO, CO2, and H2, with a 4:1 CO/CO2 ratio. Metallographic investigations revealed that the surface of the attacked pipes consisted of (Cr, Fe) carbide. The metal dusting was the result of a decomposition process (CO to CO2 + C) that deposited C on the pipe surface. Because of the high temperature, the C subsequently diffused through the surface oxide layer (Cr2O3), triggering a succession of reactions that led to pitting and the formation of craters.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001240
EISBN: 978-1-62708-234-1
Abstract
A heat exchanger made of a pipe in which oil was heated from the outside from approximately 90 deg C to 170 deg C, by superheated steam of about 8 to 10 atmospheres had developed a leak at the rolled joint of the pipe and pipe bottom. The pipes were supposed to be made from St 35.29 steel and annealed at the rolled joint to 100 mm length. The outer pipe surface was strongly pitted by corrosion all around the rolled joint. In the vicinity of the steam chamber the pipe wall had oxidized through from the exterior to the interior at one spot. Adjoining this spot, grooves caused by erosion were noticeable. This was a typical case of crevice corrosion. The rolled joint evidently was not entirely tight, so that saturated steam condensate could penetrate into the gap.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001276
EISBN: 978-1-62708-215-0
Abstract
The carbon steel feedwater piping at a waste-to-energy plant was suffering from wall thinning and leaking after being in service for approximately six years. Metallographic examination of ring sections removed front the piping revealed a normal microstructure consisting of pearlite and ferrite. However, the internal surface on the thicker regions of the rings exhibited significant deposit buildup, where the thinned regions showed none. No significant corrosion or pitting was observed on either the internal or external surface of the piping. The lack of internal deposits on the affected areas and the evidence of flow patterns indicated that the wall thinning and subsequent failure were caused by internal erosion damage. The exact cause of the erosion could not be determined by the appearance of the piping. Probable causes of the erosion include an excessively high velocity flow through the piping, extremely turbulent flow, and/or intrusions (weld backing rings or weld bead protrusions) on the internal surface of the pipes. Increasing the pipe diameter and decreasing the intrusions on the internal surface would help to eliminate the problem.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001043
EISBN: 978-1-62708-214-3
Abstract
A 76 mm (3 in.) type 304 stainless steel tube that was used as a heat shield and water nozzle support in a hydrogen gas plant quench pot failed in a brittle manner. Visual examination of a sample from the failed tube showed that one lip of the section was eroded from service failure, whereas the opposite side exhibited a planar-type fracture. Sections were removed from the eroded area and from the opposite lip for microscopic studies and chemical analysis. The eroded edges exhibited river bed ditching, indicative of thermal fatigue. Microstructural analysis showed massive carbide formations in a martensite matrix and outlining of prior-austenite grains by a network of fine, white lines. These features indicated that the material had been transformed by carburization by the impinging gas. The outer surface exhibited a heavy scale deposit and numerous cracks that originated at the surface of the tube. The cracks were covered with scale, indicating that thermal fatigue (heat cracking) had occurred. Chemical analysis confirmed that the original material was type 304 stainless steel that had been through-carburized by the formation of an endothermic gas mixture. It was recommended that plant startup and shutdown procedures be modified to reduce or eliminate the presence of the carburizing gas mixture.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001064
EISBN: 978-1-62708-214-3
Abstract
Several hundred leaks were reported in the type 304 stainless steel pipelines, vessels, and tanks of a chemical plant at a tropical location within a few weeks after startup. Investigation of the failure involved a site visit, metallographic examination and analysis of the material, analysis of hydrotest waters, and microbiological examination of slime that had formed in certain pipework sections. It was determined that the failure resulted from microbially induced corrosion promoted by the use of poor-quality hydrotest water and uncontrolled hydrotesting practice. Use of appropriate hydrotesting procedures was recommended to prevent similar failures.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001067
EISBN: 978-1-62708-214-3
Abstract
The source of cracking in the circumferential weld seam in a JIS-SM50B carbon-manganese steel pipe used in a CO2 absorber was investigated, the absorber had been in service for 18 years. The seam had been weld-repaired twice, and the repair welds had been locally stress relieved. Longitudinal seams in the same vessel, which had been stress relieved in a furnace, showed no tendency toward cracking. The solution passing through the vessel contained CO2-CO-H20, KHCO, and Cl− ions. Nondestructive testing revealed that the cracks originated in the heat-affected zone and propagated into the base metal and weld. Severe branching of the cracks characteristic of stress-corrosion cracking was observed. Microexamination revealed that crack propagation was transgranular further supporting the possibility of stress-corrosion cracking. Simulation tests carried out in the vessel confirmed this mode of cracking. It was recommended that weld seams be furnace heat treated at a temperature of 600 to 640 deg C (1110 to 1180 deg F) for a minimum of 1 h per inch of section thickness.