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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001206
EISBN: 978-1-62708-235-8
Abstract
A number of seamless pipe nipples of 70 mm diam and 3.5 mm wall thickness made of steel type 35.8 were oxyacetylene welded to collectors of greater wall thickness with a round bead. X-ray examination showed crack initiation in the interior of the nipples close to the root of the weld seam. The cracks only appeared where the originally deposited bead was remelted in the regions of overlap. Given the construction and welding technique used, it would have been preferable to make the nipples of a steel lower in sulfur content. However, by taking advantage of all the potential in shaping and welding technology, it should be possible to prevent crack formation with steel type 35.8 of normal composition.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0089734
EISBN: 978-1-62708-235-8
Abstract
A system of carbon steel headers, handling superheated water of 188 deg C (370 deg F) at 2 MPa (300 psi) for automobile-tire curing presses, developed a number of leaks within about four months after two to three years of leak-free service. All the leaks were in shielded metal arc butt welds joining 200 mm (8 in.) diam 90 deg elbows and pipe to 200 mm (8 in.) diam welding-neck flanges. A flange-elbow-flange assembly and a flange-pipe assembly that had leaked were removed for examination. Investigation (visual inspection, hardness testing, chemical analysis, magnetic-particle testing, radiographic inspection, and 2% nital etched 1.7x views) showed varying IDs on the assemblies and supported the conclusions that the failures of the butt welds were the result of fatigue cracks caused by cyclic thermal stresses that initiated at stress-concentrating notches at the toes of the interior fillet welds on the surfaces of the flanges. Recommendations included using ultrasonic testing to identify the appropriate joints and then replacing them. Special attention to accuracy of fit-up in the replacement joints was also recommended to achieve smooth, notch-free contours on the interior surfaces.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001190
EISBN: 978-1-62708-235-8
Abstract
Brass pipe couplings submitted for examination were deep-drawn from disks then annealed and subsequently cold threaded. Chemical analysis confirmed that the specified alloy Ms 63 was used for fabrication. Some of the pipe already showed fine cracks prior to their installation. In most cases however the cracks were detected after a certain period of operation. The intercrystalline course of the cracks indicated stress-cracking as it often appears in brass after heavier cold deformation. The splitting of the couplings could have been avoided by a tempering heat treatment at temperatures between 230 and 300 deg C after rolling the threads. This procedure would have reduced the internal stresses while maintaining strengthening gained by the cold deformation.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091806
EISBN: 978-1-62708-219-8
Abstract
A failure occurred in buried brass (92% Cu, 8% Zn) piping used to carry drinking water in wet clay soil after less than two years in service. Investigation (visual inspection, chemical analysis of both the pipe surface and water, and a comparison of the corrosion failure of power station condenser tubing cooled by seawater for two copper alloys, an aluminum brass alloyed with arsenic (UNS C68700, ASTM B111, or Cu-Zn-20Al DIN17660), and a cupronickel 70-30 alloy with iron added (C71500, ASTM B111, or Cu-Ni-30Fe DIN17665)) supported the conclusion that the failure was caused by microbial induced corrosion by sulfate-reducing bacteria. No recommendations were made.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091292
EISBN: 978-1-62708-219-8
Abstract
A 25 mm (1 in.) copper coupling had been uniformly degraded around most of the circumference of the bell and partially on the spigot end. One penetration finally occurred through the thinned area on the spigot end of the pipe. Investigation supported the conclusion that although the pipe was buried in noncorrosive sandy soil, it was found to incur stray currents at 2 Vdc in relation to a Cu/CuSO4 half cell. Recommendations included eliminating, moving, or shielding the source of stray current.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001017
EISBN: 978-1-62708-219-8
Abstract
A 10-in. diam, spiral-welded AISI 1020 carbon steel pipe carrying water under pressure developed numerous leaks over a four mile section. The section was fabricated using submerged-arc welding from the outside surface. Each welded length of pipe had been subjected to a proof pressure approximately twice the specified design pressure and two-thirds the approximate yield point of the parent metal. No failures or leakage were observed during proof testing. Metallurgical examination corroborated visual checks, indicating a distinct lack of root penetration in the split areas. Splitting occurred as a result of inadequate root penetration. The most likely source of difficulty in the welding process was the linear speed. Probably, the failures would not have occurred in absence of the welding problem. Also, the pipe was inadequate for the specified design pressure, as well as the reported maximum system pressure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091378
EISBN: 978-1-62708-219-8
Abstract
A 12.7 mm (0.5 in.) diam tube was removed from a potable water supply due to leaks. The tube wall thickness was 0.711 mm (0.028 in.) with a thin layer of chromium plate on the OD surface. The tube had been in service for approximately 33 years. Investigation (visual inspection, EDS deposit analysis, metallurgical examination, and unetched magnified images) supported the conclusion that failure occurred due to porous material typical of plug-type dezincification initiating from the inside surface. Where the dezincification had progressed through the tube wall, the chromium plate had exfoliated from the base material and cracked. Recommendations included replacing the piping with a more corrosion-resistant material such as red brass (UNS C23000), inhibited Admiralty brass (UNS C44300), or arsenical aluminum brass (UNS C68700).
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001168
EISBN: 978-1-62708-219-8
Abstract
Steel pipes, used for years in a food factory soft water preheater, were found to leak as a result of corrosion. The pipes, made of 18/8 steel, were immersed in steam maintained at 0.5 atm and 150 deg C. They carried desalinated process water, heating it to approximately 100 deg C. Inspection revealed a reddish-brown coating on the outside of the pipe with a few flat pitting holes and incipient cracks. Corrosion was also observed on the inner walls of the pipe, consisting of rust patches with pitting scars, branching out to predominantly transcrystalline cracks. In this case, leaking appears to be the result of a combination of pitting and stress corrosion, most likely due to chlorides. The factory was recommended to use molybdenum-alloyed steels (type 18/10 or 18/12) which are more resistant to local disruption of passivating films and pitting than molybdenum-free types such as 18/8.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001653
EISBN: 978-1-62708-219-8
Abstract
After six years of service, three water shut-off valves on a copper water line in a residential building were found to be inoperative. Macroscopic examination of the valves after disassembly revealed that all three failed at the key that holds the spindle in the gate. In addition, the color near the key changed from yellow to red-brown. The gate was made from leaded red brass (85-5-5-5) while the spindle was made from silicon brass. It was concluded that the valves failed by dezincification resulting from bimetallic galvanic corrosion. It is common in the valve industry to use components made of different alloys in the same valve, but this is not the best approach for all applications.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0047335
EISBN: 978-1-62708-219-8
Abstract
A section of cast iron water main pipe contained a hole approximately 6.4 x 3.8 cm (2.5 x 1.5 in.). The pipe was laid in clay type soil. Examination revealed severe pitting around the hole and at the opposite side of the outside diam. A macroscopic examination of a pipe section at the hole area showed that the porosity extended a considerable distance into the pipe wall. Metallographic examination revealed a graphite structure distribution expected in centrifugally cast iron with a hypoeutectic carbon equivalent. Chemical analyses of a nonporous sample had a composition typical of cast iron pipe. Chemical analyses of the porous region had a substantial increase in carbon, silicon, phosphorus, and sulfur. The porous appearance and the composition of the soft porous residue confirmed graphitic corrosion. The selective leaching of iron leaves a residue rich in carbon, silicon, and phosphorus. The high sulfur content is attributed to ferrous sulfide from a sulfate reducing bacteria frequently associated with clay soils. Reinforced coal tar protective coating was recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091384
EISBN: 978-1-62708-219-8
Abstract
A 25.4 cm (10 in.) diam gray cast iron water main pipe was buried in the soil beneath a concrete slab. The installation was believed to have been completed in the early 20th century. A leak from the pipe resulted in flooding of a warehouse. Once removed, the pipe revealed through-wall perforations and cracking along its axis. The perforations and the crack were at the 6 o'clock position. Investigation (visual inspection, radiography, unetched macrographs, and tensile testing) supported the conclusion that the failure occurred as result of years of exposure to ground water in the soil resulting in graphitic corrosion. Soils containing sulfates are particularly aggressive. Recommendations included pipe replacement. The wall thickness had been sufficiently reduced that the pipe could no longer support the required load. Water mains are designed for more than 100 years life. Ductile iron or coated and lined steel pipe, generally not susceptible to graphitic corrosion, were suggested as suitable replacement materials, and cathodic protection was also considered as a possibility.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001697
EISBN: 978-1-62708-219-8
Abstract
Corrosion in potable and nonpotable water systems has been well documented in the past, and new research discusses innovations in water treatment and materials that are designed to enhance the quality of a water system, whether commercial or residential. This paper is a collection of five case histories on the failure of copper and steels as used in potable and non-potable water systems. The case histories cover a range of applications in which copper and steel products have been used. Copper and steel pipes are the two most commonly used materials in residential, commercial and industrial applications. The projects that are discussed cover these three important applications. The purpose of presenting this information is to allow the reader to gain an understanding of real life corrosion issues that affect plumbing materials, how they should have been addressed during the design of the water system, and how a water system should be maintained during service. We share this information in the hope that the reader will gain some limited knowledge of the problems that exist, and apply that knowledge in designing or using water systems in day-to day life.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001701
EISBN: 978-1-62708-219-8
Abstract
A closed-loop hot water heating system at a museum in South Carolina was the subject of failure evaluation. The system consisted of plain carbon steel pipes (Schedule 40) made of ASTM A 106 or A 53 (ERW or seamless). The supply and return lines were made of the same materials. The fittings were mechanically threaded assemblies. Temperatures ranged from 150 to 155 deg F (65.6 to 68.3 deg C). Leaks in the system had reportedly initiated immediately after the building had been placed in service. The cause of corrosion inside the steel pipes was attributed to tuberculation caused by oxygen concentration cells and oxygen-pitting related corrosion. Both types of corrosion are due to the poor quality of the water and the lack of corrosion control in the water system.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c0048698
EISBN: 978-1-62708-228-0
Abstract
Wet natural gas was dried by being passed through a carbon steel vessel that contained a molecular-sieve drying agent. The drying agent became saturated after several hours in service and was regenerated by a gas that was heated to 290 to 345 deg C in a salt-bath heat exchanger. The tee joint in the piping between the heat exchanger and the sieve bed failed after 12 months. A hole in the tee fitting and a corrosion product on the inner surface of the pitting was revealed by visual examination. Iron sulfide was revealed by chemical analysis of the scale which indicated hydrogen sulfide attack on the carbon steel. The presence of oxygen was indicated by the carbon and sulfur found in the scale on the piping and in the sieves indicated that oxygen combined with moisture produced conditions for attack of hydrogen sulfide on carbon steel. Turbulence with some effect from the coarse grain size was interpreted to have contributed. The piping material was changed from carbon steel to AISI type 316 stainless steel as it is readily weldable and resistant to corrosion by hydrogen sulfide.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048318
EISBN: 978-1-62708-234-1
Abstract
A resistance-welded carbon steel superheater tube made to ASME SA-276 specifications failed by pitting corrosion and subsequent perforation, which caused the tube to leak. The perforation was found to have occurred at a low point in a bend near the superheater outlet header. It was found that the low points of the superheater tubes could not be completely drained during idle periods. Water-level marks were noticed on the inside surface above the area of pitting. It was revealed by microscopic examination that localized pitting had resulted from oxidation. It was concluded that water contained in the tube during shutdowns had accumulated and cumulative damage due to oxygen pitting resulted in perforation of one of the tubes. Filling the system with condensate or with treated boiler water was suggested as a corrective action. Alkalinity was suggested to be maintained at a pH of 9.0 and 200 ppm of sodium sulfite should be added to the water.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048361
EISBN: 978-1-62708-234-1
Abstract
Several failures occurred in 64-mm schedule 80 type 304 stainless steel (ASME SA-312, grade TP304) piping in a steam-plant heat-exchanger system near tee fittings at which cool water returning from the heat exchanger was combined with hot water from a bypass. Various portions of the piping were subjected to temperatures ranging from 29 to 288 deg C. Each of the failures were revealed to consist of transgranular cracking in and/or close to the circumferential butt weld joining the tee fitting to the downstream pipe leg, where the hot bypass water mixed with the cool return water. The transgranular cracks suggested that thermal fatigue was a more likely cause of failure than SCC. It was concluded by temperature measurements that circumferential temperature gradients, in combination with inadequate flexibility in the piping system as a whole, had caused the failures. The tee fitting was redesigned to alleviate the thermal stress pattern.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001699
EISBN: 978-1-62708-234-1
Abstract
A shopping mall in South Carolina was originally constructed in 1988 and a second phase completed in 1989. The HVAC system inside the mall included an open, recirculating condenser water loop that served various fan coil units located within tenant spaces. The system had a recirculating capacity of about 44,000 gal (166,000 L) of water. It consisted primarily of steel pipes fitted with threaded connectors on the 2 in. (46 cm) pipes and bolted flanged couplings on the larger pipes. Seven years following the completion of the mall, corrosion problems were noted at the outer and inner surfaces of the pipe. Visual observations on the inner diametral surfaces revealed that the pipes were, in almost all cases, filled with corrosion products. A significant amount of base metal loss was documented in all of the samples. The cause of the observed corrosion was determined to be a lack of corrosion monitoring and poor water quality. Pipe replacement and a regular water testing program were recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001227
EISBN: 978-1-62708-235-8
Abstract
An elbow of 70 mm OD and 10 mm wall thickness made from St 35.29, and exposed to 315 atmospheres internal pressure in an oil hydraulic shear installation, cracked lengthwise after a short operating period. Because the stress was not sufficient to explain the fracture of this elbow under this pressure, an investigation was conducted to establish whether material or processing errors had occurred. Microscopic examination showed that a ferritic-pearlitic structure in select locations was very fine-grained. Other signs of fast cooling as compared to normally formed structure of the core zone were noted. It was also possible that the pipe was resting on a cold plate during bending or that it came in touch with a cold tool. This apparently caused the strains at the transition to the cross-sectional part that had been cooled more slowly. The location of the crack at just this point gave rise to the conclusion that it was formed either by the sole or contributive effect of these stresses.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001421
EISBN: 978-1-62708-235-8
Abstract
The bottom flange of a vertical pipe coupled to an isolating valve in a steam supply line to a turbine failed. Steam pressure was 1,500 psi and the temperature 416 deg C (780 deg F). Multiple cracking occurred in the bore of the flange. A quarter-segment was cut out and examined. The cracks were located in the part of the flange that formed a continuation of the pipe bore. The majority of them originated at the end of the flange bore and extended axially along the pipe and radially across the flange face. Magnetic crack detection revealed a further number of cracks in the weld deposit. While the fracture in the weld metal was of the ductile type exhibiting a fine fibrous appearance, that in the flange material was of the cleavage type. Microscopic examination revealed that the cracks were blunt-ended fissures of the type characteristic of corrosion-fatigue. It was concluded that cracking was due to corrosion-fatigue, which arose from the combined effect of a fluctuating tensile stress in the presence of a mildly corrosive environment.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001234
EISBN: 978-1-62708-232-7
Abstract
In a copper hot water system, a bent pipe was soldered into a straight pipe with twice the diameter. The neighborhood of the soldered joint was covered with corrosion product predominantly blue-green in color, presumably carbonates. When these corrosion products were scratched off it was seen that the copper beneath this layer had not suffered noticeable attack. The object of the examination was the localized deep cavities located almost symmetrically to both sides of the inserted end of the narrower tube on the internal wall of the wider tube which had in one place been eaten right through. The symmetrical location on each side of the point of insertion of the narrower pipe and the localized sharp delineation of the attack indicated erosion due to the formation of turbulence. By avoiding sharp transitions and abrupt changes in cross section it is possible to design the pipe work so that localized turbulence is obviated. Degassing and cleansing of the water also would reduce the danger of erosion particularly in the case of softened water, which takes up oxygen and carbon dioxide very readily thus becoming particularly aggressive.
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