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Masts and towers
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Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001766
EISBN: 978-1-62708-241-9
Abstract
During the installation of power transmission lines across a major interstate highway, a temporary anchor stabilizing one of the poles failed, resulting in the loss of the pole and the associated power lines. It also contributed to a single vehicle incident on the adjacent roadway. Post-failure analysis revealed that the fracture was precipitated by a preexisting weld-related crack. Closed form and numerical stress analyses were also conducted, with the results indicating that the anchor was installed properly within the parameters intended by the manufacturer.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001768
EISBN: 978-1-62708-241-9
Abstract
A steel splice plate in a power transmission line tower cracked while in service. Metallographic analysis indicated the presence of a white hard martensite layer near the crack, which occurred in the heel of the plate. Mechanical property tests revealed localized hardening in the area of the crack, supporting the metallurgical findings. A substantial deterioration of the Charpy impact toughness of the material in the heel region was also observed which is believed to have caused the initiation and propagation of the cracks leading to the failure.