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Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001762
EISBN: 978-1-62708-241-9
Abstract
Rollover accidents in light trucks and cars involving an axle failure frequently raise the question of whether the axle broke causing the rollover or did the axle break as a result of the rollover. Axles in these vehicles are induction hardened medium carbon steel. Bearings ride directly on the axles. This article provides a fractography/fracture mechanic approach to making the determination of when the axle failed. Full scale tests on axle assemblies and suspensions provided data for fracture toughness in the induction hardened outer case on the axle. These tests also demonstrated that roller bearing indentions on the axle journal, cross pin indentation on the end of the axle, and axle bending can be accounted for by spring energy release following axle failure. Pre-existing cracks in the induction hardened axle are small and are often difficult to see without a microscope. The pre-existing crack morphology was intergranular fracture in the axles studied. An estimate of the force required to cause the axle fracture can be made using the measured crack size, fracture toughness determined from these tests, and linear elastic fracture mechanics. The axle can be reliably said to have failed prior to rollover if the estimated force for failure is equal to or less than forces imposed on the axle during events leading to the rollover.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0047521
EISBN: 978-1-62708-218-1
Abstract
A supplementary axle, which was used as an extension to a highway-trailer tractor to increase its load-bearing capacity, failed in service. The rolled steel channel extensions that secured the axle assembly to the tractor main-frame I-beams fractured transversely, with the crack in each instance initiating at a weld that joined the edge of the lower flange to the support bracket casting. The cracks propagated through the flange on each side until the effective cross-sectional area had been reduced sufficiently to bring about sudden and complete fracture of the remaining web and upper flange. Fatigue fracture was caused by a combination of high bending stresses in the bottom flanges of the channels due to the heavy load being carried, concentration of stresses due to the rapid change in section modulus of the channel at its point of attachment to the support-bracket casting, and brittleness of the high-hardness HAZ of the weld associated with the abnormally high carbon content in the central part of the channel. Welding of channel edges contributed to harmful gradients in section moduli and should be avoided in future assemblies.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001498
EISBN: 978-1-62708-218-1
Abstract
One end of an axle shaft containing the integral spur pinion was submitted for examination, along with the report of a tooth pitting failure. The spur pinion, integral to the axle shaft, operated in a medium-size, off-highway truck at an open-pit mine, for “a relatively short time.” Only the pinion head had been returned. The shaft portion had been torch-cut away. Chemical analysis along with the microstructure confirmed the specified material was SAE 43BV12 Ni-Cr-Mo alloy steel. The mode of failure was surface contact fatigue through the shear plane subsurface at the lowest point of single-tooth contact. The cause of failure was tooth-tip interference from the mating gear teeth. Because the mating parts within the assembly had not been returned or examined, unanswered questions remained.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001504
EISBN: 978-1-62708-217-4
Abstract
Despite extensive aircraft landing gear design analyses and tests performed by designers and manufacturers, and the large number of trouble-free landings, aircraft users have experienced problems with and failures of landing gear components. Different data banks and over 200 failure analysis reports were surveyed to provide an overview of structural landing gear component failures as experienced by the Canadian Forces over the last 20 years on more than 20 aircraft types, and to assess trends in failure mechanisms and causes. Case histories were selected to illustrate typical problems, troublesome failure mechanisms, the role of high strength aluminum alloys and steels, and situations where fracture mechanics analyses provided insight into the failures. The two main failure mechanisms were: fatigue occurring mainly in steel components, and corrosion related problems with aluminum alloys. Very few overload failures were noted. A number of causes were identified: design deficiencies and manufacturing defects leading mainly to fatigue failures, and poor materials selection and improper maintenance as the principal causes of corrosion-related failures. The survey showed that a proper understanding of the failure mechanisms and causes, by thorough failure analysis, provides valuable feedback information to designers, operators and maintenance personnel for appropriate corrective actions to be taken.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001744
EISBN: 978-1-62708-217-4
Abstract
Two examples involved brittle fracture promoted by small fatigue cracks owing to welding deficiencies. Other parts involving inadequate welding were a ski-wheel axle flange, ski fitting (brackets), and undercarriage shock strut stub assembly. In an attach fitting for an engine mount, weld cracks (severe stress concentrations) formed during repair welding. Cracks were severely oxidized. The main cause was incorrect repair and inadequate inspection of the fitting. In a cast CrNi alloy ski wheel axle, brittle fatigue failure emanated from welding cracks (notches). These welding cracks formed during the fabrication of the axle mounting plate. So-called all-purpose electrodes were used. Thus, the main cause for failure was a manufacturing deficiency-fatigue failure developed because of improper welding during fabrication of the axle. The proper electrode should have been used.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0046160
EISBN: 978-1-62708-224-2
Abstract
A stepped drive axle (hardened and tempered resulfurized 4150 steel forging) used in a high-speed electric overhead crane (rated at 6800 kg, or 7 tons, and handling about 220 lifts/day with each lift averaging 3625 to 5440 kg, or 4 to 6 tons) broke after 15 months of service. Visual examination of the fracture surface revealed three fracture regions. The primary fracture occurred approximately 50 mm (2 in.) from the driven end of the large-diam keywayed section on the stepped axle and approximately 38 mm (1 in.) from one end of the keyway where the crane wheel was keyed to the axle. Macroscopic, microscopic, and chemical examination revealed composition that was basically within the normal range for 4150 steel. This evidence supports the conclusion that cracking initiated at a location approximately opposite the keyway, and final fracture was due to mixed ductile and brittle fracture. Axial shift of the crane wheel during operation, because of insufficient interference fit, was the major cause of fatigue cracking. Recommendations included redesigning the axle to increase the critical diameter from 140 to 150 mm (5.5 to 6 in.) and to add a narrow shoulder to keep the drive wheel from shifting during operation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001495
EISBN: 978-1-62708-221-1
Abstract
An axle shaft in an open-pit mining truck hauling overburden failed after operating for 27,000 h. Previous failures had resulted from longitudinal shear, but this had not, bringing material quality into question. Chemical analysis verified that the part was SAE4340 Ni-Cr-Mo alloy steel and thus met material specification. The failure was a result of torsional fatigue in the tensile plane, originating from one of several gouges around the splined radius of the shaft. The fatigue crack progressed for a large number of cycles before final fracture. The shaft met metallurgical requirements and should have withstood normal operating conditions. The spacing of the gouge marks coincided with the spacing of the splines, indicative of careless assembly with the mating wheel gear.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047118
EISBN: 978-1-62708-235-8
Abstract
An automobile manufacturer rejected several 1035 steel stub axles because of what appeared to be short longitudinal cracks in the surfaces of the pins. The cracks were found when six axles were examined for defects by magnetic-particle inspection. However, metallographic examination showed that these lines were not cracks but slag inclusions at and immediately below the surface. Analysis (visual inspection, metallographic examination, and 100x/500x magnetic-particle inspection) supported the conclusions that the inclusions consisted of pieces of fireclay from channel brick that were flushed into the ingot mold. Although no true cracks were present, rejection of the stub axles was nevertheless justified. Slag streaks could reduce the strength of the stub axles and lead to the formation of fatigue fractures during operation. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001035
EISBN: 978-1-62708-214-3
Abstract
Following an accident in which a light pickup truck left the road and overturned, one of the rear axles, made of approximately 0.30C steel, was found to be fractured adjacent to the bearing lock nut. A keyway was present in the failed area, as were threads for the lock nut. Fracture surfaces of the failed axle and exemplar fractures obtained from simulation tests were studied using scanning electron microscope. The examination showed that the outer perimeter fracture in the axle was very flat and composed of cleavage and that the interior portion was composed of both cleavage and dimples. No evidence of prior cracking was found. The exemplar specimens from the simulation impact testing failed in a manner consistent with that observed in the axle. The examination confirmed that the failure was a one-time impact overload fracture and not the result of any prior crack in the material, indicating that the axle failure did not initiate the accident.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001040
EISBN: 978-1-62708-214-3
Abstract
Failed portions of a 4140 steel axle from a prototype urban transit vehicle were examined to determine the cause of failure. The testing procedures included visual examination, macrofractography, metallography, chemical analysis, and hardness and tensile testing. The analysis showed that a salvage welding repair had resulted in the formation of martensite that developed cracks, leading to fatigue failure of the axle. It was recommended that no weld buildup or repair be permitted on the axles.