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Luther M. Gammon, Michael V. Hyatt, G. Hari Narayanan, Henry J. Oberson, Harcayal B. Singh
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Fuselage assemblies and components
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001529
EISBN: 978-1-62708-217-4
Abstract
On 16 July 1999, a Boeing 737-800 on final approach for landing sustained a major lightning strike. Damage to the fuselage structure primarily was in the form of melting or partial melting of widely-separated rivets and adjacent Alclad 2024-T3 fuselage skin. The damage was confined to a 0.25-in. (6.4-mm) radii around the affected rivets. The repair process involved removal of the locally-affected material and addition of a skin doubler to restore the aircraft structure to the originally designed condition. Damage features are described briefly.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047076
EISBN: 978-1-62708-217-4
Abstract
Two cracks were discovered in a deck plate of an aircraft during overhaul and repair after 659 h of service. The cracks were on opposite sides of the deck plate in the flange joggles. The plate had been formed from 7178-T6 aluminum alloy sheet. Analysis (visual inspection, 0.2x/2x/2.3x electron microscope fractographs, hardness testing, and electrical conductivity testing) supported the conclusions that the failure was caused by fatigue cracks originating on the inside curved surface of the flanges. The cracks had initiated in surface defects caused by either corrosion pitting or forming notches, acting in combination with lateral forces evidenced by the moderate distortion of the fastener holes. Recommendations included eliminating the surface defects by revised cleaning and/or forming procedures. Revised design and installation should also alleviate the lateral forces.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001030
EISBN: 978-1-62708-214-3
Abstract
Cracks were discovered between interference-fit fasteners (MoS2-coated Ti-6Al-4V) that had been incorporated into a fighter aircraft primary structural frame (D6ac steel) to enhance structural fatigue life. Examination of sections cut from the cracked frame established that the cracks propagated by stress-corrosion cracking. The cause of cracking was twofold: use of interference-fit fasteners exposed to moisture intrusion from a marine environment and poor hole quality. Failure was intensified by dissimilar-metal contact in the presence of weak acidic electrolyte (dissociated MoS2). Control of machining parameters to prevent formation of brittle martensite, use of galvanically compatible fasteners, and use of an alternate lubricant were recommended.