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Wendy L. Weiss, Brian McClave
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001234
EISBN: 978-1-62708-232-7
Abstract
In a copper hot water system, a bent pipe was soldered into a straight pipe with twice the diameter. The neighborhood of the soldered joint was covered with corrosion product predominantly blue-green in color, presumably carbonates. When these corrosion products were scratched off it was seen that the copper beneath this layer had not suffered noticeable attack. The object of the examination was the localized deep cavities located almost symmetrically to both sides of the inserted end of the narrower tube on the internal wall of the wider tube which had in one place been eaten right through. The symmetrical location on each side of the point of insertion of the narrower pipe and the localized sharp delineation of the attack indicated erosion due to the formation of turbulence. By avoiding sharp transitions and abrupt changes in cross section it is possible to design the pipe work so that localized turbulence is obviated. Degassing and cleansing of the water also would reduce the danger of erosion particularly in the case of softened water, which takes up oxygen and carbon dioxide very readily thus becoming particularly aggressive.
Book Chapter
Feedwater Piping Erosion at a Waste-to-Energy Plant
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001276
EISBN: 978-1-62708-215-0
Abstract
The carbon steel feedwater piping at a waste-to-energy plant was suffering from wall thinning and leaking after being in service for approximately six years. Metallographic examination of ring sections removed front the piping revealed a normal microstructure consisting of pearlite and ferrite. However, the internal surface on the thicker regions of the rings exhibited significant deposit buildup, where the thinned regions showed none. No significant corrosion or pitting was observed on either the internal or external surface of the piping. The lack of internal deposits on the affected areas and the evidence of flow patterns indicated that the wall thinning and subsequent failure were caused by internal erosion damage. The exact cause of the erosion could not be determined by the appearance of the piping. Probable causes of the erosion include an excessively high velocity flow through the piping, extremely turbulent flow, and/or intrusions (weld backing rings or weld bead protrusions) on the internal surface of the pipes. Increasing the pipe diameter and decreasing the intrusions on the internal surface would help to eliminate the problem.