Skip Nav Destination
Close Modal
Update search
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
NARROW
Format
Topics
Book Series
Date
Availability
1-5 of 5
Fatigue limit
Close
Follow your search
Access your saved searches in your account
Would you like to receive an alert when new items match your search?
Sort by
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0048077
EISBN: 978-1-62708-221-1
Abstract
The 14-cm diam main hoist shaft of a mobile shovel was found to have multiple crack indications when ultrasonically inspected in the field. A crack around the entire circumference at the change in section was revealed by magnetic-particle inspection of the shaft. The crack was found to coincide with the junction of the fillet and the smaller diam at this change in section. A slight step in the continuity of the fillet and some machining marks were noted at this junction. A fine crack extending 2.5 mm from the surface and originating at the machining marks was revealed by microscopic examination. The shaft was identified by chemical analysis to be 1040 steel (hardness 170 HRB) which was concluded to have insufficient fatigue strength. The step at the base of the fillet was revealed as the point of initiation of the fatigue crack. Shaft material was changed to 4140 steel oil-quenched and tempered to a hardness of 302 to 352 HRB and all machining discontinuities were removed.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0048592
EISBN: 978-1-62708-218-1
Abstract
A drive-line assembly failed during vehicle testing. The vehicle had traveled 9022 km (5606 mi) before the failure occurred. Both the intact and fractured parts of the assembly were analyzed to determine the cause and sequence of failure. Visual examination of the assembly showed three of four bearing caps, two cap screws, and one universal-joint spider had fractured. Examination of the three fractured bearing caps and the spider showed no evidence of fatigue but showed that fracture occurred in a brittle manner. The bearing cap that was not destroyed still contained portions of the two fractured cap screws. It was found that the two cap screws failed in fatigue under service stresses. The three bearing caps and the universal-joint spider broke in a brittle manner. The properties of the material in the cap screws did not fulfill the specifications. The modified 1035 steel was of insufficient alloy content. Also, the tensile strength and endurance limit were lower than specified and were inadequate for the application. The material for the cap screw was changed from modified 1035 steel to 5140 steel.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0048060
EISBN: 978-1-62708-224-2
Abstract
The crane hook (rated for 13000 kg) failed in the threaded shank while lifting a load of 9072 kg. The metal in the hook was revealed by chemical analysis to be killed 1020 steel. It was disclosed by visual examination that the fracture had at the last thread on the shank and rough machining and chatter marks were evident on the threads. Beach marks that emanated from the thread-root locations on opposite sides of the fracture surface identified these locations to be the origins of the fracture. A medium-coarse slightly acicular structure was revealed by metallographic examination which indicated that the material was in the as-forged condition (which meant lower fatigue strength). The fracture was concluded to have occurred due to stress concentration in the root of the last thread. Normalizing of the crane hook after forging was suggested as a corrective measure. A stress-relief groove with a diam slightly smaller than the root diam was placed at the end of the thread and a large-radius fillet was machined at the change in diameter of the shank.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001298
EISBN: 978-1-62708-215-0
Abstract
A helicopter tail rotor blade spar failed in fatigue, allowing the outer section of the blade to separate in flight. The 7075-T7351 aluminum alloy blade had fiberglass pockets. The blade spar was a hollow “D” shape, and corrosion pits were present on the inner surface of the hollow spar A single corrosion pit, 0.38 mm (0.015 in.) deep, led to a fatigue failure of the spar The failure initiated on the pylon side of the blade. Dimensional analysis of the spar near the failure revealed measurements within engineering drawing tolerances. Though corrosion pitting was present, there was an absence of significant amounts of corrosion product and all of the pits were filled with corrosion-preventative primer. This indicated that the pitting occurred during spar manufacture, prior to the application of the primer The pitting resulted from multiple nickel plating and defective plating removal by acid etching. Post-plating baking operations subsequently reduced the fatigue strength of the spar.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001359
EISBN: 978-1-62708-215-0
Abstract
The cause of low fatigue life measurements obtained during routine fatigue testing of IMI 550 titanium alloy compressor blades used in the first stage of the high-pressure compressor of an aeroengine was investigated. The origin of the fatigue cracks was associated with a spherical bead of metal sticking to the blade surface in each case. Scanning electron microscope revealed that the cracks initiated at the point of contact of the bead with the blade surface. Energy-dispersive X-ray analysis indicated that the bead composition was the same as that of the blade. Detailed investigation revealed that fused material from the blade had been thrown onto the cold blade surface during a grinding operation to remove the targeting bosses from the forgings, thereby causing local embrittlement. It was recommended that extreme care be taken during grinding operations to prevent the hot, fused particles from striking the blade surface.