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Low-cyclic fatigue
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0048596
EISBN: 978-1-62708-221-1
Abstract
SAE grade 5 U-bolts were used to fasten auxiliary dual wheels to the axles on a farm tractor. Under typical farm usage, the bolts are expected to have infinite life. However, several U-bolts made of 29 mm diam rod broke after less than 100 h of service. The bolt legs in which the failures occurred were all in the same position relative to the direction of wheel rotation. Visual examination showed the break was a fairly flat transverse fracture in the threaded section between the washer and the nut. The appearance of the fracture surfaces was characteristic of failure by low-cycle fatigue, with a smooth matte fatigue failure region showing beach marks and generally extending over about 40 to 60% of the fracture surface, which indicated severe overload. The point of initiation of fatigue was at the root of the last thread at the edge of the nut on the side toward this washer. The U-bolts fractured in fatigue because the bolt material had poor hardenability relative to the diam of the bolts. The bolt material was changed from 1045 steel to 1527 steel, a warm-finished low-alloy steel. The diameter of the bolts was reduced to 27.2 mm and the threads were rolled rather than cut.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001149
EISBN: 978-1-62708-232-7
Abstract
A large diameter steel pipe reinforced by stiffening rings with saddle supports was subjected to thermal cycling as the system was started up, operated, and shut down. The pipe functioned as an emission control exhaust duct from a furnace and was designed originally using lengths of rolled and welded COR-TEN steel plate butt welded together on site. The pipe sustained local buckling and cracking, then fractured during the first five months of operation. Failure was due to low cycle fatigue and fast fracture caused by differential thermal expansion stresses. Thermal lag between the stiffening rings welded to the outside of the pipe and the pipe wall itself resulted in large radial and axial thermal stresses at the welds. Redundant tied down saddle supports in each segment of pipe between expansion joints restrained pipe arching due to circumferential temperature variations, producing large axial thermal bending stresses. Thermal cycling of the system initiated fatigue cracks at the stiffener rings. When the critical crack size was reached, fast fracture occurred. The system was redesigned by eliminating the redundant restraints and by modifying the stiffener rings to permit free radial thermal breathing of the pipe.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001506
EISBN: 978-1-62708-217-4
Abstract
A single-engine aircraft was climbing to 8000 ft when the engine suddenly lost power. The landing gear was torn off during the emergency landing. During the field investigation, the fuel line was found to be separated from the fuel pump outlet due to a failure of the elbow fitting. A bracket which supports the in-line fuel flow transducer also was found broken. Examination of the elbow fracture revealed characteristics of low-cycle fatigue failure. Examination of the support bracket fractures revealed a high-cycle mode of fatigue failure, with the primary fatigue extending along the full length of the 90 deg bend in the bracket. It was concluded that the failure was caused by an incorrectly-installed support bracket. It was recommended that the installation procedure be clarified.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001002
EISBN: 978-1-62708-229-7
Abstract
During the inspection of a boiler containing cracks at the superheater header connection, cracking also was detected within the main steam drum. This was fabricated from a Mn-Mo-V low-alloy steel. It operated with water and saturated steam at approximately 335 deg C. Cracking was detected at the nozzles connecting the tubes for the entry of steam and hot water to the drum, at the downcomers, and at the connection to the safety valve. All cracks had a similar morphology, running in a longitudinal direction along the drum from the cutouts in the shell. All the cracks had developed under the influence of the hoop stress and were associated with the locally increased stress levels relating to the cutouts at nozzle and pipe connections. At their ends the cracks were filled with corrosion products, and their surfaces were seen to be very irregular. The process of crack growth was not due to fatigue only but can most probably be attributed to corrosion fatigue. The boiler steam drum design should be reviewed to reduce the local level of stress at the shell-nozzle connections.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0090181
EISBN: 978-1-62708-229-7
Abstract
Cracking in gas turbine blades was found to initiate from a mechanism of low-cycle fatigue (LCF). LCF is induced during thermal loading cycles in gas turbines. However, metallography of two cracked blades revealed a change in microstructure at as-cast surfaces for depths up to 0.41 mm (0.016 in.). Evaluation by SEM confirmed the difference in structure was associated with a lack of formation of coarse gamma prime structure in the matrix. Microhardness and miniature tensile test results indicated lower strength consistent with the absence of the coarse gamma prime constituent. The blade vendor found that the lot of hot isostatically pressed (HIP) blade castings had been exposed to an improper atmosphere during the HIP process, resulting in the weakened structure. Because subsequent failures were found in blades that did not come from the suspect HIP lot, the scope of the problem was considered generic, and the conclusion was that the primary failure mechanism was LCF. Material imperfections were a secondary deficiency that had the effect of causing the blades from the bad HIP lot to crack first.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048361
EISBN: 978-1-62708-234-1
Abstract
Several failures occurred in 64-mm schedule 80 type 304 stainless steel (ASME SA-312, grade TP304) piping in a steam-plant heat-exchanger system near tee fittings at which cool water returning from the heat exchanger was combined with hot water from a bypass. Various portions of the piping were subjected to temperatures ranging from 29 to 288 deg C. Each of the failures were revealed to consist of transgranular cracking in and/or close to the circumferential butt weld joining the tee fitting to the downstream pipe leg, where the hot bypass water mixed with the cool return water. The transgranular cracks suggested that thermal fatigue was a more likely cause of failure than SCC. It was concluded by temperature measurements that circumferential temperature gradients, in combination with inadequate flexibility in the piping system as a whole, had caused the failures. The tee fitting was redesigned to alleviate the thermal stress pattern.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001296
EISBN: 978-1-62708-215-0
Abstract
A 52000 bearing steel valve guide component operating in the fuel supply system of a transport aircraft broke into two pieces after 26 h of flight. The valve guide fractured through a set of elongated holes that had been electrodischarge machined into the component. Analysis indicated that the part failed by low cycle fatigue. The fracture was brittle in nature and had originated at a severely eroded zone of craters in a hard, deep white layer that was the result of remelting during electrodischarge machining. It was recommended that the remaining parts be inspected using a stereoscopic microscope and/or a borescope.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001304
EISBN: 978-1-62708-215-0
Abstract
An exhaust diffuser assembly failed prematurely in service. The failure occurred near the intake end of the assembly and involved fracture in the diffuser cone (Corten), diffuser in take flange (type 310 stainless steel), diffuser exit flange (type 405 stainless steel), expansion bellows (Inconel 600), and bellows intake flange (Corten). Individual segments of the failed subassemblies were examined using various methods. The analysis indicated that the weld joint in the diffuser intake flange (type 310 stainless steel to Corten steel) contained diffusion-zone solidification cracks. The joints had been produced using the mechanized gas-metal arc welding process. Cracking was attributed to improper control of welding parameters, and failure was attributed to weld defects.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001041
EISBN: 978-1-62708-214-3
Abstract
Four truck cross members intended for use in heavy-duty transport trucks were investigated. Two of the members had cracked on a prototype vehicle and two had been fatigue tested in the laboratory. The cross members were fabricated from SAE 950X plate and consisted of a formed channel section and an internal fillet-welded diaphragm. Sections from each of the cross members were subjected to a complete analysis, including chemical analysis, magnetic particle testing, mechanical testing, scanning electron microscope/fractography, and metallography. The primary mode of failure was found to be fatigue cracking that initiated at the toes of the fillet welds. Secondary fatigue cracking occurred at the torque rod mounting holes. Failure was attributed to cyclic stresses at the weld toes that exceeded the lowered fatigue strength at this location. A design change that eliminated the fillet welds alleviated the problem.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001129
EISBN: 978-1-62708-214-3
Abstract
The failure of a 45 Mg (50 ton) rail crane bolster was investigated. Spectrochemical analysis indicated that the material was a 0.25C-1.24Mn-0.62Cr-0.24Mo cast steel. SEM examination revealed the presence of fatigue, as well as intergranular and ductile fractures. Microstructural analysis focused on an area where an antisway device had been welded to the structure and revealed the presence of coarse, untempered martensite that had resulted from faulty weld repair techniques. It was suggested that the use of proper welding procedures, including preheating and postheating, would have prevented the failure.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001081
EISBN: 978-1-62708-214-3
Abstract
Several compressor disks in military fighter and trainer aircraft gas turbine engines cracked prematurely in the bolt hole regions. The disks were made of precipitation-hardened AM355 martensitic stainless steel. Experimental and analytical work was performed on specimens from the fifth-stage compressor disk (judged to be the most crack-prone disk in the compressor) to determine the cause of the failures. Failure was attributed to high-strain low-cycle fatigue during service. It was also determined that the cyclic engine usage assumed in the original life calculations had been under estimated, which led to low-cycle fatigue cracking earlier than expected. Fracture mechanics analysis of the disks was carried out to assess their damage tolerance and to predict safe inspection intervals.