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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c9001244
EISBN: 978-1-62708-224-2
Abstract
The cross bars of conveyor belt links that served to transport glass containers through a stress relief furnace fractured in many cases. They consisted of wires of 5 mm diam made of low-carbon Siemens-Martin steel, while the interwoven longitudinal bars were made of strip steel of 4 x 2 sq mm. The furnace temperature was said to be 500 deg C. In addition to the fractures they also showed many more or less advanced cracks. These occurred in the circumferential grooves that recurred at regular intervals. The fractures were abraded and oxidized. They could have been fatigue fractures. The fracture probably was induced by the pressing-in or abrading of the sharp steel band edges into the surface of the cross bars. Torsion fatigue fractures may have started from these notches. Relaxation then contributed positively through recovery and recrystallization. Such damage occurs less frequently in round wire conveyor belt links because the round wire neither impresses so sharply nor abrades against the cross bars, and it also exerts less torsion than the flat wire.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0089682
EISBN: 978-1-62708-230-3
Abstract
A neck fitting (cast equivalent of AISI type 317) exhibited extreme corrosion with large, deeply pitted areas. It had been in service in a sulfite digester at 140 deg C (285 deg F) and 689 kPa (100 psi). The liquor was calcium bisulfite, and chloride content was reported to be low. Investigation (visual inspection, and micrographs of sections with electrolytic etching using 10 N KOH and then again after re-polishing and etching with Murakami's reagent) supported the conclusions that the casting never received a proper solution anneal. Recommendations included possible corrosion-screening tests in accordance with ASTM A 262 to ensure adequate corrosion resistance.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001581
EISBN: 978-1-62708-235-8
Abstract
A heavily worked 304 stainless steel wire basket recrystallized and distorted while in service at 650 deg C (1200 deg F). This case study demonstrates that heavily cold worked austenitic stainless steel components can experience large losses in creep strength, and potentially structural collapse, under elevated temperature service, even at temperatures more than 300 deg C (540 deg F) below the normal solution annealing temperature. The creep strength of the recrystallized 304/304L steel was more than 1000 times less than that achievable with solution annealed 304H. These observations are consistent with limitations (2000 Addendum to ASME Boiler and Pressure Vessel Code) on the use of cold worked austenitic stainless steels for elevated temperature service.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c0048728
EISBN: 978-1-62708-228-0
Abstract
After being in service for ten years, two admiralty brass heat-exchanger tubes from a cooler in a refinery catalytic reforming unit cracked circumferentially in the area of U-bends. A blunt transgranular cracking with minimal branching propagating from the inside surface of the tube was revealed by metallography which was typical of cracking by corrosion fatigue mechanism. Corrosion deposits on both the inside- and outside-diam surfaces were found in the tubes. The presence of copper, zinc, iron, and small amounts of chloride, sulfur, silicon, tin, and manganese was revealed by energy-dispersive analysis of the deposits. It was interpreted by the hardness values (higher than typical for annealed copper tubing) that the tubes may not have been annealed after the U-bends were formed and thus the role of residual stresses in the crack was revealed. It was concluded that the tubes failed by corrosion fatigue initiated by pitting at the inside-diam surface. The tubes were recommended to be annealed after bending to reduce residual stresses from the bending operation to an acceptable level.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c0048719
EISBN: 978-1-62708-228-0
Abstract
A tubular heat exchanger in a refinery reformer unit leaked after one month of service. The exchanger contained 167 type 304 stainless steel U-bent integral-finned tubes. Cracks in the tube wall were revealed during examination. Hardness of the tube was found to be 30 HRC at the inside surface and up to 40 HRC at the base of the fin midway between the roots which indicated that the fins were cold formed and not subsequently annealed thus susceptible to SCC because of a high residual stress level. It was revealed by metallographic examination that the fracture was predominantly by transgranular branched cracking and had originated from the inside surface. It was concluded that the tubes failed in SCC caused by chlorides in the presence of high residual stresses. The finned tubes were ordered in the annealed condition as a corrective measure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001225
EISBN: 978-1-62708-232-7
Abstract
Three radially-cracked disks that circulated the protective gases in a bell-type annealing furnace were examined. During service they had been heated in cycles of 48 h to 720 deg C for 3 h each time, then were kept at temperature for 15 h followed by cooling to 40 deg C in 30 h, while rotating at 1750 rpm. Two disks were cracked at the inner face of the sheet metal rim while the rim of the third was completely cracked through. An analysis of the sheet metal rim of one of the disks showed the following composition: 0.06C, 1.98Si, 25.8Cr, and 35.8Ni. A steel of such high chromium content was susceptible to s-phase formation when annealed under 800 deg C. The material selected was therefore unsuitable for the stress to be anticipated. In view of the required oxidation resistance, a chromium-silicon or chromium-aluminum steel with 6 or 13% Cr would have been adequate. If the high temperature strength of these steels proved inadequate, an alloy lower in chromium would have been preferable.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001238
EISBN: 978-1-62708-232-7
Abstract
Heating elements, consisting of strips, 40 mm x 2 mm, of the widely used 80Ni-20Cr resistance heating alloy, and designed to withstand a temperature of 1175 deg C, were rendered unusable by scaling after a few months service in a through-type annealing furnace, Although the temperature supposedly did not exceed 1050 deg C. Structural observations indicated a special case of internal oxidation. The required conditions for this were apparently provided by the moist hydrogen atmosphere of the annealing furnace, in which the chromium was oxidized, while the oxides of iron and nickel were reduced. Even the carbon suffered incomplete combustion and was enriched in the core. Thus, no protective layer could form or be maintained. The intergranular advancement of the oxidation may have been favored by the precipitation of chromium-rich carbides on the austenite grain boundaries. This form of internal oxidation is, in the case of Ni-Cr alloys, known as green rot. Alloys containing iron should be more resistant. As a preventive measure it was recommended to reduce the operating temperature of the strip sufficiently to allow the use of Fe-Ni-Cr alloys.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048294
EISBN: 978-1-62708-234-1
Abstract
The tubes of a stationary industrial boiler, 64 mm in diam and made of 1.25Cr-0.5Mo steel (ASME SA-213, grade T-11) failed by two different types of rupture. Noticeable swelling of the tubes in the area of rupture was revealed by visual examination. The tubes with slight longitudinal splits were interpreted to have failed by stress rupture resulting from prolonged overheating at 540 to 650 deg C as the microstructure exhibited extensive spheroidization and coalescence of carbides. The larger ruptures were tensile failures that resulted from rapid overheating to 815 to 870 deg C as a completely martensitic structure was revealed at the edges of the ruptures in these tubes because of rapid quenching by escaping fluid. The prolonged-overheating failures were concluded to have been the primary ruptures and that local loss of circulation had caused rapid overheating in adjacent tubes. Poor boiler circulation and high furnace temperatures were believed to have caused the prolonged overheating.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001186
EISBN: 978-1-62708-234-1
Abstract
A 2.3 mm diam steel wire broke during cable twisting. The fracture occurred obliquely to the longitudinal axis of the wire and showed a constriction at the end. Therefore it was a ductile fracture. File mark type work defects were noticeable on the wire surface at both sides of the fracture, but they had no effect on the breakage of the wire. Away from the fracture area, the wire had a normal structure of hyperfine lamellar pearlite (sorbite) of a “patented” and cold drawn steel wire. In the vicinity of the fracture, the cementite of the pearlite was partially spheroidized, while at the fracture itself it was completely spheroidized. Therefore the wire was locally annealed at this point. It was likely that the wire cracked at this point during the last drawing and then broke during twisting due to its lower strength in the weakened cross section after prior deformation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001198
EISBN: 978-1-62708-221-1
Abstract
Cast iron bearing caps in tractor engines fractured repeatedly after only short operating periods. The fracture originated in a cast-in groove and ran approximately radially to the shaft axis. The smallest cross section was at the point of fracture. The core structure of the caps consisted of graphite in pearlitic-ferritic matrix. Casting stresses did not play a decisive role because of the simple shape of the pieces that were without substantial cross sectional variations. Two factors exerted an unfavorable effect in addition to comparatively low strength. First, the operating stress was raised locally by the sharp-edged groove, and second, the fracture resistance of the cast iron was lowered at this critical point by the existence of a ferritic bright border. To avoid such damage in the future it was recommended to observe one or more of the following precautions: 1) Eliminate the grooves; 2) Remove the ferritic bright border; 3) Avoid undercooling in the mold and therefore the formation of granular graphite; 4) Inoculate with finely powdered ferrosilicon into the melt for the same purpose; and, 5) Anneal at lower temperature or eliminate subsequent treatment in consideration of the uncomplicated shape of the castings.