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Electroplating
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0091036
EISBN: 978-1-62708-227-3
Abstract
Socket head cap screws used in a naval application were failing in service due to delayed fracture. The standard ASTM A 574 screws were zinc plated and dichromate coated. Investigation (visual inspection, 1187 SEM images, chemical analysis, and tension testing) of both the failed screws and two unused, exemplar fasteners from the same lot supported the conclusion that the cap screws appear to have failed due to hydrogen embrittlement, as revealed by delayed cracking and intergranular fracture morphology. Static brittle overload fracture occurred due to the tension preload, and prior hydrogen charging that occurred during manufacturing. The probable source of charging was the electroplating, although postplating baking was reportedly performed as well. Recommendations included examining the manufacturing process in detail.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006448
EISBN: 978-1-62708-217-4
Abstract
Three wing flap hinge bearings were received by the laboratory for analysis. The bearings were fabricated from chromium-plated type 440C martensitic stainless steel. The intergranular fracture pattern seen in the electron fractographs, coupled with the corrosion pits observed on the inner diam of the bearings, strongly suggested that failure initiated by pitting and progressed by SCC or hydrogen embrittlement from the plating operation. It was recommended that the extent of the flap hinge bearing cracking problem be determined by using nondestructive inspection because it is possible to crack hardened type 440C during the chromium plating process. An inspection for pitting on the bearing inner diam was also recommended. It was suggested that electroless nickel be used as a coating for the entire bearing. A review of the chromium plating and baking sequence was recommended also to ensure that a source of hydrogen is not introduced during the plating operation.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0048630
EISBN: 978-1-62708-217-4
Abstract
Two clevis-head self-retaining bolts used in the throttle-control linkage of a naval aircraft failed on the aircraft assembly line. Specifications required the bolts to be heat treated to a hardness of 39 to 45 HRC, followed by cleaning, cadmium electroplating, and baking to minimize hydrogen embrittlement. The bolts broke at the junction of the head and shank. The nuts were, theoretically, installed fingertight. The failure was attributed to hydrogen embrittlement that had not been satisfactorily alleviated by subsequent baking. The presence of burrs on the threads prevented assembly to finger-tightness, and the consequent wrench torquing caused the actual fractures. The very small radius of the fillet between the bolt head and the shank undoubtedly accentuated the embrittling effect of the hydrogen. To prevent reoccurrence, the cleaning and cadmium-plating procedures were stipulated to be low-hydrogen in nature, and an adequate post plating baking treatment at 205 deg C (400 deg F), in conformity with ASTM B 242, was specified. A minimum radius for the head-to-shank fillet was specified at 0.25 mm (0.010 in.). All threads were required to be free of burrs. A 10-day sustained-load test was specified for a sample quantity of bolts from each lot.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c0048674
EISBN: 978-1-62708-222-8
Abstract
Fasteners, made in high-production progressive dies from 0.7 mm thick cold-rolled 1060 steel, were used to secure plastic fabric or webbing to the aluminum framework of outdoor furniture. It was found that approximately 30% of the fasteners cracked and fractured as they were compressed to clamp onto the framework prior to springback. The heat treatment cycle of the fasteners consisted of austenitizing, quenching, tempering to obtain a tempered martensite microstructure, acid cleaning, zinc electroplating, coating with a clear dichromate and thereafter baking to remove the nascent hydrogen. It was revealed that fasteners treated in this manner were brittle due to hydrogen embrittlement as the baking process was found to not be able to remove all the nascent hydrogen which had induced during acid cleaning and electroplating. The heat treatment cycle was modified to produce a bainitic structure and the method of plating the fastener with zinc was changed from electroplating to a mechanical deposition process to thus avoid hydrogen embrittlement.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001641
EISBN: 978-1-62708-235-8
Abstract
Near-surface porosity in zinc die castings that were subsequently plated with copper, nickel, and bright chromium was causing blemishes in the plating. Identifying die casting turbulence and hot spots were keys to process modifications that subsequently allowed porosity to be greatly minimized.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001178
EISBN: 978-1-62708-235-8
Abstract
Eight cylinderhead screws cracked after a short running time in motors. They were made of Fe-0.45C-1Cr steel, had rolled threads, were heat treated to 110 kg/sq mm tensile strength, and were electrolytically galvanized. All fractured at the root of the thread. The surfaces of fracture were fine-grained and had not spread by rubbing. Because the screws were electrolytically galvanized, failure resulted from “delayed fracture.” Experience has shown that this type of fracture is seen on production parts made of high-strength steels, which absorbed hydrogen during pickling or during a galvanic surface treatment. Such parts will rupture below the elastic limit during continuous stressing. This often occurs only after the expiration of a certain time period, and preferably at locations of stress concentrations such as changes in cross section or threads. As a rule, the hydrogen cannot be verified analytically because most of it escapes again after prolonged storage at room temperature or short heating at 100 to 200 deg C.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001613
EISBN: 978-1-62708-235-8
Abstract
The electroplated tappet adjusting screws used in diesel engines failed during initial bend testing. The analysis of the failure showed that the fracture was nucleated from the subsurface of the screw. The fracture surface was intergranular at the ID and OD region and microvoid coalescence in the center. The improper baking after electroplating of the screw led to H2-induced blistering/cracking. The high strength of the threaded region of the adjusting screw increased the failure propensity.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0048626
EISBN: 978-1-62708-225-9
Abstract
Cadmium-plated high-strength steel bolts were used to facilitate quick disassembly of a vehicle. One bolt was found fractured across the root of a thread after being torqued in place for one week. The bolts were made of 8735 steel heat treated to a tensile strength of 1241 to 1379 MPa (180 to 200 ksi) with a hardness of 39 to 43 HRC, followed by cadmium plating. The bolt that failed and several that did not were examined. It was found that failure of the bolts was the result of time-dependent hydrogen embrittlement. Had the remaining bolts been torqued to the normal stress levels, all would have failed within two weeks. The bolts were baked, as specified by ASTM B 242, at 205 deg C (400 deg F) for 30 min. No further failures occurred. Baking for 30 min is the minimum baking time; however, baking times up to 24 h are recommended for greater safety.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0048634
EISBN: 978-1-62708-225-9
Abstract
During an inspection of a structure two weeks after assembly, the heads of several cadmium-plated AISI 8740 steel fasteners were found to be completely separated from their respective shanks. SEM examination of the fracture surfaces revealed a brittle, intergranular fracture mode, indicating hydrogen embrittlement. An investigation was conducted to determine the extent of hydrogen embrittlement in the various lots of cadmium-plated 8740 steel fasteners. It was found that hydrogen embrittlement was caused by the use of a bright, impervious cadmium electroplate that hindered diffusion of mobile hydrogen outward from the surface of the pin. After the cadmium layer was removed, the mobile hydrogen contained on the surface of the steel and in the electroplated deposit was released, and the embrittlement problem was alleviated. To prevent reoccurrence, the bright cadmium layer was stripped from the pins, which were then baked and repeated with a dull, porous cadmium layer that allowed outward diffusion of hydrogen. The pins were baked again after deposition of the porous cadmium layer. This eliminated the problem.