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Furnace tubes
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001735
EISBN: 978-1-62708-220-4
Abstract
A sample tube was removed from a reformer furnace for life assessment after 69,000 h of service. Sections were cut from the tube, which was a spindle cast A297 Grade HK 40 (25 Cr, 20 Ni, 0.4 C) austenitic steel of 122.5 mm OD and 10.5 mm nominal wall thickness. They were examined metallographically on transverse sections and on longitudinal sections through the butt welds joining the separate cast segments of the tube. Creep damage was mainly concentrated within the inner one third of the wall thickness. The use of damage assessment parameters in evaluating the reformer tube remaining life showed the welds to be inadequate, and to have a strength and creep resistance below those of the base metal.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0060144
EISBN: 978-1-62708-234-1
Abstract
Two steam-methane reformer furnaces were subjected to short-time heat excursions because of a power outage, which resulted in creep bulging in the Incoloy 800 outlet pigtails, requiring complete replacement. Each furnace had three cells, consisting of 112 vertical tubes per cell, each filled with a nickel catalyst. The tubes were centrifugally cast from ASTM A297, grade HK-40 (Fe-25Cr-20Ni-0.40C), heat-resistant alloy. The tube was concluded after metallurgical inspection to have failed from creep rupture (i.e., stress rupture). A project for detecting midwall creep fissuring was instigated as a result of the failure. It was concluded after laboratory radiography and macroexamination that if the fissure were large enough to show on a radiograph, either with or without the catalyst, the tube could be expected to fail within one year. The set up for in-service radiograph examination was described. The tubes of the furnace were radiographed during shut down and twenty-four tubes in the first furnace and 53 in the second furnace showed significant fissuring. Although, radiography was concluded to be a practical technique to provide advance information, it was limited to detecting fissures caused by third-stage creep in tubes because of the cost involved in removing the catalysts.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001726
EISBN: 978-1-62708-234-1
Abstract
A carbon steel furnace tube which should have given good service for ten years ruptured after one year. The tube showed obvious swelling at the point of rupture, and the bulged surface of the tube was oxidized at a temperature far above the design temperature. There was little or no loss in wall thickness due to corrosion or scaling, and the tube wall was thinned to a knife edge at the rupture. Metallographic examination showed the condition of the material was satisfactory. The failure was mechanical in nature, typical of short time creep rupture. The localized oxidation indicated improper furnace operation or blockage of the tube. The furnace was checked and found to have a burner tip out of order. After the tip was repaired, localized overheating was minimized and further premature failures did not occur.