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Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006816
EISBN: 978-1-62708-329-4
Abstract
This article introduces some of the general sources of heat treating problems with particular emphasis on problems caused by the actual heat treating process and the significant thermal and transformation stresses within a heat treated part. It addresses the design and material factors that cause a part to fail during heat treatment. The article discusses the problems associated with heating and furnaces, quenching media, quenching stresses, hardenability, tempering, carburizing, carbonitriding, and nitriding as well as potential stainless steel problems and problems associated with nonferrous heat treatments. The processes involved in cold working of certain ferrous and nonferrous alloys are also covered.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001850
EISBN: 978-1-62708-241-9
Abstract
After about a year of uninterrupted service, one of the blow pipes on a blast furnace developed a bulge measuring 300 x 150 x 12 mm. The conical shaped section was removed from the furnace and examined to determine why it failed. The investigation consisted of visual inspection, chemical analysis, microstructural characterization, and mechanical property testing. The pipe was made from nonresulfurized carbon steel as specified and was lined with an alumina refractory. Visual inspection revealed cracks in the refractory lining, which corresponded with the location of the bulge. Microstructural and EDS analysis yielded evidence of overheating, revealing voids, scale, grain boundary oxidation, decarburization, and grain coarsening on the inner surface of the pipe, which also suggest the initiation of creep. Based on the information gathered during the investigation, the blow pipe was exposed to high temperatures when the liner cracked and subsequently bulged out due to creep.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001837
EISBN: 978-1-62708-241-9
Abstract
This case study describes the failure analysis of a steel nozzle in which cracking was observed after a circumferential welding process. The nozzle assembly was made from low-carbon CrMoV alloy steel that was subsequently single-pass butt welded using gas tungsten arc welding. Although no cracks were found when the welds were visually inspected, X-ray radiography showed small discontinuous surface cracks adjacent to the weld bead in the heat affected zone. Further investigation, including optical microscopy, microhardness testing, and residual stress measurements, revealed that the cracks were caused primarily by the presence of coarse untempered martensite in the heat affected zone due to localized heating. The localized heating was caused by high welding heat input or low welding speed and resulted in high transformation stresses. These transformation stresses, working in combination with thermal stresses and constraint conditions, resulted in intergranular brittle fracture.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c0065826
EISBN: 978-1-62708-233-4
Abstract
The wires used in a wet precipitator for cleaning the gases coming off a basic oxygen furnace failed. The system consisted of six precipitators, three separate dual units, each composed of four zones. Each zone contained rows of wires (cold drawn AISI 1008 carbon steel) suspended between parallel collector plates. It was determined that the 1008 wires failed because of corrosion fatigue. It was decided to replace all of the wires in the two zones with the highest rates of failure with cold-drawn type 304 austenitic stainless steel wire. These expensive wires, however, failed after a week by transgranular SCC. Annealed type 430 ferritic stainless steel was subsequently suggested to prevent further failures.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c0046079
EISBN: 978-1-62708-233-4
Abstract
After only a short time in service, oil-fired orchard heaters made of galvanized low-carbon steel pipe, 0.5 mm (0.020 in.) in thickness, became sensitive to impact, particularly during handling and storage. Most failures occurred in an area of the heater shell that normally reached the highest temperature in service. A 400x etched micrograph showed a brittle and somewhat porous metallic layer about 0.025 mm (0.001 in.) thick on both surfaces of the sheet. Next to this was an apparently single-phase region nearly 0.05 mm (0.002 in.) in thickness. The examination supported the conclusion that prolonged heating of the galvanized steel heater shells caused the zinc-rich surface to become alloyed with iron and reduce the number of layers. Also, heating caused zinc to diffuse along grain boundaries toward the center of the sheet. Zinc in the grain boundaries reacted with iron to form the brittle intergranular phase, resulting in failure by brittle fracture at low impact loads during handling and storage. Recommendation included manufacture of the pipe with aluminized instead of galvanized steel sheet for the combustion chamber.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001623
EISBN: 978-1-62708-232-7
Abstract
Several glass wool insulation sections from a heat-treat furnace showed visible, but only cosmetic discoloration. EDS showed the presence of silicon, aluminum, and oxygen in the nondiscolored region, and these elements are consistent with glass wool. Relatively high levels of chromium and nickel were detected in the discolored area, along with lower amounts of iron, manganese, sodium, calcium, cobalt, and sulfur, in addition to the surrounding glass wool elements. Results of this limited evaluation showed the discoloration was caused by the presence of elevated levels of chromium, nickel, and aluminum. The visual appearance, along with the EDS findings, suggested these elements were present in the form of oxides. These oxides were likely deposited from adjacent structural components of the furnace, which had oxidized during operation.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0046956
EISBN: 978-1-62708-232-7
Abstract
A brazing-furnace muffle 34 cm (13 in.) wide, 26 cm (10 in.) high, and 198 cm (78 in.) long, was fabricated from nickel-base high-temperature alloy sheet and installed in a gas-fired furnace used for copper brazing of various assemblies. The operating temperature of the muffle was reported to have been closely controlled at the normal temperature of 1175 deg C (2150 deg F); a hydrogen atmosphere was used during brazing. After about five months of continuous operation, four or five holes developed on the floor of the muffle, and the muffle was removed from service. Analysis (visual inspection, x-ray spectrometry, and metallographic examination) supported the conclusion that the muffle failed by localized overheating in some areas to temperatures exceeding 1260 deg C (2300 deg F). The copper found near the holes had dripped to the floor from assemblies during brazing. The copper diffused into the nickel-base alloy and formed a grain-boundary phase that was molten at the operating temperature. The presence of this phase caused localized liquefaction and weakened the alloy sufficiently to allow formation of the holes. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001452
EISBN: 978-1-62708-232-7
Abstract
A bracket which formed part of the carrier of a chain conveyor system used to transport components through a continuous oven fractured. A brittle crack originated on the inside of the right-angled bend, the surface having oxidized subsequently. The remaining portion of the fracture resulted from fatigue. Shallow oxidized regions adjacent to the inside surface of the bend indicated pre-existing cracks. A sulphur print on the edge of the bracket showed the material was rolled from a rimming steel ingot. The general appearance of the fracture, and the fact failure took place where embrittlement had developed following plastic straining and service at a temperature of 260 deg C (500 deg F) suggested that failure resulted from strain-age embrittlement.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0046995
EISBN: 978-1-62708-232-7
Abstract
Three radiant tubes, made of three different high-temperature alloys, were removed from a carburizing furnace after approximately eight months of service when they showed evidence of failure by collapsing (telescoping) in a region 30 cm (12 in.) from the tube bottoms in the vicinity of the burners. The tubes had an original wall thickness of 3.0 mm (0.120 in.) and were made of three different alloys: the first was Hastelloy X; the second alloy was RA 333, a wrought nickel-base heat-resistant alloy; and the third was experimental alloy 634, which contained 72% Ni, 4% Cr, and 3.5% Si. The three radiant tubes had been operated at a temperature of about 1040 deg C (1900 deg F) to maintain furnace temperatures of 900 to 925 deg C (1650 to 1700 deg F). Analysis (visual inspection and micrographic examination) supported the conclusion that all three tubes failed by corrosion. Recommendations included replacing the material with an alloy, such as RA 333, with a higher chromium content and with an additional element, like silicon, resistant to carburization-oxidation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001233
EISBN: 978-1-62708-232-7
Abstract
High-chromium steel pipes 42.25 x 3.25 mm from a blast furnace gas fired recuperator for the preheating of air were heavily oxidized and perforated in places. It was found that the blast furnace gas had a high sulfur content. Both the carburization and the formation of sulfide proved that in addition, from time to time at least, combustion was incomplete and the operation was carried out in a reducing atmosphere, with the result that oxygen deficiency prevented the formation or maintenance of a protective surface layer on the external surface of the pipes. The sulfur would probably not have damaged the nickel-free steel used here at the given temperatures if it had been present as sulfur dioxide in an oxidizing atmosphere. The damage was therefore caused primarily by an incorrectly conducted combustion process.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001532
EISBN: 978-1-62708-232-7
Abstract
Work rolls made of indefinite chill double-poured (ICDP) iron are commonly used in the finishing trains of hot-strip mills (HSMs). In actual service, spalling, apart from other surface degeneration modes, constitutes a major mechanism of premature roll failures. Although spalling can be a culmination of roll material quality and/or mill abuse, the microstructure of a broken roll can often unveil intrinsic inadequacies in roll material quality that possibly accentuate failure. This is particularly relevant in circumstances when rolls, despite operation under similar mill environment, exhibit variations in roll life. The paper provides an insight into the microstructural characteristics of spalled ICED HSM work rolls, which underwent failure under similar mill operating environment in an integrated steel plant under the Steel Authority of India Limited. Microstructural features influencing ICDP roll quality, viz. characteristics of graphite, carbides, martensite, etc., have been extensively studied through optical microscopy, quantitative image analysis (QIA), and electron-probe microanalysis (EPMA). These are discussed in the context of spalling propensity and roll life.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0046926
EISBN: 978-1-62708-232-7
Abstract
Over a period of about one year, three RA 330 alloy salt pots from a single heat-treating plant were submitted to failure analysis. All of the pots, which had 9.5 mm thick walls, were used primarily to contain neutral salts at temperatures from about 815 to 900 deg C (1500 to 1650 deg F). However, some cyaniding was also performed in these pots, which, when not in use, were idled at 760 deg C (1400 deg F). It was reported that sludge was removed from the bottom of the pots once a day. Normal pot life varied from about 6 to 20 months. The pots were removed from the furnace, visually inspected, and rotated 120 deg every three weeks to ensure that no single location was overheated for a prolonged period of time. Analysis (visual inspection, chemical analysis, metallographic examination, and x-ray analysis, 60x micrograph etched with 10% oxalic acid) supported the conclusion that the cause of failure of each of the three salt pots was severe intergranular corrosion accompanied by substantial chromium depletion. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001245
EISBN: 978-1-62708-232-7
Abstract
A working roll of 210 mm diam and 500 mm face length was examined because of shell-shaped fractures. The roll consisted of Fe-0.83C-1.6Cr steel. The chromium content was low for a roll of this diam. The crack origin was located about 10 mm under the roil face. Surface hardness (HV1) of 900 kp/sq mm was exceptionally high corresponding to the martensitic peripheral structure. An untempered piece with such a thick cross section and a hardened peripheral zone with such high hardness must have high residual stresses that culminate in the transition zone. Therefore it must be very sensitive against additional stresses, be these of a mechanical or thermal nature. This contributed to the fragmenting of the roll face.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0091757
EISBN: 978-1-62708-232-7
Abstract
A kiln, 7.6 m (25 ft) long with a 1 m (3 ft) internal diameter and a 6.3 mm (0.25 in.) wall thickness, is used to regenerate spent charcoal returned by water utilities. This charcoal contains up to 0.57% S and 2.04% Cl. The kiln is made of Inconel 601 (N06601) welded using Inconel 617 (N06617) as a filler alloy. Wet charcoal is fed in at one end of the kiln and travels while being tumbled within the inclined rotating vessel. Temperatures range from 480 deg C (900 deg F) (Zone 1) to 900 deg C (1650 deg F) (Zones 2 and 3). Steam is introduced at the discharge end at 95 g/s (750 lb/h), 34 to 69 kPa (5 to 10 psi), and 125 deg C (260 deg F). The kiln developed perforations within eight months of operation. Investigation (visual inspection, metallurgical analysis, energy-dispersive spectroscopy, and 44X micrographs) supported the conclusion that the sulfur and chlorine in the charcoal attacked the Inconel 601, forming various sulfides and chlorides. Recommendations included on-site testing, and installation of test coupons of various alloys before fabricating another kiln. The suggested alloys were RA85H, 800HT, HR-120, Haynes 556, and HR-160.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001225
EISBN: 978-1-62708-232-7
Abstract
Three radially-cracked disks that circulated the protective gases in a bell-type annealing furnace were examined. During service they had been heated in cycles of 48 h to 720 deg C for 3 h each time, then were kept at temperature for 15 h followed by cooling to 40 deg C in 30 h, while rotating at 1750 rpm. Two disks were cracked at the inner face of the sheet metal rim while the rim of the third was completely cracked through. An analysis of the sheet metal rim of one of the disks showed the following composition: 0.06C, 1.98Si, 25.8Cr, and 35.8Ni. A steel of such high chromium content was susceptible to s-phase formation when annealed under 800 deg C. The material selected was therefore unsuitable for the stress to be anticipated. In view of the required oxidation resistance, a chromium-silicon or chromium-aluminum steel with 6 or 13% Cr would have been adequate. If the high temperature strength of these steels proved inadequate, an alloy lower in chromium would have been preferable.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001668
EISBN: 978-1-62708-232-7
Abstract
A detailed investigative failure analysis was conducted on an autoclave which blew apart in a furnace for no apparent reason. Bolt failure resulted in separation of the autoclave lid and subsequent destruction of the furnace. Analysis using metallography, fractography, mechanical testing and exemplar tests were performed on the bolt material. Mechanical engineering analysis and leak-before-break criteria were extensively analyzed. Results led to only one possible conclusion: that an explosion occurred within the autoclave. Suggestions for autoclave design are presented as a result of the analysis.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001238
EISBN: 978-1-62708-232-7
Abstract
Heating elements, consisting of strips, 40 mm x 2 mm, of the widely used 80Ni-20Cr resistance heating alloy, and designed to withstand a temperature of 1175 deg C, were rendered unusable by scaling after a few months service in a through-type annealing furnace, Although the temperature supposedly did not exceed 1050 deg C. Structural observations indicated a special case of internal oxidation. The required conditions for this were apparently provided by the moist hydrogen atmosphere of the annealing furnace, in which the chromium was oxidized, while the oxides of iron and nickel were reduced. Even the carbon suffered incomplete combustion and was enriched in the core. Thus, no protective layer could form or be maintained. The intergranular advancement of the oxidation may have been favored by the precipitation of chromium-rich carbides on the austenite grain boundaries. This form of internal oxidation is, in the case of Ni-Cr alloys, known as green rot. Alloys containing iron should be more resistant. As a preventive measure it was recommended to reduce the operating temperature of the strip sufficiently to allow the use of Fe-Ni-Cr alloys.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001490
EISBN: 978-1-62708-232-7
Abstract
A steel pot used as crucible in a magnesium alloy foundry developed a leak that resulted in a fire and caused extensive damage. Hypotheses as to the cause of the leak included a defect in the pot, overuse, overheating, and poor foundry practices. Scanning electron microscopy, transmission electron microscopy, optical microscopy, and x-ray microanalysis in conjunction with dimensional analysis, phase diagrams and thermodynamics considerations were employed to evaluate the various hypotheses. All evidence pointed to an oxide mass in the area where the hole developed, likely introduced during the steelmaking process.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001231
EISBN: 978-1-62708-232-7
Abstract
The rim of a gear wheel of 420 mm width and 3100 mm in diam broke after four years of operation time in a sheet bar three-high rolling mill. The rim was forged from steel with about 0.4C, 0.8Si and 1.1Mn. The rim started to break in the tooth bottom from a fatigue fracture which extended from the gear side to more than half the rim width. A second incipient failure commenced from the opposite tooth bottom. Both fractures joined below the tooth of the rim. Both incipient cracks were fatigue fractures with several starting points, all located in the transition between tooth flank and tooth bottom. The remaining failure was a fine-grained ductile fracture. It was found that the teeth were not supported uniformly over the entire width and were thus overloaded on one side. The transition from the tooth flanks to the tooth bottom was sharp-edged, causing a tension peak there. The tooth bottom was machined only roughly. Also, the yield point was a little bit too low.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001513
EISBN: 978-1-62708-232-7
Abstract
While in the stationary mode, capillary action at the contact line between roller and race in a steel rolling mill taper bearing caused a concentration of lubricant and moisture to occur. This lead to lines of corrosion pits at roller intervals. During subsequent operation, the individual corrosion pits acted as stress raisers and initiated coarse grain spalling. Due to a bending moment on the rotating element, this in turn initiated bending fatigue normal to the longitudinal axis, which propagated through to the bore of the inner ring. Stain marks were visible in the bore at a spacing corresponding to roller intervals where lubricant had flowed through the cracks from the race.