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Printing machinery
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c9001551
EISBN: 978-1-62708-233-4
Abstract
A multi-million dollar, four-color printing press used to produce a major weekly magazine was breaking pinions (shouldered shafts) on rolls. The cause of fracture was cyclic fatigue. Steel quality and heat treatment met expected standards. The pinion fracture showed multiple origins indicating rotational vibration fatigue. Keeping bolts tight solved this problem. In another case, grinding machines were unable to produce surfaces of uniform quality and smoothness on steel bearing products. Measurements showed that self-excited vibrations were created when particular steels were ground. It was found that the natural frequency of the wheel truing device was the culprit. A tuned damped absorber was designed and built to modify the resonance. This eliminated the problem.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0051292
EISBN: 978-1-62708-225-9
Abstract
Type 302 stainless steel springs used in a printing operation failed by breaking into several pieces after two months in service. The springs were operating over a very small deflection and were regulating the flow of ink, in which they were constantly immersed. Fatigue fractures on every piece of the spring were revealed by visual examination. Each of the fractures was found to be oriented at 45 deg to the wire axis. Clear evidence of pitting corrosion at the fatigue fracture origin was also observed. Free chloride ions were revealed to be present in the ink in which the spring was operating. An alternative ink that contained no free chloride ions was recommended.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001267
EISBN: 978-1-62708-215-0
Abstract
Music wire springs used in a printer return mechanism failed near the bend in the hook portion of the spring during qualification testing. Samples were examined in a scanning electron microscope equipped with an energy-dispersive x-ray microprobe. Fatigue fractures originated at rub marks on the inside edge of the spring. An investigation of loads encountered in service indicated that the springs had been loaded to a large fraction of the yield strength. Redesign of the spring mechanism was recommended.