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Offshore rig platforms
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001672
EISBN: 978-1-62708-236-5
Abstract
Failed ferrous components were analyzed from a crane that operated on an offshore platform. The crane failed during operation and fell into the sea. The brake spring on the boom hoist was found to have fractured in four places. The spring contained a line defect (seam) that was the source of each crack. The fracture of the oil quenched and tempered (HRC 50 ASTM A229) spring was by stress-corrosion cracking after the crane fell into the sea because fatigue cannot account for the fractures observed. The crane failure was caused by an overload created by the operator catching a free-falling load.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001167
EISBN: 978-1-62708-228-0
Abstract
Visual examination, optical and scanning electron microscopy were used to determine the cause of failure in the connector groove of a marine riser coupling. The specified steel was AISI 4142 (0.40 to 0.45% C; 0.75 to 1.00% Mn; 0.20 to 0.35% Si; 0.80 to 1.10% Cr; 0.15 to 0.25% Mo) normalized from 9000C. Microscopic examination revealed the crack's initiation point and subsequent propagation. SEM examination of chemically stripped corrosion showed that corrosion fatigue and stress corrosion might have contributed to the initial slow crack growth. Impact tests revealed a fracture transition temperature in excess of 1000C. The sequence of events leading to failure was detailed. The main recommendation was to quench and temper existing couplings and to use a lower carbon quenched and tempered steel for new couplings.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001114
EISBN: 978-1-62708-214-3
Abstract
An API type 2 steel clamp located on the riser of a semisubmersible drilling rig between the lower ball joint and riser blowout preventer (BOP) conductor failed after 7 years of service. Failure analysis revealed the cause of failure to be the low toughness of the clamp material. Contributing factors included the presence of a hard, brittle, heat-affected zone and weld defects at the handling pad eye. It was recommended that the replacement clamp be made from a material with good toughness and that any installation of attachments by welding be done according to qualified procedures.