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Luther M. Gammon, Michael V. Hyatt, G. Hari Narayanan, Henry J. Oberson, Harcayal B. Singh
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Wrought aluminum alloys
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.machtools.c9001183
EISBN: 978-1-62708-223-5
Abstract
In a continuously cast aluminum press stud, two small foreign metal slivers were found that had caused difficulties with the cable sheathing press. Spectroscopic examination revealed the slivers consisted of a chromium-molybdenum-vanadium steel with minor (unintentional) additions of copper, nickel, and cobalt. A steel of similar composition, X38Cr-MoV5 1 (W-No. 2343) was used for hot working tools. The sliver originated from a damaged press tool.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001695
EISBN: 978-1-62708-229-7
Abstract
Large quantities of aluminum-clad spent nuclear materials have been in interim storage in the fuel storage basins at The Savannah River Site while awaiting processing since 1989. This extended storage as a result of a moratorium on processing resulted in corrosion of the aluminum clad. Examinations of this fuel and other data from a corrosion surveillance program in the water basins have provided basic insight into the corrosion process and have resulted in improvements in the storage facilities and basin operations. Since these improvements were implemented, there has been no new initiation of pitting observed since 1993. This paper describes the corrosion of spent fuel and the metallographic examination of Mark 31A target slugs removed from the K-basin storage pool after 5 years of storage. It discusses the SRS Corrosion Surveillance Program and the improvements made to the storage facilities which have mitigated new corrosion in the basins.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001710
EISBN: 978-1-62708-229-7
Abstract
Aluminum-clad spent nuclear fuel is stored in water filled basins at the Savannah River Site awaiting processing or other disposition. After more than 35 years of service underwater, the aluminum storage racks that position the fuel bundles in the basin were replaced. During the removal of the racks from the basin, a failure occurred in one of the racks and the Savannah River Technology Center was asked to investigate. This paper presents the results of the failure analysis and provides a discussion of the effects of corrosion on the structural integrity of the storage racks.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0091350
EISBN: 978-1-62708-227-3
Abstract
Cracks occurred in a new ship hull after only three months in service. It was noted that the 5xxx series of aluminum alloys are often selected for weldability and are generally very resistant to corrosion. However, if the material has prolonged exposure at slightly elevated temperatures of 66 to 180 deg C (150 to 350 deg F), an alloy such as 5083 can become susceptible to intergranular corrosion. Investigation (visual inspection, corrosion testing, SEM images) supported the conclusion that the cracks occurred because during exposures to chloride solutions like seawater, galvanic couples formed between precipitates and the alloy matrix, leading to severe intergranular attack. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0091669
EISBN: 978-1-62708-227-3
Abstract
During a routine inspection, cracks were discovered in several aluminum alloy (similar to either 2014 or 2017) coupling nuts on the fuel lines of a missile. The fuel lines had been exposed to a marine atmosphere for six months while the missile stood on an outdoor test stand near the seacoast. A complete check was then made, both visually and with the aid of a low-power magnifying glass, of all coupling nuts of this type on the missile. Investigation (visual inspection, spectrographic and chemical analysis, and metallographic examination) supported the conclusion that the cracking of the aluminum alloy coupling nuts was caused by stress corrosion. Contributing factors included use of a material that is susceptible to this type of failure, sustained tensile stressing in the presence of a marine (chloride-bearing) atmosphere, and an elongated grain structure transverse to the direction of stress. The elongated grain structure transverse to the direction of stress was a consequence of following the generally used procedure of machining this type of nut from bar stock. Recommendations included changing the materials specification for new coupling nuts for this application to permit use of only aluminum alloys 6061-T6 and T651 and 2024-T6, T62, and T851.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001140
EISBN: 978-1-62708-227-3
Abstract
Several pressurized air containers (i.e., diving tanks) made of non-heat-treatable Al-5Mg aluminum alloy failed catastrophically. Catastrophic failure occurred when a subcritical stress corrosion crack reached a critical size. Critical crack size for unstable propagation was reached prior to wall penetration, which could have led to subsequent loss of pressure, resulting in explosion of the cylinder. It was recommended that more stress corrosion resistant alloys be used for sea diving applications. Furthermore, cylinders should have a reduced wall thickness that can be determined employing the “leak-before-break” design philosophy, developed using fracture mechanics, to eliminate the possibility of catastrophic ruptures.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0047199
EISBN: 978-1-62708-234-1
Abstract
The lower receiver of the M16 rifle is an anodized forging of aluminum alloy 7075-T6. Degradation of the receivers was observed after three years of service in a hot, humid atmosphere. The affected areas were those in frequent contact with the user's hands. There was no question that the material failed as a result of exfoliation corrosion, so an investigation was undertaken, centered around the study of thermal treatments that would increase the exfoliation resistance and still develop the required 448 MPa (65 ksi) yield strength. The results of the study concluded that rolled bar stock should be preferred to extruded bar stock. Differences in grain structure of the forgings, as induced by differences in thermal-mechanical history of the forged material, can have a significant effect on susceptibility to exfoliation corrosion. Regarding thermal treatment, the results show conclusively that large changes in strength and exfoliation characteristics of 7075 forgings can be induced by changes in temperature or time of thermal treatment. With regard to the effect of quenching rate on exfoliation characteristics, a cold-water quench below 25 deg C (75 deg F) would appear to be far superior to an elevated-temperature quench to minimize exfoliation for 7075 forgings in the T6 temper.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001691
EISBN: 978-1-62708-234-1
Abstract
The Advanced Photon Source (APS) is a state-of-the-art synchrotron light source. The storage ring vacuum chamber is fabricated from 6061 extruded aluminum. Water connections to the vacuum chambers that were fabricated from 3003 aluminum had developed water leaks, which were subsequently remedied after considerable investigations.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046418
EISBN: 978-1-62708-234-1
Abstract
Equipment in which an assembly of in-line cylindrical components rotated in water at 1040 rpm displayed excessive vibration after less than one hour of operation. The malfunction was traced to an aluminum alloy 6061-T6 combustion chamber that was part of the rotating assembly. Analysis (visual inspection, 100x/500x/800x micrographic examination, spectrographic analysis, and hardness testing) supported the conclusions that, as a result of improper heat treatment, the combustion-chamber material was too soft for successful use in this application. Misalignment of the combustion chamber and one or both of the mating parts resulted in eccentric rotation and the excessive vibration that caused malfunction of the assembly. Irregularities in the housing around the combustion chamber and temperature variation relating to the combustion pattern in the chamber were considered to be possible contributing factors to localization of the cavitation erosion. Recommendations included adopting inspection procedures to ensure that the specified properties of aluminum alloy 6061-T6 were obtained and that the combustion chamber and adjacent components were aligned within specified tolerances. In a similar situation, consideration should also be given to raising the pressure in the coolant in order to suppress the formation of cavitation bubbles.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001516
EISBN: 978-1-62708-234-1
Abstract
This paper deals with disk drive failures that occur in the interface area between the head and disk. The failures often lead to the loss of stored data and are characterized by circumferential microscratches that are usually visible to the unaided eye. The recording media in disk drives consists of a metal, glass, ceramic, or plastic substrate coated with a magnetic material. Data errors are classified as ‘soft’ or ‘hard’ depending on their correctability. Examination has shown that hard errors are the result of an abrasive wear process that begins with contact between head and disk asperities. The contact generates debris that, as it accumulates, increases contact pressure between the read-write head and the surface of the disk. Under sufficient pressure, the magnetic coating material begins wearing away, resulting in data loss.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001537
EISBN: 978-1-62708-234-1
Abstract
After completing a fatigue test of an aluminum alloy component machined from a 7079-T6 forging, technicians noted a 5 in. crack which ran longitudinally above and through the flange. When the fracture face was examined by light microscopy, observers could not ascertain the exact mode of fracture. Electron fractography revealed that five different modes of crack growth were operative as the part failed. Region 1 was a shallow zone (about 0.002 in. at its deepest) of dimpled structure typical of an overload failure. Region 2 was a zone that grew by a stress corrosion mechanism. Through a fatigue mechanism was operative in Region 3, it was not the cause of the large crack. Region 4, which covered 50% of the fracture area, developed mainly by stress corrosion. This zone gradually changed into the combination of intergranular and transgranular overload in Region 5, which covered approximately the remaining 50% of the fracture. Apparently, after stress corrosion moved halfway through, the part failed by overload. This failure analysis proved that a crack, originally thought to be a fatigue failure, was actually a stress corrosion crack.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001455
EISBN: 978-1-62708-234-1
Abstract
Aluminum alloy BS.1476-HE.15 by virtue of its high strength and low density finds application in the form of bars or sections for cranes, bridges, and other such structures where a reduction in dead weight load and inertia stresses is advantageous. Bars and sections in H.15 alloy are mostly produced by extrusion. Some material processed this way has been prone to exfoliation corrosion. Extended aging for 24 h at a temperature of 185 deg C (365 deg F) virtually suppresses the tendency for exfoliation corrosion to develop. Also, the use of a sprayed coating, either of aluminum or Al-1Zn alloy, was effective in halting and preventing this form of attack. While alarming, the appearance of exfoliation corrosion provides a valuable warning to the engineer or inspector before a severe weakening of the particular sections has occurred.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001734
EISBN: 978-1-62708-234-1
Abstract
An aircraft engine in which an in-flight fire had occurred was dismantled and examined. A bracket assembly fabricated from 2024 aluminum, one of several failed components, was of prime interest because of apparent heat damage. Scanning electron microscopy was used to compare laboratory-induced fractures made at room and elevated temperatures with the bracket failure. The service failure exhibited grain separation and loss of delineation of the grain boundaries due to melting. SEM revealed deep voids between grains and tendrils that connected grains, which resulted from surface tension during melting. Microscopic examination of polished, etched section through the fractured surface verified intergranular separation and breakdown of grain facets. The absence of any reduction of thickness on the bracket assembly at the point of fracture, along with evidence of intense heat at this point, indicated that little stress had been applied to the part. Comparisons of the service failure and laboratory-induced failures in conjunction with macroscopic and metallographic observations showed that the bracket assembly failed because an intense, localized flame had melted the material.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001510
EISBN: 978-1-62708-217-4
Abstract
Proper stress analysis during component design is imperative for accurate life and performance prediction. The total stress on a part is comprised of the applied design stress and any residual stress that may exist due to forming or machining operations. Stress-corrosion cracking may be defined as the spontaneous failure of a metal resulting from the combined effects of a corrosive environment and the effective component of tensile stress acting on the structure. However, because of the orientation dependence in aluminum, it is the residual stress occurring in the most susceptible direction that must be considered of primary importance in material selection for design configuration. A Navy UH-1N helicopter main rotor blade grip manufactured from a 2014-T6 aluminum alloy forging failed because of a design flaw that left a high residual tensile stress along the short transverse plane; this in turn provided the necessary condition for stress corrosion to initiate. A complete failure investigation to ascertain the exact cause of the failure was conducted utilizing stereomicroscopic examination, scanning electron microscopy, metallographic inspection and interpretation, energy-dispersive chemical analysis, physical and mechanical evaluation. Stereomicroscopic examination of the opened crack fracture surface revealed one large fan-shaped region that had propagated radially through the thickness of the material from two distinct origin areas on the internal diam of the grip. Higher magnification inspection near the origin area revealed a flat, wood-like appearance. Scanning electron microscopy divulged the presence of substantial mud cracking and intergranular separation on the fracture surface. Metallographic examination revealed intergranular cracking and substantial leaf separation along the elongated grains parallel to the fracture surface. Chemical composition and hardness requirements were found to be as specified. The blade grip failed due to a stress corrosion crack which initiated on the inner diam and propagated in the short transverse direction through the thickness of the component. The high residual tensile stress in the part resulting from the forging and exposed after machining of the inner diam, combined with the presence of moisture, provided the necessary conditions to facilitate crack initiation and propagation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001747
EISBN: 978-1-62708-217-4
Abstract
This report covers case histories of failures in fixed-wing light airplane and helicopter components. In a 2025-T6 or 2219 aluminum alloy propeller blade that failed near the tip, cracks started on the leading edge at surface damage in the critical area-the zone between 4 and 10 in. from the tip of the blade. Incorrect dressing and inadequate pre-flight inspection were the two main causes. Two other types of propeller blade fatigue failures resulted mainly from propeller straightening operations, usually performed after previous blade bending damage. To eliminate blade tip failures, all surface-damaged material should be removed and polished smooth before further flight. The blade should be correctly dressed. Also, the tachometer should be calibrated to ensure the engine/propeller combination is not operated in the critical speed range at normal cruising speeds.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006387
EISBN: 978-1-62708-217-4
Abstract
A routine examination on a seat ejection system found that the catapult attachment swivel fabricated from 7075-T651 aluminum alloy plate contained cracks on opposite sides of the part. This swivel, or bath tub, does not experience extreme loads prior to activation of the catapult system. Some loads could be absorbed however, when the aircraft is subjected to G loads. Visual examination of the part revealed that cracks through the wall thickness initiated on the inner walls of the fixture. Scanning electron microscopy (SEM) and electron optical examination revealed that the cracking pattern initiated and progressed by an intergranular failure mechanism. It was concluded that failure of the catapult attachment swivel fixture occurred by SCC. It was recommended that the 7075 aluminum ejection seat fixture be supplied in the T-73 temper to minimize susceptibility to SCC.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0091674
EISBN: 978-1-62708-217-4
Abstract
Forged aluminum alloy 2014-T6 hinge brackets in naval aircraft rudder and aileron linkages were found cracked in service. The cracks were in the hinge lugs, adjacent to a bushing made of cadmium-plated 4130 steel. Investigation (visual inspection and 250X micrographs) supported the conclusion that the failure of the hinge brackets occurred by SCC. The corrosion was caused by exposure to a marine environment in the absence of paint in stressed areas due to chipping. The stress resulted from the interference fit of the bushing in the lug hole. Recommendations included inspecting all hinge brackets in service for cracks and for proper maintenance of paint. Also suggested was replacing the aluminum alloy 2015-T6 with alloy 7075-T6, and surface treatment for the 7075-T6 brackets was recommended using sulfuric acid anodizing and dichromate sealing. Finally, it was also recommended that the interference fit of the bushing in the lug hole be discontinued.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006398
EISBN: 978-1-62708-217-4
Abstract
Inspections and microstructural analysis revealed intergranular corrosion of 6061-T6 aluminum alloy aircraft fuel line beneath ferrules. The cause of the corrosion was traced to the fuel line marking process, which involved electrolytic labeling. Although subsequent rinsing of the fuel lines washed off most of the electrolyte, some was trapped between the 6061-T6 tubing and the ferrule. This condition made intergranular corrosion of the fuel lines inevitable. The attack caused grains to become dislodged, giving the appearance of pitting. Corrosion penetrated approximately 0.13 mm (0.005 in.) into the tubing. Experiments indicated that the corrosion products were inactive. It was recommended that another marking process be used that does not involve corrosive materials. The prevention of electrolyte from being trapped between the tubing and ferrules by using a MIL-S-8802 sealant was recommended.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001529
EISBN: 978-1-62708-217-4
Abstract
On 16 July 1999, a Boeing 737-800 on final approach for landing sustained a major lightning strike. Damage to the fuselage structure primarily was in the form of melting or partial melting of widely-separated rivets and adjacent Alclad 2024-T3 fuselage skin. The damage was confined to a 0.25-in. (6.4-mm) radii around the affected rivets. The repair process involved removal of the locally-affected material and addition of a skin doubler to restore the aircraft structure to the originally designed condition. Damage features are described briefly.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047636
EISBN: 978-1-62708-217-4
Abstract
Several elbow subassemblies comprising segments of oil-line assemblies that recycled aircraft-engine oil from pump to filter broke in service. The components of the subassemblies were made of aluminum alloy 6061-T6. Two subassemblies were returned to the laboratory to determine cause of failure. In one, the threaded boss had separated from the elbow at the weld. In the other, the failure was by fracture of the elbow near the flange. The separation of the threaded boss from the elbow was due to a poor welding procedure. Crack propagation was accelerated by fatigue caused by cyclic service stresses. The fracture of the second elbow near the flange was caused by overaging during repair welding of the boss weld. Satisfactory weld penetration was achieved by improved training of the welders plus more careful inspection. Repair welding was prohibited, to avoid recurrence of overaging from the welding heat. Additional support for the oil line was installed to reduce vibration and minimize fatigue of the elbow.
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