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R. Bradley, S. Ahmad
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Tito Luiz da Silveira, Francisco Solano Moreira, Miriam Conçeicão Garcia Chavez, Iain Le May
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R.J. Gommans, K.F. Verheesen, J.H. Heerings
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Wrought iron-based superalloys
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Book Chapter
Failure of a Transfer Line on an Ethane Cracking Furnace Due to Sulfidation
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001638
EISBN: 978-1-62708-228-0
Abstract
An Incoloy 800H (UNS N08810) transfer line on the outlet of an ethane-cracking furnace failed during decoking of the furnace tubes after nine years in service. A metallographic examination using optical and scanning electron microscopy as well as energy-dispersive x-ray spectroscopy revealed that the failure was due to sulfidation. The source of the sulfur in the furnace effluent was either dimethyl disulfide, injected into the furnace feed to prevent coke formation and carburization of the furnace tubes, or contamination of the feed with sulfur bearing oil.
Book Chapter
Failure of an Incoloy 800 Piping System
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046991
EISBN: 978-1-62708-234-1
Abstract
The outlet-piping system of a steam-reformer unit failed by extensive cracking at four weld locations. The welded system consisted of Incoloy 800 (Fe-32Ni-21Cr-0.05C) pipe and fittings. The exterior surfaces of the system were insulated with rock wool that did not contain weatherproofing. On-site visual examination and magnetic testing indicated severe external corrosion of most of the piping. The system showed extensive cracking in weld HAZ. One specimen indicated that corrosion extended to a depth of 3.2 mm and cracks were seen at the edge of the cover bead and in the HAZ of the weld. Metallographic examination showed that cracking was intergranular and that adjacent grain boundaries had undergone deep intergranular attack. Examination at higher magnification revealed heavy carbide precipitation, primarily at grain boundaries, indicating that the alloy had been sensitized, which resulted from heating during welding. Electron probe x-ray microanalysis showed the outside surface of the tube did not have the protective chromium oxide scale normally found on Incoloy 800. The inside surface of the tube had a thin chromium oxide protective scale. This evidence supported the conclusions that the deep oxidation greatly decreased the strength of the weld HAZ and cracking followed.
Book Chapter
Metallographic Studies of a Reformer Tube Failure Due to Thermal Fatigue
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001675
EISBN: 978-1-62708-220-4
Abstract
The failure of a reformer tube furnace manifold has been examined using metallography. It has been shown that the cause of failure was thermal fatigue; the damage was characterized by the presence of voids produced by creep mechanisms operating during the high temperature cycle under high local stress. The study indicates that standard metallographic procedures can be used to identify failure modes in high temperature petrochemical plants.
Book Chapter
Oxidation Cracking and Residual Creep Life of an Incoloy 800H Bottom Manifold in a Steam Reformer at 800 °C
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001738
EISBN: 978-1-62708-220-4
Abstract
During a planned shut-down in 1990 it appeared that the bottom manifold parts made of wrought Incoloy 800H had undergone diametrical expansion of up to 2% due to creep. Further, cracking at the outer diam was found. It was decided to replace these parts. Microscopical investigations showed that the cracking could not be caused by creep. It was found that the cracking was confined to a 4-mm deep coarse-grained zone (ASTM 0-1) at the outer diameter. The cracking appeared to be caused by strain-induced intergranular oxidation. When the cracks reached the fine-grained material, the oxidation-cracks stopped. To determine the residual creep life of the sound (non-cracked) bottom manifold material, iso-stress creep tests were performed. It was found that tertiary creep started at 7% strain. The time-to-rupture was greater than 100,000 h. It was concluded that the bottom manifold (and thus the furnace) could be used safely during the foreseen production period.